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i BYRON NUCLEAR PONER STATIOM UNIT 1 AND UNIT 2 MONTHLY PERTORMANCE REPORT CODNOtmCALTH EDISON COMPANY
BYRON NUCLEAR PONER STATIOM UNIT 1 AND UNIT 2 MONTHLY PERTORMANCE REPORT CODNOtmCALTH EDISON COMPANY
?
?
NRC DOCKET 110. 050-454 NRC DOCKET NO. 050-455 LICENSE NO. NPF-37 LICENSE NO. NPF-66                                                                                                 ,
NRC DOCKET 110. 050-454 NRC DOCKET NO. 050-455 LICENSE NO. NPF-37 LICENSE NO. NPF-66 r
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I i
PDR               ADOCK 05000454                                                                                                                                                                                   !
l 8809190247 880831 PDR ADOCK 05000454 R
R                                                      PNU                       .
PNU c
c (0625M/0062M-2)
(0625M/0062M-2)


          'f.             '
'f.
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  !                            I. Monthly Report . fat. Byron _. Unit .1.for. tht_Ronth of August 191Jt,             [
Monthly Report. fat. Byron _. Unit.1.for. tht_Ronth of August 191Jt,
i A. .. Summary _.sLpperating Experlenes ,for _ Unit i The unit began this reporting period in Mode 1 at 92% power.             The unit
[
  ,                                operated at power levels of up to 98% until 8/4/88 at 004*/ when a reactor trip occurred (grid stability trip).           The reactor was taken critical at j                                   1902 on 8/4/88 and synchronised to the grid at 0208 on 8/5/88. The unit           ;
i A... Summary _.sLpperating Experlenes,for _ Unit i The unit began this reporting period in Mode 1 at 92% power.
4 operated at power levels of up to 98% for the rest of the reporting period.
The unit operated at power levels of up to 98% until 8/4/88 at 004*/ when a reactor trip occurred (grid stability trip).
The reactor was taken critical at j
1902 on 8/4/88 and synchronised to the grid at 0208 on 8/5/88.
The unit 4
operated at power levels of up to 98% for the rest of the reporting period.
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(0625N/0062M-3)
(0625N/0062M-3)


h_. OPERATING DATA REPORT DOCKET NO.               050-454 UNIT:             Byron One DATE: 09/10/88 COMPILED BY:             D. J. Spitzer TELEPHONE:               (61S)234-5441 x2023 OPERAT?i30 STATUS
h_. OPERATING DATA REPORT DOCKET NO.
: 1.     Reporting Period: August 1988. Gross Hours         744
050-454 UNIT:
: 2.     Currently Authorised Power Level 3411 (MWt)
Byron One DATE: 09/10/88 COMPILED BY:
D. J. Spitzer TELEPHONE:
(61S)234-5441 x2023 OPERAT?i30 STATUS 1.
Reporting Period: August 1988. Gross Hours 744 2.
Currently Authorised Power Level 3411 (MWt)
Design Electrical Rating: 11/5 (MWe-gross)
Design Electrical Rating: 11/5 (MWe-gross)
Design Electrical Rating: 1120 (Hhe-net)                                                                                         ,
Design Electrical Rating: 1120 (Hhe-net)
Max Dependable Capacity: 1105 (MWe-net)
Max Dependable Capacity: 1105 (MWe-net) 3.
: 3.     Power Level to Which Restricted (If Any): 1097 (MWe-net)
Power Level to Which Restricted (If Any): 1097 (MWe-net) 4.
: 4. Reasons for Restriction (If Any):       Steam Generator Split Flow (23MW)                                                         .
Reasons for Restriction (If Any):
l THIS MONTH YR TO DATE CUMULATIVE *
Steam Generator Split Flow (23MW) l THIS MONTH YR TO DATE CUMULATIVE
: 5. Report Period Hrs.                                 744           5855                                                 25944 l               6. Rx Critical Hours                                   725.7         5125.7                                               20437.7
* 5.
: 7. Rx Reserve Shutdown Hours                             0                               0                                   37.8 i
Report Period Hrs.
: 8. Hours Generator on Line                             718 6         5094.7                                               20055.7
744 5855 25944 l
: 9. Unit Reserve Shutdown Hours                               0                               0                                   0
6.
: 10. Gross Thermal Energy (MWH)                         2116529     16000060                                                 59595910
Rx Critical Hours 725.7 5125.7 20437.7 7.
: 11. Gross Elec. Energy (MWH)                           786919       5359514                                               19985291
Rx Reserve Shutdown Hours 0
: 11. Net Elec. Energy (MWH)                             745469       5060295                                               18799772     !
0 37.8 i
: 13. Acactor Service Factor                                 9/.5                     87.5                                         78.8
8.
: 14. Reactor Availability Tactor                             97.5                     87.5                                         78.9
Hours Generator on Line 718 6 5094.7 20055.7 9.
: 15. Unit Service Factor                                     96.6                     87.0                                         77.3   i
Unit Reserve Shutdown Hours 0
: 16. Unit Availability Tactor                               96.6                     87.0                                         77.3
0 0
: 17. Unit Capacity Factor (MDC not)                         90.7                   78.2                                         65.6   ,
: 10. Gross Thermal Energy (MWH) 2116529 16000060 59595910
: 18. Unit Capacity rector (DER net)                         89.5                   77.2                                         64.7
: 11. Gross Elec. Energy (MWH) 786919 5359514 19985291
: 19. Unit Forced Outage Mrs.                                 25.4           122.5                                               1034.6
: 11. Net Elec. Energy (MWH) 745469 5060295 18799772
  ;                20. Unit Forced Outage Rate                                 3.4                               2.3                                 4.9   !
: 13. Acactor Service Factor 9/.5 87.5 78.8
\                                                                                                                                                           \
: 14. Reactor Availability Tactor 97.5 87.5 78.9
: 21. Shutdowns Scheduled Over Next 6 Months 09/03/88                                                                                       i
: 15. Unit Service Factor 96.6 87.0 77.3 i
: 22. If Shutdown at End of Report Period, Estirieted Date of Startups                                                                     f 6
: 16. Unit Availability Tactor 96.6 87.0 77.3
: 17. Unit Capacity Factor (MDC not) 90.7 78.2 65.6
: 18. Unit Capacity rector (DER net) 89.5 77.2 64.7
: 19. Unit Forced Outage Mrs.
25.4 122.5 1034.6
: 20. Unit Forced Outage Rate 3.4 2.3 4.9
\\
\\
: 21. Shutdowns Scheduled Over Next 6 Months 09/03/88 i
: 22. If Shutdown at End of Report Period, Estirieted Date of Startups f
6
: 23. Units in Test Status (Prior to Commercial Operation): None l
: 23. Units in Test Status (Prior to Commercial Operation): None l
l                                                                                                                                                           ,
l
* Note - The cumulati're numbers do not reflect p4wer generated prior to commercial                                                       !
* Note - The cumulati're numbers do not reflect p4wer generated prior to commercial service.
service.                                                                                                                                 >
I l
I l
(0625M/0062H-4) l         ._          ,___ - _ ---- --    -          - _
(0625M/0062H-4) l
: c. EVERAct_DA2LY UNIT POWER LEVEL DOCKET NO.                                           050-454 UNIT                         Byron One DATE: 09/10/88 COMPILED Bt                                             D. J. Spitzer TELEPHCHE:                                         (815)234-5441                                         :
 
x2023 MONTH: August, 1988 DAY           AVERAGE DAILY POWE3 LEVEL (MWe-Net)                                                                                                                                                   '
c.
: 1.                                             1044 MW             16.                                       1068 MW
EVERAct_DA2LY UNIT POWER LEVEL DOCKET NO.
: 2.                                             1073 MW             17.                                       1064 MW                                                                   ,
050-454 UNIT Byron One DATE: 09/10/88 COMPILED Bt D. J. Spitzer TELEPHCHE:
: 3.                                             1074 MW             18.                                       1050 MW                                                           ,__
(815)234-5441 x2023 MONTH: August, 1988 DAY AVERAGE DAILY POWE3 LEVEL (MWe-Net) 1.
: 4.                                                   12_MW         19.                                       loss WW
1044 MW 16.
: 5.                                               3 80 MW           20.                                     .1086 WW                                                                       ;
1068 MW 2.
: 6.                                               728 MW           21,                                       1083 WW                                                                   I l
1073 MW 17.
: 7.                                             1042 MW             22.                                       1084 WW f       8.                                             1076 WW             23.                                       1083 WW
1064 MW 3.
: 9.                                             1082 MW             24.                                       1085 MW l
1074 MW 18.
l 10,                                           1031.MW             25,                                       1087 MW
1050 MW 4.
: 11.                                           1049 MW             26.                                       1090 MW                                                                   I l                                                                                                                                                                                                       l
12_MW 19.
: 12.                                           1068 MW             27.                                       1086 MW
loss WW 5.
: 13.                                           1067 MW             28.                                       1086 MW                                                                   :
3 80 MW 20.
: 14.                                           loss MW             29.                                       1066 MW I
.1086 WW 6.
: 15.                                           1071 WW             30.                                       1103 MW                                                             __.
728 MW 21, 1083 WW I
l                                                                                31.                                       1036 MW                                                                   j INSTRUCTIONS On this form list the average daily unit power level in MWe-Net for each day                                                                                                             1 in the reporting month. Compute to the nearest whole megawatt. These figures will be used to plot a graph for each reporting month. Note that when maximum                                                                                                             {
l 7.
dependable capacity is used for the not electrical rating of the unit there                                                                                                               !
1042 MW 22.
i              may be occasions when the daily average power level exceeds the 100% line (or                                                                                                             t the restricted power level line.) In such cases the average daily unit power output shee"; should be footnoted to explain the apparent anomaly.                                                                                                                         ,
1084 WW f
8.
1076 WW 23.
1083 WW 9.
1082 MW 24.
1085 MW l
l 10, 1031.MW 25, 1087 MW 11.
1049 MW 26.
1090 MW I
l l
12.
1068 MW 27.
1086 MW 13.
1067 MW 28.
1086 MW 14.
loss MW 29.
1066 MW I
15.
1071 WW 30.
1103 MW l
31.
1036 MW j
INSTRUCTIONS On this form list the average daily unit power level in MWe-Net for each day 1
in the reporting month.
Compute to the nearest whole megawatt.
These figures will be used to plot a graph for each reporting month. Note that when maximum
{
dependable capacity is used for the not electrical rating of the unit there i
may be occasions when the daily average power level exceeds the 100% line (or t
the restricted power level line.)
In such cases the average daily unit power output shee"; should be footnoted to explain the apparent anomaly.
(0625M/0062M-5) l
(0625M/0062M-5) l
_ . _ _ _ _ . - _ _ . ~ _ _ , , _ _ . _ . - . _ . __   _ _ . _    _ _- - _ _ _ _ _ _ _ _ _ _ , , _ . _ _ _ . _ , _ _ . _ . _ . - - - _ , _ _ . _                            _
_. _ _ _ _. - _ _. ~ _ _,, _ _. _. -. _. __


                                                                                                                                                                                    ~
~
R port Period August, 1988                                           UNIT SHUTDOtetS/REDUCTICMS
I R port Period August, 1988 UNIT SHUTDOtetS/REDUCTICMS BTRON (UNIT 1)
* BTRON           *                  * *
)
(UNIT 1)               **************************                              '
Date Typt._ Hours Reason Method f r* M-her Syse==
        )                       Date         Typt._ Hours Reason Method           f r* M-her         Syse==   C m annt   cause & Corrective Action to Prevent Recurrence
C m annt cause & Corrective Action to Prevent Recurrence 10.
: 10.     08/04/88                 F     25.4           A   3       88-005-00           Ar                 Offsite electrical distribution unit stability trip caused main generator to trip, resulting in a turbine trip causing a reactor trip.
08/04/88 F
ococo.........s o           S -mary
25.4 A
* 0C.00..........
3 88-005-00 Ar Offsite electrical distribution unit stability trip caused main generator to trip, resulting in a turbine trip causing a reactor trip.
TYPE                                     Reason                                             Methad                         System & C - nent F-Forced                                 A-Equip Failure F-Admin                           1-Manual                     Exhibit F & H S-Sched                                   B-Maint or Test G-Oper Error                       2-Manual Scram                 Instructions for C-Refus11ag           H-Other                     3-Auto Scram                 Preparation of D-Regulatory 3estriction                           4-Continued                   Data Entry Sheet E-operator Training                               5-Reduced Load               Licensee Event Report
ococo.........s o
                                                    & License Examination                           9-Other                         (LER) File (NUREG-0161)
S -mary 0C.00..........
TYPE Reason Methad System & C - nent F-Forced A-Equip Failure F-Admin 1-Manual Exhibit F & H S-Sched B-Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Refus11ag H-Other 3-Auto Scram Preparation of D-Regulatory 3estriction 4-Continued Data Entry Sheet E-operator Training 5-Reduced Load Licensee Event Report
& License Examination 9-Other (LER) File (NUREG-0161)
(0325N/0062M-6) l i
(0325N/0062M-6) l i
I l
I l
l
l


                .                                                                                                          l E. UNIout REPORTIN'3_.RgournEuzNTs (UNIT 1) for the month of Auaust 1988                               i
E.
: 1. Safety /Relhof valve operations for Unit One.
UNIout REPORTIN'3_.RgournEuzNTs (UNIT 1) for the month of Auaust 1988 i
VALVES         NO & MPE         PLANT           DESCRIPTION DAIE         AC"IUATED       ACTUATION       CQlDITICal     OF EVENT                               '
1.
None i
Safety /Relhof valve operations for Unit One.
: 2. Licensee generated changes to ODCM.   (Y/N)                                                       ,
VALVES NO & MPE PLANT DESCRIPTION DAIE AC"IUATED ACTUATION CQlDITICal OF EVENT None i
No                                                                                                 L P
2.
: 3. Indications of failed fuel.   (Y/N)
Licensee generated changes to ODCM.
Yes. I 131 = 4.5E-3 pcuries/gr.                                                                 '
(Y/N)
!                                                                                                                        t
No L
'                                                                                                                        t h
P 3.
L i
Indications of failed fuel.
i                                                                                                                       !
(Y/N)
Yes.
I 131 = 4.5E-3 pcuries/gr.
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(0625M/0062M-7) i i


T...LICElllEE EVENT REPORTS (UNIT ll The following is a tabular sumnary of all Licensee Event Reports for Byron Nuclear Power Station, Unit One, submitted during the reporting period, August 1 through August 31, 1988. This information is provided ?ursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.
T...LICElllEE EVENT REPORTS (UNIT ll The following is a tabular sumnary of all Licensee Event Reports for Byron Nuclear Power Station, Unit One, submitted during the reporting period, August 1 through August 31, 1988.
Occurrence Ligansee Event Report Ni=her   DAtt     Title of Occurrence 88-004 00                     07/16/88   Tachometer       Failure   Caused Overspeed Trip of Main reed Pump, Resulting in a Reactor Trip 88-005-00                     08/04/88   Main Generator Stability Trip I
This information is provided ?ursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.
Caused     by   Microwave Noise Resulting in a Reactor Trip i
Occurrence Ligansee Event Report Ni=her DAtt Title of Occurrence 88-004 00 07/16/88 Tachometer Failure Caused Overspeed Trip of Main reed Pump, Resulting in a Reactor Trip 88-005-00 08/04/88 Main Generator Stability Trip Caused by Microwave Noise I
Resulting in a Reactor Trip i
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4 1
4 1
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F (0625M/0062H-8) w
F (0625M/0062H-8) w


4 Ile ggnthly Reggrt for Byron Unit 2 for the raanth of August 1988 A. S -ary of Onaratina Emnerience for Unit 2 The unit began this reporting period in Mode 1 at 75% power. The unit operated at power levels of up to 95% until 8/7/88 when a load
4 Ile ggnthly Reggrt for Byron Unit 2 for the raanth of August 1988 A.
!                    reduction, for line stability, occurred. The unit operated at power l                     1evels of up to 87% for the rest of the reporting period.
S -ary of Onaratina Emnerience for Unit 2 The unit began this reporting period in Mode 1 at 75% power.
The unit operated at power levels of up to 95% until 8/7/88 when a load reduction, for line stability, occurred.
The unit operated at power l
1evels of up to 87% for the rest of the reporting period.
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                  'B . OPreATIht! DATA REPORT DOCKET NO. 050-455 UNIT:   Byron Two DATE:   09/10/88 COMPILED BY     D. J. Spitser TELEPHONE:   (815)234-5441 x2023 OPERATING STATUS                                                                       ,
'B. OPreATIht! DATA REPORT DOCKET NO.
: 1. Reporting Parlod   August 1988. Gross Hours:   744
050-455 UNIT:
: 2. Currently Authorised Power Levels 3411 (MWt)                                     L Desiga Electrical Rating: 1175 (MWe-gross)                                       !
Byron Two DATE:
09/10/88 COMPILED BY D. J. Spitser TELEPHONE:
(815)234-5441 x2023 OPERATING STATUS 1.
Reporting Parlod August 1988. Gross Hours:
744 2.
Currently Authorised Power Levels 3411 (MWt)
L Desiga Electrical Rating: 1175 (MWe-gross)
Design Electrical Rating: 1120 (MWe-not)
Design Electrical Rating: 1120 (MWe-not)
Man Dependable Capacity: 1105 (MWe-not)
Man Dependable Capacity: 1105 (MWe-not) 3.
: 3. Power Level to which Restricted (If Any):   1055 (MWe-not)                       *
Power Level to which Restricted (If Any):
: 4. Reasons for Restriction (If Any): Steam Generator Split Flow. (65 MW)
1055 (MWe-not) 4.
THIS MONTH YR TO DATE CUMULATIVE 8
Reasons for Restriction (If Any): Steam Generator Split Flow. (65 MW)
: 5. Report Period Hrs.                               744         5855         9048
THIS MONTH YR TO DATE CUMULATIVE 8 5.
: 6. Rx Critical Hours                               744         5761.9       8091.1
Report Period Hrs.
: 7. Rs Reserve Shutdowr Hours                         0           0           0
744 5855 9048 6.
: 8. Hours Generator on Line                         744         5511.2       ~/91.6
Rx Critical Hours 744 5761.9 8091.1 7.
: 9. Unit Reserve Shutdown Hours                       0           0           0
Rs Reserve Shutdowr Hours 0
: 10. Gross Thermal gnergy (MWH)                   1696191     15498916     21971080
0 0
: 11. Gross Elec. Energy (MWH)                     570435       5205408     7309719
8.
: 12. Net Elec. Energy (MWM)                       533256       4904629     6875530
Hours Generator on Line 744 5511.2
~/91.6 9.
Unit Reserve Shutdown Hours 0
0 0
: 10. Gross Thermal gnergy (MWH) 1696191 15498916 21971080
: 11. Gross Elec. Energy (MWH) 570435 5205408 7309719
: 12. Net Elec. Energy (MWM) 533256 4904629 6875530
[
[
: 13. Reacsor Service Factor                           100           98.4         89.4 j
: 13. Reacsor Service Factor 100 98.4 89.4 j
: 14. Reactor Availability Tactor                       100           98.4         80.4 !
: 14. Reactor Availability Tactor 100 98.4 80.4
: 15. Lait Service Factor                               100           94.1         86.1
: 15. Lait Service Factor 100 94.1 86.1
: 16. snit Availability Factor                         100           94.1         86.1 (
: 16. snit Availability Factor 100 94.1 86.1
: 17. Unit Capacity Tactor (MDC not)                      64.9        75.8        68.8
(
(
: 18. Unit Capacity Factor (DER not)                     64.0         74.8         67.8 j
(
: 19. Unit Forced Dutage Mrs.                             0         156.2       443.2 l
: 17. Unit Capacity Tactor (MDC not) 64.9 75.8 68.8
: 20. Unit Forced Outage Rate                             0           2.7         5.4 f
: 18. Unit Capacity Factor (DER not) 64.0 74.8 67.8 j
: 21. Shutdowns Scheduled Over Next 6 Months:   1/7/89                                 [
: 19. Unit Forced Dutage Mrs.
0 156.2 443.2 l
f
: 20. Unit Forced Outage Rate 0
2.7 5.4
: 21. Shutdowns Scheduled Over Next 6 Months:
1/7/89
[
l
l
: 22. If Shutdown at End of Report Period, Estimated Date of Startups l
: 22. If Shutdown at End of Report Period, Estimated Date of Startups l
: 23. Units in Test Status (Prior to Commercial Operation): None                       ;
: 23. Units in Test Status (Prior to Commercial Operation): None
[
[
* Note - The cumulative numbers do not reflect power generated prior to commercial   j rervice.                                                                   t i
* Note - The cumulative numbers do not reflect power generated prior to commercial j
rervice.
t i
(0625M/0062M-10)
(0625M/0062M-10)
: c. AY1EAGE._ DAILY UNIT POWER LEVEL DOCKET NO. 050-453 UNIT   Byron Two DATE: 09/10/88 COMPILED BY   D. J. Spitser TELEPHONE:   (815)234-5141 x2023 MONTH: August, 1988 DAY   AbERAGE DAILY POWER LEVEL (MWe-Net)
 
: 1.               907 MW                   16.             95s WW
c.
: 2.               1045 MW                   17.             954 MW
AY1EAGE._ DAILY UNIT POWER LEVEL DOCKET NO.
: 3.               1047 MW                   18.             926 MW
050-453 UNIT Byron Two DATE: 09/10/88 COMPILED BY D. J. Spitser TELEPHONE:
: 4.               1037 MW                   19.             861 MW
(815)234-5141 x2023 MONTH: August, 1988 DAY AbERAGE DAILY POWER LEVEL (MWe-Net) 1.
: 5.               1Q50 MW                   20.             814 MW
907 MW 16.
: 6.               1023 WW                   21,             641 WW
95s WW 2.
: 7.               739 MW                   22,             664 MW
1045 MW 17.
: 8.               833 MW                   23,             310 MW
954 MW 3.
: 9.               839 MW                   24,             309 WW
1047 MW 18.
: 10.               836 MW                   25.             310 MW
926 MW 4.
: 11.               866 WW                   26.             313 WW 12,               907 MW                   27.             280 WW
1037 MW 19.
: 13.               952 MW                   28.             254 MW               ,
861 MW 5.
: 14.               869 MW                   29.             252 MW
1Q50 MW 20.
: 15.               920 MW                   30.             241 Nw
814 MW 6.
: 31.             248 MW INSTRUCTIONS On this form list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt. These figures will be used to plot a graph for each reporting month. Note that when m<simum dependable capacity is used for the not electrica*. rating of the unit there may be occasions when the daily average power level exceeds the 100% line (or the restricted power level line.)     In such cases the average daily unit power output sheet should be footnoted to explain the apparent anomaly.
1023 WW 21, 641 WW 7.
739 MW 22, 664 MW 8.
833 MW 23, 310 MW 9.
839 MW 24, 309 WW 10.
836 MW 25.
310 MW 11.
866 WW 26.
313 WW 12, 907 MW 27.
280 WW 13.
952 MW 28.
254 MW 14.
869 MW 29.
252 MW 15.
920 MW 30.
241 Nw 31.
248 MW INSTRUCTIONS On this form list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
These figures will be used to plot a graph for each reporting month. Note that when m<simum dependable capacity is used for the not electrica*. rating of the unit there may be occasions when the daily average power level exceeds the 100% line (or the restricted power level line.)
In such cases the average daily unit power output sheet should be footnoted to explain the apparent anomaly.
(0625M/0062M-11)
(0625M/0062M-11)


                                                                                  *********eeeee**eeeeeeeeen Report Period August, 1988                   UNIT SHUTDOWNS / REDUCTIONS
*********eeeee**eeeeeeeeen Report Period August, 1988 UNIT SHUTDOWNS / REDUCTIONS BTRON e
* BTRON         e                     *
(UNIT 2)
(UNIT 2)               *********************e****
*********************e****
* Mo. Date   Ms Hours Reason Method LER Mumber System Component             C=<e & Corrective Action to Prevent Recurrente
Mo.
: 16. 08/07/88 N/A           A     5                                     Line 15501 - Line open Stability Trip Disabled ee*****eeeeeeee o     Summary
Date Ms Hours Reason Method LER Mumber System Component C=<e & Corrective Action to Prevent Recurrente 16.
* oceoceeeeeeeee.
08/07/88 N/A A
TYPE                 Reason                                   Meth^d                   System &CS nent F-Forced             A-Equip Failure F-Admin                 1-Manual                 Exhibit F & H S-Sched               B-Maint or Test G-Oper Error             2-Manual Scram           Instructions for C-Refuellag     B-Other                 3-Auto Scram             Preparation of D-Regulatory Restriction                 4-Continued               Data Entry Sheet E-Operator Training                     5-Reduced Load           Licensee Event Report
5 Line 15501 - Line open Stability Trip Disabled ee*****eeeeeeee o
                        & License Esamination                 9-Other                   (LER) File (NUREG-0161)
Summary oceoceeeeeeeee.
TYPE Reason Meth^d System &CS nent F-Forced A-Equip Failure F-Admin 1-Manual Exhibit F & H S-Sched B-Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Refuellag B-Other 3-Auto Scram Preparation of D-Regulatory Restriction 4-Continued Data Entry Sheet E-Operator Training 5-Reduced Load Licensee Event Report
& License Esamination 9-Other (LER) File (NUREG-0161)
(0325M/0062M-12)
(0325M/0062M-12)
                                                                  /
/


4 E.       UNIQUE REPORTING REQUIREMENTS (UNIT 2) for the month of Aucunt 1988
4 E.
: 1.       Safety / Relief valve operations for Unit Two.
UNIQUE REPORTING REQUIREMENTS (UNIT 2) for the month of Aucunt 1988 1.
VALVES               NO & TYPE                                                           PLANT                                 DESCRIPTION                                                     ;
Safety / Relief valve operations for Unit Two.
DATE                 ACTUATED             ACWATICM                                                             CCMDITICM                             QF EVENT                                                       ;
VALVES NO & TYPE PLANT DESCRIPTION DATE ACTUATED ACWATICM CCMDITICM QF EVENT None I
None I
i l
i l
: 2.       Licensee generated changes to ODCM.                                         (Y/N) f No                                                                                                                                                                                                                     I I
2.
i
Licensee generated changes to ODCM.
: 3.       Indications of failed fuel.                 (Y/N)
(Y/N) f No I
Yes. No steady stato data, r.
I i
3.
Indications of failed fuel.
(Y/N)
Yes.
No steady stato data, r
I d
I d
a I
a I
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l                                                                                                                                                                                                                                                             ,
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3                                                                                                                                                                                                                                                             i f
3 f
i t
i i
i i                                                                                                                                                                                                                                                           ,
t i
1 I
1 I
(0625M/0062M-13) 1 i
(0625M/0062M-13) 1 i
E f
E f
    . _ _ - - _ - . -            -.._r..___._    __-...___ _        . . . . , _  _ . _ . . _ _ _ - - _ _ , . - - - - . . . _ . - . - __- - _ _ . , , _ - _ . . . .                                    -
-.. r..


                  ,r.
,r.
LICEMBEE EVENT REPORTE fUNIT U The following is a tabular summary of all Licensee Event Reports for Byron Nuclear Power Station, Unit Two, subrnitted during the reporting period, August 1 through August 31, 1988. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.
LICEMBEE EVENT REPORTE fUNIT U The following is a tabular summary of all Licensee Event Reports for Byron Nuclear Power Station, Unit Two, subrnitted during the reporting period, August 1 through August 31, 1988.
i Occurrence 4
This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.
4 Liggggem Event Report NumhgI     W       Title of Occurrengs 88-009-00                     07/15/88   Thermal     Binding     of   Steam Generator     Preheater     Bypass Valves Resulting in Low Steam Generator Level Reactor Trip I                       88-010-00                     07/27/88   Exceeded                   Technics 1 l                                                                 Specification     Sample   Interval for     Inoperable       Radiation Monitor Due to Personnel Error i
i 4
Occurrence Liggggem Event Report NumhgI W
Title of Occurrengs 4
88-009-00 07/15/88 Thermal Binding of Steam Generator Preheater Bypass Valves Resulting in Low Steam Generator Level Reactor Trip I
88-010-00 07/27/88 Exceeded Technics 1 l
Specification Sample Interval for Inoperable Radiation Monitor Due to Personnel Error i
i t
i t
4 a
4 a
Line 260: Line 369:


W
W
  *4 ' . '          x Commoncrith Edison
*4 x Commoncrith Edison
            /            Byron Nuct:ar St: tion
') 4450 North G:rman Church Road Byron Nuct:ar St: tion
          !          ') 4450 North G:rman Church Road
/
                - 7 Byron, Illinois 61010
- 7 Byron, Illinois 61010
              %j September 10, 1988 Director, Office of Management Information and Program Control United States Nuclear Regulatory Commission Washington, D.C. 20555 AT111:       Document Control Desk Gentlemen Enclosed for ycur information is the Monthly Pe r f o rmance Report covering Byron Nuclear Power Station for the period August 1 through August 31, 1988.
%j September 10, 1988 Director, Office of Management Information and Program Control United States Nuclear Regulatory Commission Washington, D.C.
20555 AT111:
Document Control Desk Gentlemen Enclosed for ycur information is the Monthly Pe r f o rmance Report covering Byron Nuclear Power Station for the period August 1 through August 31, 1988.
Sincerely, he- --
Sincerely, he- --
R. Pleniewies Station Manager Byron Nuclear Power Station cci         A.B. Davis, NRC, Region III NRC Resident Inspector Byron Gary Wright, Ill. Dept. of Nuclear Safety T.J. Malman/K.L. Graesser H. E. Bliss Nuclear Fuel Services, PWR Plant Support L. Anastasia, Station Nuclear Engineering INPO Records Center L. Olshan - USNRC LTR         DYRON 88-0954 FILE:       2.7.200 (0625M/0062H-1)                                                         \
R. Pleniewies Station Manager Byron Nuclear Power Station cci A.B. Davis, NRC, Region III NRC Resident Inspector Byron Gary Wright, Ill. Dept. of Nuclear Safety T.J. Malman/K.L. Graesser H.
E. Bliss Nuclear Fuel Services, PWR Plant Support L. Anastasia, Station Nuclear Engineering INPO Records Center L. Olshan - USNRC LTR DYRON 88-0954 FILE:
2.7.200 (0625M/0062H-1)
\\
L}}
L}}

Latest revision as of 01:01, 11 December 2024

Monthly Operating Repts for Aug 1988 for Byron Nuclear Power Station
ML20154F085
Person / Time
Site: Byron  Constellation icon.png
Issue date: 08/31/1988
From: Pleniewicz R, Spitzer D
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
BYRON-88-0954, BYRON-88-954, NUDOCS 8809190247
Download: ML20154F085 (14)


Text

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BYRON NUCLEAR PONER STATIOM UNIT 1 AND UNIT 2 MONTHLY PERTORMANCE REPORT CODNOtmCALTH EDISON COMPANY

?

NRC DOCKET 110. 050-454 NRC DOCKET NO. 050-455 LICENSE NO. NPF-37 LICENSE NO. NPF-66 r

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l 8809190247 880831 PDR ADOCK 05000454 R

PNU c

(0625M/0062M-2)

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Monthly Report. fat. Byron _. Unit.1.for. tht_Ronth of August 191Jt,

[

i A... Summary _.sLpperating Experlenes,for _ Unit i The unit began this reporting period in Mode 1 at 92% power.

The unit operated at power levels of up to 98% until 8/4/88 at 004*/ when a reactor trip occurred (grid stability trip).

The reactor was taken critical at j

1902 on 8/4/88 and synchronised to the grid at 0208 on 8/5/88.

The unit 4

operated at power levels of up to 98% for the rest of the reporting period.

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(0625N/0062M-3)

h_. OPERATING DATA REPORT DOCKET NO.

050-454 UNIT:

Byron One DATE: 09/10/88 COMPILED BY:

D. J. Spitzer TELEPHONE:

(61S)234-5441 x2023 OPERAT?i30 STATUS 1.

Reporting Period: August 1988. Gross Hours 744 2.

Currently Authorised Power Level 3411 (MWt)

Design Electrical Rating: 11/5 (MWe-gross)

Design Electrical Rating: 1120 (Hhe-net)

Max Dependable Capacity: 1105 (MWe-net) 3.

Power Level to Which Restricted (If Any): 1097 (MWe-net) 4.

Reasons for Restriction (If Any):

Steam Generator Split Flow (23MW) l THIS MONTH YR TO DATE CUMULATIVE

  • 5.

Report Period Hrs.

744 5855 25944 l

6.

Rx Critical Hours 725.7 5125.7 20437.7 7.

Rx Reserve Shutdown Hours 0

0 37.8 i

8.

Hours Generator on Line 718 6 5094.7 20055.7 9.

Unit Reserve Shutdown Hours 0

0 0

10. Gross Thermal Energy (MWH) 2116529 16000060 59595910
11. Gross Elec. Energy (MWH) 786919 5359514 19985291
11. Net Elec. Energy (MWH) 745469 5060295 18799772
13. Acactor Service Factor 9/.5 87.5 78.8
14. Reactor Availability Tactor 97.5 87.5 78.9
15. Unit Service Factor 96.6 87.0 77.3 i
16. Unit Availability Tactor 96.6 87.0 77.3
17. Unit Capacity Factor (MDC not) 90.7 78.2 65.6
18. Unit Capacity rector (DER net) 89.5 77.2 64.7
19. Unit Forced Outage Mrs.

25.4 122.5 1034.6

20. Unit Forced Outage Rate 3.4 2.3 4.9

\\

\\

21. Shutdowns Scheduled Over Next 6 Months 09/03/88 i
22. If Shutdown at End of Report Period, Estirieted Date of Startups f

6

23. Units in Test Status (Prior to Commercial Operation): None l

l

  • Note - The cumulati're numbers do not reflect p4wer generated prior to commercial service.

I l

(0625M/0062H-4) l

c.

EVERAct_DA2LY UNIT POWER LEVEL DOCKET NO.

050-454 UNIT Byron One DATE: 09/10/88 COMPILED Bt D. J. Spitzer TELEPHCHE:

(815)234-5441 x2023 MONTH: August, 1988 DAY AVERAGE DAILY POWE3 LEVEL (MWe-Net) 1.

1044 MW 16.

1068 MW 2.

1073 MW 17.

1064 MW 3.

1074 MW 18.

1050 MW 4.

12_MW 19.

loss WW 5.

3 80 MW 20.

.1086 WW 6.

728 MW 21, 1083 WW I

l 7.

1042 MW 22.

1084 WW f

8.

1076 WW 23.

1083 WW 9.

1082 MW 24.

1085 MW l

l 10, 1031.MW 25, 1087 MW 11.

1049 MW 26.

1090 MW I

l l

12.

1068 MW 27.

1086 MW 13.

1067 MW 28.

1086 MW 14.

loss MW 29.

1066 MW I

15.

1071 WW 30.

1103 MW l

31.

1036 MW j

INSTRUCTIONS On this form list the average daily unit power level in MWe-Net for each day 1

in the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that when maximum

{

dependable capacity is used for the not electrical rating of the unit there i

may be occasions when the daily average power level exceeds the 100% line (or t

the restricted power level line.)

In such cases the average daily unit power output shee"; should be footnoted to explain the apparent anomaly.

(0625M/0062M-5) l

_. _ _ _ _. - _ _. ~ _ _,, _ _. _. -. _. __

~

I R port Period August, 1988 UNIT SHUTDOtetS/REDUCTICMS BTRON (UNIT 1)

)

Date Typt._ Hours Reason Method f r* M-her Syse==

C m annt cause & Corrective Action to Prevent Recurrence 10.

08/04/88 F

25.4 A

3 88-005-00 Ar Offsite electrical distribution unit stability trip caused main generator to trip, resulting in a turbine trip causing a reactor trip.

ococo.........s o

S -mary 0C.00..........

TYPE Reason Methad System & C - nent F-Forced A-Equip Failure F-Admin 1-Manual Exhibit F & H S-Sched B-Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Refus11ag H-Other 3-Auto Scram Preparation of D-Regulatory 3estriction 4-Continued Data Entry Sheet E-operator Training 5-Reduced Load Licensee Event Report

& License Examination 9-Other (LER) File (NUREG-0161)

(0325N/0062M-6) l i

I l

l

E.

UNIout REPORTIN'3_.RgournEuzNTs (UNIT 1) for the month of Auaust 1988 i

1.

Safety /Relhof valve operations for Unit One.

VALVES NO & MPE PLANT DESCRIPTION DAIE AC"IUATED ACTUATION CQlDITICal OF EVENT None i

2.

Licensee generated changes to ODCM.

(Y/N)

No L

P 3.

Indications of failed fuel.

(Y/N)

Yes.

I 131 = 4.5E-3 pcuries/gr.

t t

h L

i i

I l

l t

l i

4 i

r l

e i

I i

I L

I I

(0625M/0062M-7) i i

T...LICElllEE EVENT REPORTS (UNIT ll The following is a tabular sumnary of all Licensee Event Reports for Byron Nuclear Power Station, Unit One, submitted during the reporting period, August 1 through August 31, 1988.

This information is provided ?ursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.

Occurrence Ligansee Event Report Ni=her DAtt Title of Occurrence 88-004 00 07/16/88 Tachometer Failure Caused Overspeed Trip of Main reed Pump, Resulting in a Reactor Trip 88-005-00 08/04/88 Main Generator Stability Trip Caused by Microwave Noise I

Resulting in a Reactor Trip i

l 1

4 1

1 l

)

F (0625M/0062H-8) w

4 Ile ggnthly Reggrt for Byron Unit 2 for the raanth of August 1988 A.

S -ary of Onaratina Emnerience for Unit 2 The unit began this reporting period in Mode 1 at 75% power.

The unit operated at power levels of up to 95% until 8/7/88 when a load reduction, for line stability, occurred.

The unit operated at power l

1evels of up to 87% for the rest of the reporting period.

l i

l i

(0625M/0062M-9)

l

'B. OPreATIht! DATA REPORT DOCKET NO.

050-455 UNIT:

Byron Two DATE:

09/10/88 COMPILED BY D. J. Spitser TELEPHONE:

(815)234-5441 x2023 OPERATING STATUS 1.

Reporting Parlod August 1988. Gross Hours:

744 2.

Currently Authorised Power Levels 3411 (MWt)

L Desiga Electrical Rating: 1175 (MWe-gross)

Design Electrical Rating: 1120 (MWe-not)

Man Dependable Capacity: 1105 (MWe-not) 3.

Power Level to which Restricted (If Any):

1055 (MWe-not) 4.

Reasons for Restriction (If Any): Steam Generator Split Flow. (65 MW)

THIS MONTH YR TO DATE CUMULATIVE 8 5.

Report Period Hrs.

744 5855 9048 6.

Rx Critical Hours 744 5761.9 8091.1 7.

Rs Reserve Shutdowr Hours 0

0 0

8.

Hours Generator on Line 744 5511.2

~/91.6 9.

Unit Reserve Shutdown Hours 0

0 0

10. Gross Thermal gnergy (MWH) 1696191 15498916 21971080
11. Gross Elec. Energy (MWH) 570435 5205408 7309719
12. Net Elec. Energy (MWM) 533256 4904629 6875530

[

13. Reacsor Service Factor 100 98.4 89.4 j
14. Reactor Availability Tactor 100 98.4 80.4
15. Lait Service Factor 100 94.1 86.1
16. snit Availability Factor 100 94.1 86.1

(

(

17. Unit Capacity Tactor (MDC not) 64.9 75.8 68.8
18. Unit Capacity Factor (DER not) 64.0 74.8 67.8 j
19. Unit Forced Dutage Mrs.

0 156.2 443.2 l

f

20. Unit Forced Outage Rate 0

2.7 5.4

21. Shutdowns Scheduled Over Next 6 Months:

1/7/89

[

l

22. If Shutdown at End of Report Period, Estimated Date of Startups l
23. Units in Test Status (Prior to Commercial Operation): None

[

  • Note - The cumulative numbers do not reflect power generated prior to commercial j

rervice.

t i

(0625M/0062M-10)

c.

AY1EAGE._ DAILY UNIT POWER LEVEL DOCKET NO.

050-453 UNIT Byron Two DATE: 09/10/88 COMPILED BY D. J. Spitser TELEPHONE:

(815)234-5141 x2023 MONTH: August, 1988 DAY AbERAGE DAILY POWER LEVEL (MWe-Net) 1.

907 MW 16.

95s WW 2.

1045 MW 17.

954 MW 3.

1047 MW 18.

926 MW 4.

1037 MW 19.

861 MW 5.

1Q50 MW 20.

814 MW 6.

1023 WW 21, 641 WW 7.

739 MW 22, 664 MW 8.

833 MW 23, 310 MW 9.

839 MW 24, 309 WW 10.

836 MW 25.

310 MW 11.

866 WW 26.

313 WW 12, 907 MW 27.

280 WW 13.

952 MW 28.

254 MW 14.

869 MW 29.

252 MW 15.

920 MW 30.

241 Nw 31.

248 MW INSTRUCTIONS On this form list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that when m<simum dependable capacity is used for the not electrica*. rating of the unit there may be occasions when the daily average power level exceeds the 100% line (or the restricted power level line.)

In such cases the average daily unit power output sheet should be footnoted to explain the apparent anomaly.

(0625M/0062M-11)

                  • eeeee**eeeeeeeeen Report Period August, 1988 UNIT SHUTDOWNS / REDUCTIONS BTRON e

(UNIT 2)

                                          • e****

Mo.

Date Ms Hours Reason Method LER Mumber System Component C=<e & Corrective Action to Prevent Recurrente 16.

08/07/88 N/A A

5 Line 15501 - Line open Stability Trip Disabled ee*****eeeeeeee o

Summary oceoceeeeeeeee.

TYPE Reason Meth^d System &CS nent F-Forced A-Equip Failure F-Admin 1-Manual Exhibit F & H S-Sched B-Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Refuellag B-Other 3-Auto Scram Preparation of D-Regulatory Restriction 4-Continued Data Entry Sheet E-Operator Training 5-Reduced Load Licensee Event Report

& License Esamination 9-Other (LER) File (NUREG-0161)

(0325M/0062M-12)

/

4 E.

UNIQUE REPORTING REQUIREMENTS (UNIT 2) for the month of Aucunt 1988 1.

Safety / Relief valve operations for Unit Two.

VALVES NO & TYPE PLANT DESCRIPTION DATE ACTUATED ACWATICM CCMDITICM QF EVENT None I

i l

2.

Licensee generated changes to ODCM.

(Y/N) f No I

I i

3.

Indications of failed fuel.

(Y/N)

Yes.

No steady stato data, r

I d

a I

l i

l l

I t

I i

3 f

i i

t i

1 I

(0625M/0062M-13) 1 i

E f

-.. r..

,r.

LICEMBEE EVENT REPORTE fUNIT U The following is a tabular summary of all Licensee Event Reports for Byron Nuclear Power Station, Unit Two, subrnitted during the reporting period, August 1 through August 31, 1988.

This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.

i 4

Occurrence Liggggem Event Report NumhgI W

Title of Occurrengs 4

88-009-00 07/15/88 Thermal Binding of Steam Generator Preheater Bypass Valves Resulting in Low Steam Generator Level Reactor Trip I

88-010-00 07/27/88 Exceeded Technics 1 l

Specification Sample Interval for Inoperable Radiation Monitor Due to Personnel Error i

i t

4 a

i t

ll 4

I l

3 1

s I

i (0625M/0062M-14)

W

  • 4 x Commoncrith Edison

') 4450 North G:rman Church Road Byron Nuct:ar St: tion

/

- 7 Byron, Illinois 61010

%j September 10, 1988 Director, Office of Management Information and Program Control United States Nuclear Regulatory Commission Washington, D.C.

20555 AT111:

Document Control Desk Gentlemen Enclosed for ycur information is the Monthly Pe r f o rmance Report covering Byron Nuclear Power Station for the period August 1 through August 31, 1988.

Sincerely, he- --

R. Pleniewies Station Manager Byron Nuclear Power Station cci A.B. Davis, NRC, Region III NRC Resident Inspector Byron Gary Wright, Ill. Dept. of Nuclear Safety T.J. Malman/K.L. Graesser H.

E. Bliss Nuclear Fuel Services, PWR Plant Support L. Anastasia, Station Nuclear Engineering INPO Records Center L. Olshan - USNRC LTR DYRON 88-0954 FILE:

2.7.200 (0625M/0062H-1)

\\

L