ML20204J495: Difference between revisions

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{{Adams
#REDIRECT [[IR 05000413/1986024]]
| number = ML20204J495
| issue date = 07/24/1986
| title = Insp Repts 50-413/86-24 & 50-414/86-26 on 860526-0625. Violation Noted:Failure to Follow Performance Test & Instrumentation Procedures
| author name = Lesser M, Peebles T, Skinner P, Van Doorn P
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =
| addressee affiliation =
| docket = 05000413, 05000414
| license number =
| contact person =
| document report number = 50-413-86-24, 50-414-86-26, IEIN-85-033, IEIN-85-059, IEIN-85-33, IEIN-85-59, NUDOCS 8608110112
| package number = ML20204J483
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 11
}}
See also: [[see also::IR 05000413/1986024]]
 
=Text=
{{#Wiki_filter:_ _ _ _ _ _ _ _ _ _ _ _ _ - - -
                                                                                                      k
i- %-
          .
  .                                                                        UNITED STATES
        , [p "Guq'o  '
                                                                  NUCLEAR REGULATORY COMMISSION
                                                                              REGloN 11
        [                              n
                                                                      101 MARIETTA STREET, N.W.
        g                                j
        *I                              *                              ATLANTA, GEORGI A 30323
        \  * a..+ /
        Report Nos.                                50-413/86-24 and 50-414/86-26
        Licensee: Duke Power Company
                      422 South Church Street
                      Charlotte, N.C. 28242
      , Docket Nos.: 50-413 and 50-414                                                  License Nos.: NPF-35 and NPF-52
        Facility Name: Catawba 1 and 2
        Inspection Conducted: May 26 - June 25, 1986
        Inspectors:                                    ,    ,    /ArfLM          /w                          f /h
                                  P. K. Van Door'n~ g&                          6 Wdaaw/ ['                  7/ ate 'Kgn~edMfx
                                                        '      ~~
                                    PT . SKinne                              ///                              Aate'pigTied~
                                    M. S.'
                                                      r      i    14d/h .                                    fhY
                                                                                                              '/ Dale'ylgned
                                                          Lesser ' -~ [      ///
        Approved by:                                                *
                                                                        [o__.                                    AY      h
                                              T. Peeble's, Section Chief                                      'Dats Sir,aed
                                                Projects Branch 3
                                              Division of Reactor Projects
                                                                                                                      &
                                                                                                -
                                                                            SUMMARY
        Scope: This routine, unannounced inspection was conducted on site inspecting in
        the areas of, review of plant operations (Units 1 & 2); surveillance observation
        (Units 1 & 2); maintenance observation (Units 1 & 2); review of licensee
        nonroutine event reports (Units 1 & 2); procedures (Units 1 & 2);                                          survey  of
        Licensee Response to Safety Issues (Units 1 & 2), Followup of Information Notices
        (Units 1 & 2); and preparations for refueling (Unit 1).                                            s
        Results:              Of the eight (8) areas inspected, two (2) apparent violations were
        identified, (Failure to follow procedures, paragraphs 6.b and 11.d; and Failure
        to provide adequate procedures, paragraph 11.b).                                          1
                                                                                                          ,
      8608110112 860725
      PDR ADOCK C5000413
      G                                              PDR
 
                      _.                                  _              _                _
    .
.
                                      REPORT DETAILS
  1.    Persons Contacted
        Licensee Employees
        J. W. Hampton, Station Manager
        E. M. Couch, Construction Maintenance Central Manager
        H. B. Barron, Operations Superintendent
      *M. J. Brady, Asst. Operating Engineer
        A. S. Bhatnager, Performance Engineer
        T. B. Bright, Construction Engineer Manager
        S. Brown, Reactor Engineer
        B. F. Caldwell, Station Services Superintendent
      *J. W. Cox, Superintendent, Technical Services
        T. E. Crawford, Operations Engineer
        L. R. Davidson, QA Manager Technical Support
        B. East, I. & E. Engineer
      *C. S. Gregory, I. & E. Support Engineer
        C. L. Hartzell, Licensing and Projects Engineer
      *J. A. Kammer, Performance Test Engineer
      *J. Knuti, Operating Engineer
        P. G. LeRoy, Licensing Engineer
        W. W. McCollough, Mechanical Maintenance Supervisor
      *W.  R. McCullum, Superintendent, Integrated Scheduling
        C. E. Muse, Operating Engineer
        K. W. Reynolds, Construction Maintenance
      *F. P. Schiffley, II, Licensing Engineer
        G. T. Smith, Maintenance Superintendant
        J. Stackley, I. & E. Engineer
        D. Tower, Operating Engineer
        Other licensee employees contacted included technicians, operators,
        mechanics, security force members, and office personnel.
      * Attended exit interview.                                      _
  2.    Exit Interview
        The inspection scope and findings were summarized on June 25, 1986, with
        those persons indicated in paragraph 1 above. The inspector described the
        areas inspected and discussed in detail the inspection findings.        No
        dissenting comments were received from the licensee. The licensee did not
        identify as proprietary any of the materials provided to or reviewed by the
        inspectors during this inspection.
                                                              .  - - -
                                                                            .-_.  _-_ - -_  . - _ .
 
              .          .        ._ _ . _                  _ _ _ _ __-.            _                              _ _ _ _ . . - . -_                  . . .-                ..
$
        .
  .
                                                                                2
.
                                                                                                                                                    '
    3.  Licensee Action on Previous Enforcement Hotters                                                                  (Units 1 & 2)
          (92702)
          a.    (OPEN) Unresolved Item 413/84-87-03- Review of operations corrective
                action program.                          The inspectors reviewed the employee training
                presentation for the Pro'olem Investigation Report program being
                developed to answer this item.                                    This presentation appears acceptable.
                This item remains open pending full implementation of the new program.
          b.    (OPEN)    Unresolved Item No. 414/85-56-03: Evaluation of Human
                Engineering Discrepancies in Control Room. The discrepancies identi-
                fied by this item have been corrected except for numbers on I/R Amps
                meter and the legends not removed for valves 2RC3, 2RC4, 2ND26 and
                2ND60. Further review will be conducted regarding the remaining two
                items.
          c.    (CLOSED) Unresolved Item 414/86-22-01 : Review of Licensee Actions
i                Concerning Control of Welding Inserts. The licensee had completed the
                review of this issue. The inspector held discussions with licensee
                personnel to review the findings. It appears that reuse of the inserts
-
                was being considered only if they could be fully justified by reestab-
'
                lishing traceability plus providing further technical justification.
                It is clear that new inserts were used and there is no evidence that a
                coverup was attempted. Quality Assurance personnel were cognizant of
i                the problem during its initial stages.                                                            The inspector considers
                licensee actions regarding this item to be acceptable.
4        No violations or deviations were identified.
    4.  Unresolved Items *
          A new unresolved item is identified in paragraph 11.c. * An Unresolved
,
          Item is a matter about which more information is required to determine
-
          whether it is acceptable or may involve a violation.
    5.  Plant Operations Review (Units 1 & 2) (71707 and 71710)
I
          a.    The inspectors reviewed plant operations throughout the reporting
                period to verify conformance with regulatory requirements. Technical
;                Specifications (TS), and administrative controls. Control room logs,
                danger tag logs, Technical Specification Action Item Log, and the
l-              removal and restoration log were routinely reviewed.                                                                      Shift turnovers
                were observed to verify that they were conducted in accordance with
                approved procedures.
                The inspectors verified by observation and interviews, the measures
                taken to assure physical protection of the facility met current
'
                  requirements. Areas inspected included the security organization, the
                establishment and maintenance of gates, doors, and isolation zones in
                  the proper condition, that access control and badging were proper and
i                procedures followed.
i
I
4
                              _ . - , . , , , - , - , , ,              .  - ,  ,    ,,,,,..----.-_,._,._______.---y-                          , ,..- - , .- - -...--... ,,,__..
 
                                                              .    . . _ _ -    -      .        .                    - - _
    .
  .
                                                                3                                                                  1
            In addition to the areas discussed above, the areas toured were
            observed for fire prevention and protection activities. These included
            such things as combustible material control, fire protection systems
            and materials, and fire protection associated with maintenance                                                          ,
            activities.
                                                                                                                                    ,
                                                                                                                                    '
          b. On June 5,                      1986, the licensee requested a seventy-two (72) hour
            extension to the time allowed under the Action statement of Technical
            Specification (TS) 3/4.4.6.2 " Operational Leakage". This request was
            made due to an unidentified leakage of 1.9 gpm. The request was to
            allow the unit to remain in Hot Standby to identify the leak. Relief
            was granted based on discussions between NRR, Region II, the Resident
'
            Inspector and the licensee. The licensee has addressed this issue in a
            letter to Region II dated June 10, 1986,
          c. At approximately 11:00am on June 13, 1986, the computer program for
            calculating unidentified leakage was showing                          1.79 pm unidentified
            leakage. An Unusual Event was declared at 3:00pm.                                At 3:42pm, a                            ,
            breaker shorted in a turbine building non-safety related power panel
            (IMXD) causing smoke and damage to the panel along with a loss of power
            to all loads served by that panel. One of these loads was the Hydrogen
            cooling pump, the loss of which caused main generator temperatures to
            start increasing.                      The operator began unloading the generator due to
            temperature increases. A second load was power to the control circuit
            of the variable letdown orifice control valve (INV 849). The loss of
            this control circuit caused this valve to fail full open giving a
            letdown flowrate of about 110gpm. The operator shifted the letdown
            orifice to a 45gpm orifice and immediately noted a high charging rate
            and a very low letdown rate indicating a primary system leak.                            Due to                        '.
,          cooldown caused by unloading the generator and the leak, leakage rate
            at first appeared to be about 150gpm. After about forty-five (45)
            minutes the operators shut the letdown isolation valves (INV-1 and
            1NV-2) which stopped the leak. A controlled shutdown of the reactor
            was continued and the generator taken off the line. The Unit was in
            Mode 3 at 5:00pm.                      Subsequent leakage calculation (prior to shutting
            INV-1 & INV-2) identified a leak of about 25gpm. A containment entry
,          was made and identified a 360 degree crack in a one (1) inch socket
'
            weld to the flange for the <ariable orifice control valve (INV 849)
            outlet side. Cooldown and d. pressurization was continued and the plant
            was placed in Mode 5 at a15am on June 15, 1986.                                  The resident
            inspectors were on site and closely monitored this event. The cause of
            the failure of IMXD had been identified to be a vendor installed
            nameplate (size 1" x 2.5"), which had caused a short circuit.
"
            Preliminary evaluation by licensee design personnel indicates probable
            cause of the socket weld failure to be vibration induced fatigue. The
'.
            weld was sent to the Westinghouse hot laboratory in Pittsburg, Penn.
              for analysis.                    Further licensee actions have included radiography of
            welds, vibration tests on both units, procedural changes limiting use
            of valve 1NV 849, removal of label plates from transformers in both
4
      -. .      . _ _ . - . - . . - . . - -        . ,-.---__    -  .-      --        ,_
                                                                                            -
                                                                                              ,y2  . ._m . , _ _ _ - ,      , - _
 
          .
    .
                                                4
                units and rewelding to reinstall INV 849.      The inspectors verified
                licensee actions. Long term corrections are being reviewed. The
                residents will continue followup of this problem which will be reported
                in detail to the NRC as a Licensee Event Report.
            No violations or deviations were identified.
      6.  Surveillance Observation (Units 1 & 2) (61726)
            a.  During the inspection period, the inspector verified plant operations
                were in compliance with various TS requirements. Typical of these
                requirements were confirmation of compliance with the TS for reactor
                coolant chemistry, refueling water tank, emergency power systems,
                safety injection, emergency safeguards systems, control room ventila-
                tion, and direct current electrical power sources.        The inspector
                verified that surveillance testing was performed in accordance with the
                approved written procedures, test instrumentation was calibrated,
  ,
                limiting conditions for operation were met, appropriate removal and
                restoration of the affected equipment was accomplished, test results
                met requirements and were reviewed by personnel other than the
                individual directing the test, and that any deficiencies identified
                during the testing were properly reviewed and resolved by appropriate
                management personnel,
            b.  On June 11, 1986, a reactor trip from 85% power occurred on Unit 1.
                Investigation into this by the licensee will be documented in a
                Licensee Event Report. The inspector reviewed this event and identi-
                fied the following sequence.      The instrumentation technicians (IAE)
                were performing IP 0/A/3?40/11, Excore Nuclear Instrumentation System,
                dated 7/16/85. In accordance with step 10.1.6, IAE had requested the
                reactor operator (RO) to turn the Steam Generator Program Level
                Setpoint Indicator to a channel other than the one being tested. The
                IAE performed the required adjustments on the specific channel he was
                working. He then proceeded to the next channel without notification to
                the R0 as required by a repeat of doing step 10.1.6. This failure
                resulted in the I/E performing action on the channel selected to
                provide input to the steam generator level circuit. The input caused a
'
                decrease of feed water to the steam generators and a resultant low-low
                level steam generator B reactor trip before actions could be taken to
                correct the situation.      The actions by the IAE personnel in not
,
                performing step 10.1.6 of IP 0/A/3240/11, is a violation of TS 6.8.1
{                which requires procedures to be implemented as they are approved. This
'
                example is being combined with other examples discussed in paragraph
                11.d to constitute one violation 413/86-24-01,414/86-26-01, Failure to
                follow procedures associated with IP 0/A/3240/11, Station Directive
                3.2.2, Operations Management Procedure 2-29 and Maintenance Management
                Procedure 1.0.
            One violation was identified as described in paragraph 6.b. above.        No
!          deviations were identified.
l-
 
                                                        _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _              _ _ _ _ _ _ .
_ . . .. .
                      .
                .
                                                                                                                      5
                    7.  Maintenance Observations (Units 1& 2) (62703)                                                                                                                      ;
                        Station maintenance activities of selected systems and components were
                        observed / reviewed to ascertain that they were conducted in accordance with
                        requirements. The inspector verified licensee conformance to the require-
                        ments in the following areas of inspection:                                                                              the activities were accomp-
                        lished using approved' procedures, and functional testing and/or calibrations
                        were performed prior to returning components or systems to service; quality
                        control records were maintained; activities performed were accomplished by
                        qualified personnel; and materials used were properly certified.                                                                                            Work
                        requests were reviewed to determine status of outstanding jobs and to assure
                                                                                                                                                                .
                        that priority is assigned to safety-related equipment maintenance which may
                        effect system performance.
                        No violations or deviations were identified.
                    8.  Review of Licensee Nonroutine Event Reports (Units 1 & 2) (92700)
                        a.    The below listed Licensee Event Reports (LER) were reviewed to
                              determine if the information provided met NRC requirements. The
                              determination included: adequacy of description, verification of
                              compliance with Technical Specifications and regulatory requirements,
                              corrective action taken, existence of potential generic problems,
                              reporting requirements satisfied, and the relative safety significance
                              of each event. Additional inplant reviews and discussion with plant
                              personnel, as appropriate, were conducted for those reports indicated
                              by an (*). The following LERs are closed:
                              *LER 413/85-53                                                                                Diesel Generator 1A Battery Charger
                                                                                                                              Inoperable Due to Blown Fuses
                                  LER 413/85-67 Rev.1                                                                        Reactor Trip on Loss of Main Feedwater
                                                                                                                              Pump Due to Design Deficiency
                              *LER 413/86-01                                                                                Procedural            Deficiency        Caused        Missed
                                                                                                                              Surveillance of Control                          Room Carbon
                                                                                                                              Filters
                                  LER 413/86-06                                                                                Reactor Trip Due to Trip of the 1C2
l
                                                                                                                              Heater Drain Tank Pump
                                *LER 413/86-07                                                                                Auxiliary Feedwater Start on Loss of Main
                                                                                                                                Feedwater Pump Turbine Condenser Vacuum
                                *LER 413/86-10                                                                                Alternate Power Sources Not Verified
                                                                                                                              Operable While            Diesel              Generator  1B
                                                                                                                                  Inoperable
                                *LER 413/86-11                                                                                  Both Trains of Annulus Ventilation System
                                                                                                                                  Inoperable Due to Personnel Error
  ..      .. .  .
                        ..    .
                                                                                                                                                      _
 
                                  --                        __  _-
      .
  .
                                                                                          i
                                                6
                *LER 413/86-12 Rev.1          Both    trains  of Containment Valve
                                                Injection Water System Inoperable Due to
                                                Defective Procedure
                  LER 413/86-13                Termination of Containment Release Due to
4
                                                Spurious Radiation Alarm
                  LER 413/86-14                Control Rod Surveillance Not Performed
                                                Due to Defective Procedure
                  LER 413/86-16                Penetration    Surveillance  Interval
                                      -
                                                Exceeded Due to Personnel Error and
                                                Defective Procedure
                *LER 413/86-17                Axial Flux Difference Requirements Not
                                                Met Due to Computer Malfunctions
                *LER 413/86-23                Reactor Trip Due to Failure to Block
                                                Source Range High Flux Trip Setpoint
>
                    LER 414/86-03              ESF Actuation - High/High Steam Generator
                                                Level Caused By Main Feedwater Isolation
                    LER 414/86-09              Failure to Place Inoperable Steam
                                                Generator In A Tripped Condition Within
                                                One Hour
                    LER 414/86-10              ESF Actuation - Auxiliary Feedwater Auto
-
                                                Start Due to High/High Steam Generator
                                                Level
                    LER 414/86-12              ESF Actuation - Main Feedwater Isolation
,                                              on Steam Generator 2A Due to High/High
i                                              Steam Generator Level
i          b.    (CLOSED) CDR 413/84-16, 414/84-16: Unconsidered effects of superheated
i                steam on safety-related components. The inspectors observed safety
                related equipment in the Unit 2 exterior doghouse to verify that the
                  licensee responses appropriately identified equipment possibly affected
                by superheated steam.  Final NRC approval of the licensee analysis is
                complete.
'
          No violations or deviations were identified.
    9.    Survey of Licensee's Response to Safety Issues (Units 1 & 2) (92701)
          The inspector reviewed the licensee's response to the issue of biofouling of
          cooling water heat exchangers as addressed in Inspection and Enforcement
-
          Manual TI 2515/77.
l
        ..    -.        -                - _                        -
 
                                                                        .      .    . ,
1      .
  .
                                            7
,
        The licensee has developed several procedures that are used to monitor flow
        through service water heat exchangers. These procedures are conducted on a
        quarterly basis by the performance engineering personnel.          Installed
        instrumentation is not used to monitor degradation but more precision test
        equipment is installed. Trends are maintained by these engineers.        Heat
        exchangers that are not feasible to measure various parameters, have been
        scheduled for routine periodic cleaning.      Fire protection systems are
        periodically flushed and, in addition, are being modified to include a
        chlorination system for chemical treatment. Based on this review, the
,      actions taken and scheduled by the licensee appear to be acceptable.
        No violations or deviations were identified.
i                                                                          ?
    10. Preparations for Refueling (Unit 1) (60705)
,
        The inspector reviewed preparations for refueling of Unit 1 presently
        scheduled to commence August 15, 1986 and complete on October 23, 1986. The
        inspector reviewed procedures for fuel handling, transfers, and core
        verification; inspection of fuel to be reused; and various other procedures
        that will be required during refueling.        The inspector reviewed the
        following specific procedures:
              IP 1/A/3230/06      Procedure for Disconnecting and Connection of
                                  Incore T/C Cables, dated 6/2/86
.
              MP 0/A/7150/43      Reactor Vessel Internals Removal and Replacement,
                                  dated 4/25/86
              MP 0/A/7150/50      UHI Piping Removal and Replacement, dated 9/30/85
              MP 0/A/7150/76      Rod Drive Assembly Installation and Removal, dated
                                  11/21/85
              MP 1/A/7150/42      Reactor Vessel Head Removal and Replacement, dated
                                  2/4/86
;              OP 0/A/6550/04      Transferring New Fuel to the Elevator, dated
l                                  6/19/84
l
              OP 0/A/6550/05      Primary Neutron Source Handling, dated 6/27/84
              OP 0/A/6S50/07      Reactor Building Manipulator Crane Operation, dated
                                  2/20/86
!
!              OP 0/A/6550/08      Fuel Transfer System Operation, dated 6/27/84
l              OP 0/A/6550/09      RCCA Change Fixture Operation, dated 6/21/84
              OP 0/A/6550/14      Draining and Filling Spent Fuel Pool Transfer Canal
                                  and Cask Area, dated 6/26/84
I
t
 
      o
*
  e
                                                          8
                OP 1/A/6200/13          Filling, Draining, and Purification of Refueling
                                        Cavity, dated 6/29/84
                OP 1/A/6550/06-        Transferring Fuel With the Spent Fuel Manipulator
                                        Crane, dated 6/21/84
          In addition, although' procedure identification numbers have been assigned
          for areas such as Vessel Irradiation Sample Removal, Refueling Procedure,
          Total Core Unloading, Total' Core Reloading and Spent Fuel Pool Shuffle of
          Core Components, these procedures have not been issued at this time. The
          inspector identified to the licensee his concern over issuance of these
          procedures and minor errors in the procedures listed above including that a
          two year review had not been performed to date.
          The inspector also reviewed a proposed schedule for the refueling that
          identifies major work to be accomplished during the outage. This schedule
          also shows the Nuclear Station Modifications that are scheduled to be
          performed.
          No violations or deviations were identified.
    11.  Plant Procedures (Units 1 & 2) (42700)
          a.    The inspector reviewed various plant procedures to determine whether
                overali plant procedures are in accordance with regulatory require-
                ments, procedure changes were made in accordance with TS requirements,
                the technical adequacy of the reviewed procedures is consistent with
                desired actions and modes of operation, and procedures, when used, are
                being followed as required.              In addition to the procedures identified
                in paragraph 10 above the below listed procedures were also reviewed:
                      PT 1/A/4200/02A                      Monthly Outside Containment Integrity
.
                                                          Verification
                      PT 2/A/4200/02A                      Monthly Outside Containment Integrity
                                                          Verification
                      PT 1/A/4200/02B                      Cold    Shutdown    Inside  Containment
1
                                                            Integrity Verification
                      PT 2/A/4200/02B                      Cold    Shutdown    Inside  Containment
                                                            Integrity Verification
                      IP 0/A/3240/11                      Excore Nuclear Instrumentation System
                      IP 1/A/3101/02                      Refueling Water System Instrumentation
                                                          Calibration
                      SD 3.1.17                            Fuel Handling Interlocks
!
      -_.                      - _ __    _    - . . _ _
 
                                                    ~          .          _    .
        s
      e
                                              9
                                                                                                  ,
                            TP 1/A/1450/18    Spent Fuel Pool Filter Train Functional
                                              Test
              'As a result of this review one violation and one unresolved item was
                identified as discussed below.
'
            b.  The review discussed above identified several examples of inadequate
'
.
                procedures. The first example is contained in PT 2/A/4200/02A, Monthly
                Outside Containment Integrity Verification for Unit 2. The purpose of
                this PT is to insure that containmeat penetration integrity is being
                maintained by verifying conditions of the penetration isolations
                located outside of the containment. A' review by the licensee of this
                PT identified approximately twenty-five (25) valves located on various
                penetrations that were not included in this procedure. These are
                identified in the licensee's non-routine event report C86-77-2 dated
                6/5/86. The omission of these valves resulted in a violation of TS
                4.6.1.1.a , which requires the penetrations to be checked every thirty
                one (31) days. A subsequent check of these valves found them all in
                their required positions.    Adequate corrective actions would have
                included the prompt identification and correction of the following
                examples and therefore this licensee identified example is a violation.
                A second example was associated with . PT 2/A/4200/02B, Cold Shutdown
                Inside Containment Integrity Verification. The purpose of this PT is
                to insure that containment penetration integrity is being maintained by
                verifying conditions of penetrations inside the containment. A review
                of this procedure identified twelve (12) valves that are a part of
                these penetrations that were not included in this procedure. As a
                result of this the licensee violated T.S. 4.6.1.1.a.      A subsequent
                check of these valves found them all in their required position.
                The third example of inadequate procedures is associated with PT
                1/A/4200/02A, Monthly Outside Containment Integrity Verification for
                Unit 1. A review of this procedure by the inspector identified one
                valve that should be included in the procedure. The omission of this
                valve also resulted in a violation of TS 4.6.1.1.a. This valve was
;
                also found in its required position.
                These three examples are combined to constitute one Violation,
                413/86-24-02 414/86-26-02, Failure to provide adequate procedures
t
                resulting in a violation of TS 4.6.1.1.a.
            c.  During the inspectors review of PT 2/A/4200/02A several additional
                questions were identified.    A comparison of this PT to the Unit 1
                procedure identified approximately twenty (20) valves that were on the
'
                Unit 1 procedure that were identified by the licensee, but similar Unit
!              2 valves were not identified. Positions for Numerous valves on the
                Unit 2 procedure were identified as " CLOSED" whereas the Unit 1
                procedure and the system flow diagrams identify these same valves as
                " LOCKED CLOSED". These questions are being identified as an Unresolved
                Item 413/86-24-03, 414/86-26-03: Procedural discrepancies associated
                with similar procedures between Units 1 & 2 pending review by the
  _ -    .        ._- _ - - _ _    _  --__                                            _ _ - . _
 
    s
  .
                                            10
            licensee and additional review by the inspector to determine the extent
            and significance of the discrepancies.
        d.  The inspector also reviewed several administrative procedures that are
            used to control work and testing associated with work.        The specific
            procedures reviewed were Station Directive (SD) 3.2.2, Development and
            Conduct of the Periodic Testing Program, Operations Management
            Procedure (OMP) 2-29, Technical Specifications Logbook, and Maintenance
            Management Procedure (MMP) 1.0, Work Request Preparation. In addition
            to this review, the inspector reviewed various work items to insure
            they were conducted in accordance with these administrative procedures.
            SD 3.2.2, Section 8.0 requires after a valve has undergone maintenance
            and prior to its return to service, it shall be tested as necessary to
            demonstrate that the parameters affected by the maintenance are within
            acceptable limits. On May 17,1986, 2CF-87, 2CF-33, and 2CF-60 were
            repaired and returned to service on May 19, 1986, without being tested
            to demonstrate that the parameters affected were within acceptable
            limits. OMP 2-29, Section 3.3.8 requires inoperable equipment that
            causes operation in an ACTION statement of TS for the existing mode be            ,
-
            logged in the TS Action Item Log (TSAIL).      Work request 31838 OPS,
l            31841 OPS, 32033 OPS and 32046 OPS were all processed to be performed
            on May 14, 1986, and were not logged in the TSAIL. The results of this
            failure allowed work to be performed without performance of the
            required functional testing. MMP 1.0, paragraph 4.3.10 states that the
!            section of the Work Request entitled " Procedure Numbers" shall reflect
            a complete listing of procedures to perform work, A review of the work
            requests identified above identified that the procedures that were
            required to be used to perform the required retesting was omitted
            contributing to the failure to retest the work activity. The above
            examples are combined with the example discussed in paragraph 6.b to be
              identified as one Violation : 413/86-24-01, 414/86-26-01; Failure to
              follow procedures associated with IP 0/A/3240/11, Station Directive
            3.2.2, Operations Management Procedure 2-29 and Maintenance Management
            Procedure 1.0.
        Two violations were identified as described in paragraphs 11.b. and d.                .
        above. No deviations were identified.
    12. Followup of IE Notices and IE Bulletins Sent For Information (Units 1 & 2)
        (92701)
        The inspector reviewed the actions taken by the licensee upon receipt of an
        IE Notice (IEN) sent for information purposes only.            The Compliance
        Engineer, at present, controls receipt and distribution of these documents
        to assure appropriate personnel review the contents and determine actions
        that may be required as a result. The following notices were reviewed to
        assure receipt, review by appropriate personnel, and any resulting action
        identified, documented and followed to completion:
        IE Notices 85-33
                    85-59
,
        No violations or deviations were identified.
!
i
                      , ,  _ _ _ , _                        _    --    _    .-.    _ , .
}}

Revision as of 19:41, 7 December 2024