ENS 55975: Difference between revisions

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| event date = 07/04/2022 01:04 CDT
| event date = 07/04/2022 01:04 CDT
| last update date = 07/04/2022
| last update date = 07/04/2022
| title = Reactor Manual SCRAM Due to Lowering Reactor Water Level
| title = Reactor Manual Scram Due to Lowering Reactor Water Level
| event text = The following information was received from the licensee via facsimile:
| event text = The following information was received from the licensee via facsimile:
On July 4, 2022 at 0104 CDT, with Unit 2 in Mode 1 at 100 percent power, a manual scram was inserted on U2 due to lowering reactor water level, which occurred following an unexpected closure of the 2A Feedwater Regulating Valve. Following the reactor scram, reactor water level decreased to approximately minus 16 inches, which resulted in an automatic Group II and Group III isolation (expected response). Following the scram, reactor water level rose to plus 75 inches resulting in a trip of all three Reactor Feedwater Pumps. At 0114 CDT, Reactor Water Level lowered to less than the Feedwater Pump High Level Trip setpoint and the 2C Reactor Feedwater Pump was restarted. Reactor Water Level control has been established in a normal band. The cause and details of the event are under investigation.
On July 4, 2022 at 0104 CDT, with Unit 2 in Mode 1 at 100 percent power, a manual scram was inserted on U2 due to lowering reactor water level, which occurred following an unexpected closure of the 2A Feedwater Regulating Valve. Following the reactor scram, reactor water level decreased to approximately minus 16 inches, which resulted in an automatic Group II and Group III isolation (expected response). Following the scram, reactor water level rose to plus 75 inches resulting in a trip of all three Reactor Feedwater Pumps. At 0114 CDT, Reactor Water Level lowered to less than the Feedwater Pump High Level Trip setpoint and the 2C Reactor Feedwater Pump was restarted. Reactor Water Level control has been established in a normal band. The cause and details of the event are under investigation.

Latest revision as of 15:01, 4 January 2024

ENS 55975 +/-
Where
Quad Cities Constellation icon.png
Illinois (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-0.12 h-0.005 days <br />-7.142857e-4 weeks <br />-1.64376e-4 months <br />)
Opened: Mike Maclennan
05:57 Jul 4, 2022
NRC Officer: Donald Norwood
Last Updated: Jul 4, 2022
55975 - NRC Website
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