ML20212Q052: Difference between revisions

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                                                      J M 2 1 iBB7
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                  Docket / License: 50-423/NPF-49
J M 2 1 iBB7
                  Northeast Nuclear Energy Company
Docket / License:
                  ATTN: Mr. Edward J. Mroczka
50-423/NPF-49
                          Senior Vice President, Nuclear
Northeast Nuclear Energy Company
                          Engineering and Operations
ATTN: Mr. Edward J. Mroczka
                  P.O. Box 270
Senior Vice President, Nuclear
                  Hartford, Connecticut     06101-0270
Engineering and Operations
                  Gentlemen:
P.O. Box 270
                  Subject: Millstone 3 Special Inspection 50-423/86-39
Hartford, Connecticut
                  This transmits the findings of the December 29, 1986 - January 7, 1987 special NRC
06101-0270
                  inspection of the inoperability of the Millstone 3 "B" safety injection (SIH) pump
Gentlemen:
                  during the neriod from November   26-30, 1986.   On December 1, 1986, the NRC was in-
Subject: Millstone 3 Special Inspection 50-423/86-39
                  formed aboLt the pump inoperability and your plan to conduct a thorough investiga-
This transmits the findings of the December 29, 1986 - January 7, 1987 special NRC
                  tion of the circumstances. A special inspection was begun when the resident in-
inspection of the inoperability of the Millstone 3 "B" safety injection (SIH) pump
                  spector became aware of the results of the investigation during discussions at the
during the neriod from November 26-30, 1986.
                  Plant Operations Review Committee (PORC) meeting on December 29, 1986, shortly be-
On December 1, 1986, the NRC was in-
                  fore your December 30, 1986 licensee event report (LER) on this matter was sub-
formed aboLt the pump inoperability and your plan to conduct a thorough investiga-
                  mitted. This event involved exceeding a Limiting Condition for Operation and the
tion of the circumstances.
                  recording of false surveillance test data for a test that was not accomplished.
A special inspection was begun when the resident in-
                We concluded that the overall safety function remained capable of being fulfilled
spector became aware of the results of the investigation during discussions at the
                  by the second train of emergency core cooling equipment. The inoperable equip-
Plant Operations Review Committee (PORC) meeting on December 29, 1986, shortly be-
                  ment was promptly corrected as soon as it was identified on November 30, 1986.
fore your December 30, 1986 licensee event report (LER) on this matter was sub-
                Also, substantive corrective action has been initiated. During the special in-
mitted.
                  spection, our inspectors found all personnel contacted to be fully responsive
This event involved exceeding a Limiting Condition for Operation and the
                  and open, including the individual who shut the valve which made the safety
recording of false surveillance test data for a test that was not accomplished.
                  injection pump inoperable and who falsely recorded the data.     Although the
We concluded that the overall safety function remained capable of being fulfilled
                  specific test involved and the recording of data from that test are not required
by the second train of emergency core cooling equipment.
                by the NRC, the importance of assuring safety equipment operability and proper
The inoperable equip-
                  recording of data are significant issues that need to be addressed. Therefore,
ment was promptly corrected as soon as it was identified on November 30, 1986.
                we are not forwarding a notice of violation for this matter at this time and
Also, substantive corrective action has been initiated.
                will contact you separately to schedule an enforcement conference in the NRC             1
During the special in-
                                                                                                          !
spection, our inspectors found all personnel contacted to be fully responsive
                Region I office in King of Prussia. During the enforcement conference, we would         I
and open, including the individual who shut the valve which made the safety
                  like you to address your evaluation of and actions taken or planned on the
injection pump inoperable and who falsely recorded the data.
                  following:                                                                             .
Although the
                                                                              -
specific test involved and the recording of data from that test are not required
                --
by the NRC, the importance of assuring safety equipment operability and proper
                        Safety significance.
recording of data are significant issues that need to be addressed.
                --
Therefore,
                        Root cause evaluation.
we are not forwarding a notice of violation for this matter at this time and
                        Broader implications of this event.-
will contact you separately to schedule an enforcement conference in the NRC
                --
Region I office in King of Prussia. During the enforcement conference, we would
                --
like you to address your evaluation of and actions taken or planned on the
                        Corrective actions to prevent recurrence.
following:
            8702020126
.
            PDR           870121                                                                /
-
            Q      ADOCK 05000423
Safety significance.
  _ _ _ _
--
                                PDR  .
Root cause evaluation.
                                                                                                    l{
--
Broader implications of this event.-
--
Corrective actions to prevent recurrence.
--
/
8702020126 870121
PDR
ADOCK 05000423
.
l{
Q
PDR
_ _ _ _


        :-
: -
*
,
,
.
Northeast Nuclear Energy Company
2
Thank you for your cooperation.
Sincerely,
Uriatco131snad B75
William F. Kane, Director
Division of Reactor Projects
.
Enclosure: NRC Region I Inspection Report 50-423/86-39
cc w/ enc):
V. Papadopoli, Construction Quality Assurance Supervisor
E. R. Fester, Director of Generation Construction
W. D. Romberg, Vice President, Nuclear Operations
D. O. Nordquist, Manager of Quality Assurance
R. M. Kacich, Manager, Generation Facilities Licensing
S. E. Scace, Station Superintendent
Public Document Room (PDR)
Local Public Document Room (LPDR)
,
,
            *
Nuclear Safety Information Center (NSIC)
      ,
NRC Senior Resident Inspector
        .
State of Connecticut
                  Northeast Nuclear Energy Company          2
bcc w/ encl:
                  Thank you for your cooperation.
Region I Docket Room (with concurrences)
                                                            Sincerely,
Management Assistant, DRMA (w/o enc 1)
                                                            Uriatco131snad B75
DRP Section Chief
                                                            William F. Kane, Director
L. Prividy, RI, BV-2
                                                            Division of Reactor Projects
T. Rebelowski, SRI, Millstone 1&2
.
B. Doolittle, LPM, NRR
                  Enclosure: NRC Region I Inspection Report 50-423/86-39
Robert J. Bores, DRSS
                  cc w/ enc):
                  V. Papadopoli, Construction Quality Assurance Supervisor
                  E. R. Fester, Director of Generation Construction
                  W. D. Romberg, Vice President, Nuclear Operations
                  D. O. Nordquist, Manager of Quality Assurance
                  R. M. Kacich, Manager, Generation Facilities Licensing
                  S. E. Scace, Station Superintendent
                  Public Document Room (PDR)
,                Local Public Document Room (LPDR)
                  Nuclear Safety Information Center (NSIC)
                  NRC Senior Resident Inspector
                  State of Connecticut
                  bcc w/ encl:
                  Region I Docket Room (with concurrences)
                  Management Assistant, DRMA (w/o enc 1)
                  DRP Section Chief
                  L. Prividy, RI, BV-2
                  T. Rebelowski, SRI, Millstone 1&2
                  B. Doolittle, LPM, NRR
4
4
                  Robert J. Bores, DRSS
J. Joyner, DRSS
                  J. Joyner, DRSS
k
              ** RI:DRP             ** RI:DRP       **RI:DRP               k            RI:RA
** RI:DRP
                  Shedloskly/meo       McCabe         Wenzinger         K31           Murley
** RI:DRP
                  1/7/87
**RI:DRP
            **SEE PREVIOUS CONCURRENCE
RI:RA
  , .             -
Shedloskly/meo
                                      .   - - - -   .
McCabe
                                                                    --   .   .,.   .-         - . - - . _ . - ..
Wenzinger
K31
Murley
1/7/87
**SEE PREVIOUS CONCURRENCE
, .
-
.
.
- - - -
.
--
.
.,.
.-
- . - - .
. - ..


:'- '.
:'- '
                I
I
  .
.
          Northeast Nuclear Energy Company           2
.
                                                              JAN 211997
Northeast Nuclear Energy Company
          Thank you for your cooperation.
2
                                                      Sincerely,
JAN 211997
                                                      William F. Kane, Director
Thank you for your cooperation.
                                                      Division of Reactor Projects
Sincerely,
          Enclosure:   NRC Region I Inspection Report 50-423/86-39
William F. Kane, Director
          cc w/ encl:
Division of Reactor Projects
          V. Papadopoli, Construction Quality Assurance Supervisor
Enclosure:
          E. R. Foster, Director of Generation Construction
NRC Region I Inspection Report 50-423/86-39
        W. D. Romberg, Vice President, Nuclear Operations
cc w/ encl:
        D. O. Nordquist, Manager of Quality Assurance
V. Papadopoli, Construction Quality Assurance Supervisor
        R. M. Kacich, Manager, Generation Facilities Licensing
E. R. Foster, Director of Generation Construction
        S. E. Scace, Station Superintendent
W. D. Romberg, Vice President, Nuclear Operations
        Public Document Room (PDR)
D. O. Nordquist, Manager of Quality Assurance
        Local Public Document Room (LPDR)
R. M. Kacich, Manager, Generation Facilities Licensing
        Nuclear Safety Information Center (NSIC)
S. E. Scace, Station Superintendent
        NRC Senior Resident Inspector
Public Document Room (PDR)
        State of Connecticut
Local Public Document Room (LPDR)
        bcc w/ enc 1:
Nuclear Safety Information Center (NSIC)
        Region I Docke.t Room (with concurrences)             '
NRC Senior Resident Inspector
        Management Ass ~istant, DRMA (w/o enc 1)
State of Connecticut
        DRP Section Chief
bcc w/ enc 1:
        L. Prividy, RI, BV-2
Region I Docke.t Room (with concurrences)
        T. Rebelowski, SRI, Millstone 1&2
'
        B. Doolittle, LPM, NRR
Management Ass ~istant, DRMA (w/o enc 1)
        Robert J. Bores, DRSS
DRP Section Chief
        J. Joyner, DRSS                                       -
L. Prividy, RI, BV-2
      RI:DRP                 RI:DRP
T. Rebelowski, SRI, Millstone 1&2
                                                  '
B. Doolittle, LPM, NRR
                                                    P             F         RI:RA
Robert J. Bores, DRSS
            @b                 (&
J. Joyner, DRSS
      Shedlo'skly/meo       McCabe             nzinger
-
                                                                    .
RI:DRP
                                                                            Murley
RI:DRP
      1     87
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                                              .                 i    q'l
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                                11 0          g  gc            1     6
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                                      0FFICIAL RECORD COPY
RI:RA
@b
(&
.
Shedlo'skly/meo
McCabe
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Murley
1
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Latest revision as of 04:10, 4 December 2024

Forwards Insp Rept 50-423/86-39 on 861229-870107 of Inoperability of Safety Injection Pump B from 861126-30. Safety Function Fulfilled by Second Train of Emergency Cooling Equipment.Enforcement Conference Will Be Scheduled
ML20212Q052
Person / Time
Site: Millstone 
Issue date: 01/21/1987
From: Kane W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Mroczka E
NORTHEAST NUCLEAR ENERGY CO.
Shared Package
ML20212Q054 List:
References
NUDOCS 8702020126
Download: ML20212Q052 (3)


See also: IR 05000423/1986039

Text

.

_

,

'

.

.

.

J M 2 1 iBB7

Docket / License:

50-423/NPF-49

Northeast Nuclear Energy Company

ATTN: Mr. Edward J. Mroczka

Senior Vice President, Nuclear

Engineering and Operations

P.O. Box 270

Hartford, Connecticut

06101-0270

Gentlemen:

Subject: Millstone 3 Special Inspection 50-423/86-39

This transmits the findings of the December 29, 1986 - January 7, 1987 special NRC

inspection of the inoperability of the Millstone 3 "B" safety injection (SIH) pump

during the neriod from November 26-30, 1986.

On December 1, 1986, the NRC was in-

formed aboLt the pump inoperability and your plan to conduct a thorough investiga-

tion of the circumstances.

A special inspection was begun when the resident in-

spector became aware of the results of the investigation during discussions at the

Plant Operations Review Committee (PORC) meeting on December 29, 1986, shortly be-

fore your December 30, 1986 licensee event report (LER) on this matter was sub-

mitted.

This event involved exceeding a Limiting Condition for Operation and the

recording of false surveillance test data for a test that was not accomplished.

We concluded that the overall safety function remained capable of being fulfilled

by the second train of emergency core cooling equipment.

The inoperable equip-

ment was promptly corrected as soon as it was identified on November 30, 1986.

Also, substantive corrective action has been initiated.

During the special in-

spection, our inspectors found all personnel contacted to be fully responsive

and open, including the individual who shut the valve which made the safety

injection pump inoperable and who falsely recorded the data.

Although the

specific test involved and the recording of data from that test are not required

by the NRC, the importance of assuring safety equipment operability and proper

recording of data are significant issues that need to be addressed.

Therefore,

we are not forwarding a notice of violation for this matter at this time and

will contact you separately to schedule an enforcement conference in the NRC

Region I office in King of Prussia. During the enforcement conference, we would

like you to address your evaluation of and actions taken or planned on the

following:

.

-

Safety significance.

--

Root cause evaluation.

--

Broader implications of this event.-

--

Corrective actions to prevent recurrence.

--

/

8702020126 870121

PDR

ADOCK 05000423

.

l{

Q

PDR

_ _ _ _

-

,

,

.

Northeast Nuclear Energy Company

2

Thank you for your cooperation.

Sincerely,

Uriatco131snad B75

William F. Kane, Director

Division of Reactor Projects

.

Enclosure: NRC Region I Inspection Report 50-423/86-39

cc w/ enc):

V. Papadopoli, Construction Quality Assurance Supervisor

E. R. Fester, Director of Generation Construction

W. D. Romberg, Vice President, Nuclear Operations

D. O. Nordquist, Manager of Quality Assurance

R. M. Kacich, Manager, Generation Facilities Licensing

S. E. Scace, Station Superintendent

Public Document Room (PDR)

Local Public Document Room (LPDR)

,

Nuclear Safety Information Center (NSIC)

NRC Senior Resident Inspector

State of Connecticut

bcc w/ encl:

Region I Docket Room (with concurrences)

Management Assistant, DRMA (w/o enc 1)

DRP Section Chief

L. Prividy, RI, BV-2

T. Rebelowski, SRI, Millstone 1&2

B. Doolittle, LPM, NRR

Robert J. Bores, DRSS

4

J. Joyner, DRSS

k

    • RI:DRP
    • RI:DRP
    • RI:DRP

RI:RA

Shedloskly/meo

McCabe

Wenzinger

K31

Murley

1/7/87

    • SEE PREVIOUS CONCURRENCE

, .

-

.

.

- - - -

.

--

.

.,.

.-

- . - - .

. - ..

'- '

I

.

.

Northeast Nuclear Energy Company

2

JAN 211997

Thank you for your cooperation.

Sincerely,

William F. Kane, Director

Division of Reactor Projects

Enclosure:

NRC Region I Inspection Report 50-423/86-39

cc w/ encl:

V. Papadopoli, Construction Quality Assurance Supervisor

E. R. Foster, Director of Generation Construction

W. D. Romberg, Vice President, Nuclear Operations

D. O. Nordquist, Manager of Quality Assurance

R. M. Kacich, Manager, Generation Facilities Licensing

S. E. Scace, Station Superintendent

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Senior Resident Inspector

State of Connecticut

bcc w/ enc 1:

Region I Docke.t Room (with concurrences)

'

Management Ass ~istant, DRMA (w/o enc 1)

DRP Section Chief

L. Prividy, RI, BV-2

T. Rebelowski, SRI, Millstone 1&2

B. Doolittle, LPM, NRR

Robert J. Bores, DRSS

J. Joyner, DRSS

-

RI:DRP

RI:DRP

'

P

F

RI:RA

@b

(&

.

Shedlo'skly/meo

McCabe

nzinger

i

q'l

Murley

1

87

11 0

.

1

c

6

g g

0FFICIAL RECORD COPY