ENS 50587: Difference between revisions

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| event date = 11/01/2014 02:48 EDT
| event date = 11/01/2014 02:48 EDT
| last update date = 11/01/2014
| last update date = 11/01/2014
| title = Dual Unit Manual Reactor Trips Due To Lowering Condenser Vacuum And Degraded Forebay
| title = Dual Unit Manual Reactor Trips Due to Lowering Condenser Vacuum and Degraded Forebay
| event text = On November 1, 2014, at 0249 [EDT], DC Cook Unit 1 reactor was manually tripped and at 0248 [EDT] DC Cook Unit 2 was manually tripped due lowering condenser vacuum caused by degraded forebay conditions (observed thick grass and sand).  U-1 and U-2 entered Abnormal Operating Procedure for Degraded Forebay on November 1, 2014 at 0153 [EDT]. Conditions degraded in U-1 and U-2 until all but 2 screens in each unit were tripped on overload and main condenser vacuum was lowering.  U-1 and U-2 met criteria in the Degraded Forebay procedure to remove the units from service and remove all circulating water pumps from service.
| event text = On November 1, 2014, at 0249 [EDT], DC Cook Unit 1 reactor was manually tripped and at 0248 [EDT] DC Cook Unit 2 was manually tripped due lowering condenser vacuum caused by degraded forebay conditions (observed thick grass and sand).  U-1 and U-2 entered Abnormal Operating Procedure for Degraded Forebay on November 1, 2014 at 0153 [EDT]. Conditions degraded in U-1 and U-2 until all but 2 screens in each unit were tripped on overload and main condenser vacuum was lowering.  U-1 and U-2 met criteria in the Degraded Forebay procedure to remove the units from service and remove all circulating water pumps from service.
This event is reportable under 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation, as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight (8) hour report.
This event is reportable under 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation, as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight (8) hour report.

Latest revision as of 20:49, 1 March 2018

ENS 50587 +/-
Where
Cook American Electric Power icon.png
Michigan (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.75 h-0.0729 days <br />-0.0104 weeks <br />-0.0024 months <br />)
Opened: Perry Graham
05:03 Nov 1, 2014
NRC Officer: Daniel Mills
Last Updated: Nov 1, 2014
50587 - NRC Website
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