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| | February 16, 1983 UNITED STATES OF AMERICA NUCLEAR REGULATORY COMMISSION BEFORE THE ATOM 2"C SAFETY AND LICENSING APPEAL BOARD In the Matter of ) |
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| | METROPOLITAN EDISON COMPANY ) Docket No. 50-289 |
| | ) (Restart) |
| | (Three Mile Island Nuclear ) |
| | Station, Unit No. 1) ) |
| | LICENSEE'S TESTIMONY OF ROBERT C. JONES, JR., AND LOUIS C. LANESE IN RESPONSE TO ALAB-708 ISSUE NO. 9 (RELIANCE ON FEED AND BLEED COOLING) 8302220381 830226 (DRADOCK 05000289 PDR |
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| | ==SUMMARY== |
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| | l This testimony is in response to the Appeal Board's request that Licensee and the Staff set forth the ponditions for which feed and bleed cooling will be relied upon at TMI-1. |
| | The testimony confirms Licensee's previously stated position that feed and bleed cooling is only required for those beyond design basis events involving an extended loss of both main and emergency feedwater. This testimony also shows that the TMI-1 l- safety valves are capable of successfully relieving two-phase flow. |
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| | INTRODUCTION 1 |
| | This testimony, by Robert C. Jones, Jr., Supervisory 2 |
| | Engineer, Operational Analysis Unit, Babcock & Wilcox Company, 3 |
| | and Louis C. Lanese, Senior Safety Analysis and Plant Control 4 |
| | Engineer, GPU Nuclear Corporation, is addressed to Issue No. 9 5 |
| | f the Appeal Board's Memorandum and Order of December 29, 1982 6 |
| | (ALAB-708), which states: |
| | 7 |
| | : 9. Whether and under what circumstances reliance 8 |
| | on feed and bleed is necessary at TMI-l (from g the licensee and the staff). |
| | 10 This testimony will also respond to the concerns expressed by 11 the Appeal Board at page 39 of ALAB-708, regarding the ability 12 f the TMI-l pressurizer safety valves to successfully pass two-phase flow, and the resultant effects on feed and bleed 13 cooling capability. |
| | 14 15 RESPONSE TO ISSUE NO. 9 16 BY WITNESS JONES: |
| | 17 The feed and bleed method of providing core cooling -- |
| | 18 utilizing the High Pressure Injection System (HPI) to " feed" 19 water to the Reactor Coolant System (RCS) and " bleeding" the 20 water from the RCS through the pressurizer relief (PORV) and/or 21 safety valves -- is an additional method of providing forced 22 cooling which would be used as a defense in depth procedure for 23 events beyond the design basis. |
| | 24 25 26 |
| | . l In the event of a loss of main feedwater transient, with 1 |
| | or without a concurrent small-break LOCA, actuation of emer-2 gency feedwater (resulting in automatic actuation of HPI) or 3 |
| | actuation of HPI within approximately 20 minutes will assure 4 |
| | adequate heat removal througP the steam generators.1/ It is 5 |
| | only for those beyond-design-basis events, involving an 6 |
| | extended loss of both main and emergency feedwater, that feed 7 |
| | and bleed would be required to remove decay heat from the 8 |
| | primary system.2/ |
| | 9 The feed and bleed mode of core cooling has been thor-10 oughly analyzed by B&W in conjunction with the additional 11 small-break LOCA analyses performed following the TMI-2 12 accident. The scenarios analyzed included: (a) a loss of all 13 feedwater (main and emergency) with a single failure in the HPI 14 system, (b) a loss of all feedwater coincident with small 15 breaks of various sizes (0.07 ft2, 0.02 ft2, 0.01 ft2), and (c) 16 a loss of all feedwater with t very small break (0.01 ft2) and 17 with a subsequent PORV failure. (These analyses are summarized 18 19 1/ For small-break LOCAs greater than approximately 0.02 ft2, secondary side heat removal is not required, as the break 20 itself is large enough to remove the core decay heat. In addi-tion, automatic actuation of HPI will occur for these break 21 sizes. |
| | 22 2/ In this case, the inventory injected by the HPI is used to assure the core is covered by liquid coolant or a two-phase 23 mixture and thus adequately cooled, while the water discharged through the PORV or safety valves removes the energy added to 24 the primary system by the core. |
| | 25 26 in Tables 2, 3 and 8 of Licensee's Testimony of Robert C. |
| | 1 Jones, Jr., and T. Gary Broughton in Response to UCS Contention 2 |
| | No. 8 and ECNP Contention No. 1(e), ff. Tr. 5038, and at Tr. |
| | 3 5064-73, 5074-87 and 5103-04 (Jones).) Initiation of HPI -- |
| | 4 and thereby initiation of the feed and bleed mode -- within 5 |
| | approximately 20 minutes (for those cases where the ESFAS 6 |
| | setpoint is not reached) assure:s the provision of adequate core 7 |
| | cooling. |
| | 8 g BY WITNESS LANESE: |
| | 10 At page 39 of ALAB-708, the Appeal Board has requested 11 inf rmation concerning the ability of the TMI-1 safety valves 12 to pass two-phase flow and the effect that this ability may 13 have upon the TMI-1 plant's capability to achieve feed and bleed cooling. GPU Nuclear, in conjunction with other partici-14 15 pating utilities, sponsored a program to test safety and relief valves. The test program was conducted through the Electric 16 Power Research Institute (EPRI). The valves tested included the same model Dresser safety and relief valves used at TMI-1. |
| | 18 g The EPRI test program was the subject of testimony presented before the Licensing Board in response to Board Questions on UCS Contention 6. See Correa, et al., ff. Tr. 8746, and Zudans, ff. Tr. 8824. |
| | The results of those tests showed that the pressurizer relief valve was acceptab.'e for the range of operation at l |
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| | 1 TMI-1, including feed and bleed cooling under both steam and 1 |
| | liquid relief conditions. The safety valves were shown to be 2 |
| | acceptable under all modes of operation after certain modifica-3 tions were made. |
| | 4 First, the safety valve inlet piping has been changed from 5 |
| | a long inlet to a short inlet arrangement. Test results 6 |
| | indicated that valve instabilities could occur for the long 7 |
| | inlet arrangement in situations where the valve was discharging 8 |
| | water from the loop seal. |
| | 9 Second, the TMI-1 safety valve settings were revised to 10 allow blowdown of no more than 20% (versus the previous 11 blowdown of 3%). This increased blowdown eliminates valve 12 instabilities that were detected for both steam and water flow 13 situations. |
| | 14 Four tests were performed in which the TMI-1 model safety 15 valves were required to relieve liquid. One test was a 16 transition from steam to liquid, and three tests were liquid 17 flow tests. In the transition case and two liquid flow cases, IO the valve flow rate met the test acceptance criteria. In the 19 final liquid flow case, pressure in the test loop was not 20 controlled by the valve; however, the valve flow rate (550,000 21 lbm/hr) achieved during the test exceeded the requirements for 22 controlling pressure and cooling the core at TMI-1. All four 23 cases demonstrated that the pressurizer safety valves are 24 suitable for operation in the feed and bleed mode of cooling at 25 26 _4_ |
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| | TMI-1. Moreover, the results confirmed the analysis provided 1 |
| | in Licensee Exhibit 9 (the B&W analysis of feed and ble.ed 2 |
| | cooling). |
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| | 5 6 |
| | 7 81 9 |
| | 10 11 12 13 14 15 16 17 18 19 20 1 |
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| | ROBERT C. JONES, JR. |
| | Business Address: Babcock & Wilcox Company Nuclear Power Generation Division Post Office Box 1260 Lynchburg, Virginia 24505 Education: B.S., Nuclear Engine'ering, Pennsylvania State University, 1971. Post Graduate Courses in Physics, Lynchburg College. |
| | Experience: July 1982 to present; Supervisory Engineer, Operational Analysis Unit, B&W. Responsible for the performance of plant transient analyses and analyses used in the development of operator guidelines. During this period, has continued as Project Engineer for B&W analyses performed in response to NUREG-0737 Item II.K.3.30. |
| | June 1975 to July 1982: Acting Supervisory Engineer and Supervisory Engineer, ECCS Analysis Unit, B&W. Responsible for calculation of large and small break ECCS evaluations, evaluations of mass and energy releases to the containment during a LOCA, and performance of best estimate pretest predictions of LOCA experiments as part of the NRC Standard Problem Program. Involved in the pre-paration of operator guidelines for small-break LOCA's and inadequate core cooling mitigation. |
| | June 1971 to June 1975: Engineer, ECCS Analysis Unit, B&W. Performed both large and small break ECCS analyses under both the Interim Acceptance l Criteria and the present Acceptance Criteria of 10 CFR 50.46 and Appendix K. |
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| | , . , - . . - c. - . - - . r g. g. ., -z.- |
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| | e LOUIS C. LANESE Business Address: GPU Nuclear Corporation 100 Interpace Parkway Parsippany, New Jersey 07054 Education: B.S., Engineering Science, Newark College of Engineering, 1970, M.E., Nuclear Engineering, New York University, 1972. Nuclear Engineering courses, Polytechnic Institute of New York, 1975 to 1980. Com-pleted course work for Degree of Engineer. |
| | Experience: Senior Safety Analysis and Plant Control Engineer, GPU Nuclear Corporation, 1979 to present. Responsi-bilities include the performance of the TMI-l Restart Safety Analysis; TMI-l Emergency Feedwater design, design review of TMI-l restart and long-term modifications. Member of TMI-2 Generation |
| | . Review Committee (GRC), 1979 through June 198.2. |
| | Member of TMI'-l GRC, 1979 to present. |
| | Chairman of the Babcock & Wilcox Owners Group Analysis Subcommittee from May 1981 to July 1982. |
| | Currently a member of the Analysis Subcommittee. |
| | Member of the GPUNC inhouse committee responsible for implementing the Abncrmal Transient Operating Guidelines (ATOG) at TMI-1. Currently working on improvement of steam generator tube rupture emer-gency procedures,* including analyses of tube rupture events using the RETRAN computer code. Working with EPRI in benchmarking RETRAN with RELAP 5 for tube rupture events. Independent safety reviewer for emergency procedures from-August 1982 to present. |
| | Control and Safety Analysis Engineer, GPU Service Corporation, 1978 to 1979. Responsibilities included the performance of containment analyses in support of plant operation; developing analyses in support of the TMI-2 feedwater system modifica-tion; preparation of the TMI-l restart safety analysis. |
| | Lead Nuclear Licensing Engineer, GPU Service Corporation, 1977 to 1978. Primary responsibility for TMI-2 licensing activities and for licensing matters involving generic safety issues affecting all GPU system plants. |
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| | LOUIS C. LANESE Page Two Safety and Licensing Engineer, GPU Service Corporation, 1974 to 1977. Responsibilities included technical resolution of TMI-2 licensing open items; conformance of Forked River systems design to licensing criteria; and, safety review of Oyster Creek radwaste facility. |
| | Assistant Safety and Licensing Engineer, Ebasco Services, Inc., Performed licensing and safety review of St. Lucie Units 1 and 2 Safety Analysis Report pertaining to instrumentation and power systems; cooling water and HVAC systems, radwaste systems; and, accident analysis. Performed dose analyses and developed secondary system source terms. |
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Category:LEGAL TRANSCRIPTS & ORDERS & PLEADINGS
MONTHYEARML20210B8491999-07-21021 July 1999 Exemption from Certain Requirements of 10CFR50.54(w),for Three Mile Island Nuclear Station Unit 2 to Reduce Amount of Insurance for Unit to $50 Million for Onsite Property Damage Coverage ML20206D4141999-04-20020 April 1999 Exemption from Requirements of 10CFR50,App R,Section III.G.2 Re Enclosure of Cable & Equipment & Associated non-safety Related Circuits of One Redundant Train in Fire Barrier Having 1-hour Rating ML20206T7211999-02-11011 February 1999 Memorandum & Order (CLI-99-02).* Denies C George Request for Intervention & Dismisses Subpart M License Transfer Proceeding.With Certificate of Svc.Served on 990211 ML20198A5111998-12-11011 December 1998 Comment Opposing Proposed Rule 10CFR50.65 Re Requirements for Monitoring Effectiveness of Maintenance at Nuclear Power Plants.Proposed Rulemaking Details Collaborative Efforts in That Rule Interjects Change ML20154G2941998-09-17017 September 1998 Transcript of 980917 Public Meeting in Rockville,Md Re License Transfer of TMI-1 from Gpu Nuclear,Inc to Amergen. Pp 1-41 ML20199J0121997-11-20020 November 1997 Comment on Pr 10CFR50 Re Financial Assurance Requirements for Decommisioning Nuclear Power Reactors.Three Mile Island Alert Invokes Comments of P Bradford,Former NRC Member ML20148R7581997-06-30030 June 1997 Comment on NRC Proposed Bulletin 96-001,suppl 1, Control Rod Insertion Problems. Licensee References Proposed Generic Communication, Control Rod Insertion, & Ltrs & 961022 from B&W Owners Group ML20078H0431995-02-0101 February 1995 Comment Opposing Proposed Rule 10CFR50 Re Shutdown & Lowpower Operations for Nuclear Reactors ML20077E8231994-12-0808 December 1994 Comment Supporting Proposed Rules 10CFR2,51 & 54 Re Rev to NRC NPP License Renewal Rule ML20149E2021994-04-20020 April 1994 R Gary Statement Re 10 Mile Rule Under Director'S Decision DD-94-03,dtd 940331 for Tmi.Urges Commissioners to Engage in Reconsideration of Author Petition ML20065Q0671994-04-0707 April 1994 Principal Deficiencies in Director'S Decision 94-03 Re Pica Request Under 10CFR2.206 ML20058A5491993-11-17017 November 1993 Exemption from Requirements in 10CFR50.120 to Establish, Implement & Maintain Training Programs,Using Sys Approach to Training,For Catorgories of Personnel Listed in 10CFR50.120 ML20059J5171993-09-30030 September 1993 Transcript of 930923 Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-130.Related Documentation Encl ML20065J3461992-12-30030 December 1992 Responds to Petition of R Gary Alleging Discrepancies in RERP for Dauphin County,Pa ML20065J3731992-12-18018 December 1992 Affidavit of Gj Giangi Responding to of R Gary Requesting Action by NRC Per 10CFR2.206 ML20198E5581992-12-0101 December 1992 Transcript of Briefing by TMI-2 Advisory Panel on 921201 in Rockville,Md ML20210D7291992-06-15015 June 1992 Exemption from Requirements of 10CFR70.24 Re Criticality Accident Requirements for SNM Storage Areas at Facility Containing U Enriched to Less than 3% in U-235 Isotope ML20079E2181991-09-30030 September 1991 Submits Comments on NRC Proposed Resolution of Generic Issue 23, Reactor Coolant Pump Seal Failure. Informs That Util Endorses Comments Submitted by NUMARC ML20066J3031991-01-28028 January 1991 Comment Supporting SECY-90-347, Regulatory Impact Survey Rept ML20059P0531990-10-15015 October 1990 Comment Opposing Proposed Rules 10CFR2,50 & 54 Re Nuclear Power Plant License Renewal ML20059N5941990-10-0404 October 1990 Transcript of 900928 Public Meeting in Rockville,Md Re Studies of Cancer in Populations Near Nuclear Facilities, Including TMI ML20055F4411990-06-28028 June 1990 Comment Supporting Petition for Rulemaking PRM-50-55 Re Revs to FSAR ML20248J1891989-10-0606 October 1989 Order.* Grants Intervenors 891004 Motion for Permission for Opportunity to Respond to Staff Correspondence.Response Requested No Later That 891020.W/Certificate of Svc.Served on 891006 ML20248J1881989-10-0303 October 1989 Motion for Permission for Opportunity to Respond to Staff Correspondence in Response to Board Order of 890913.* Svc List Encl ML20248J0301989-09-29029 September 1989 NRC Staff Response to Appeal Board Order.* Matters Evaluated in Environ Assessment Involved Subjs Known by Parties During Proceeding & Appear in Hearing Record & Reflect Board Final Initial Decision LBP-89-7.W/Certificate of Svc ML20247E9181989-09-13013 September 1989 Order.* Requests NRC to Explain Purpose of 890911 Fr Notice on Proposed Amend to Applicant License,Revising Tech Specs Re Disposal of Accident Generated Water & Effects on ASLB Findings,By 890929.W/Certificate of Svc.Served on 890913 ML20247G0361989-07-26026 July 1989 Transcript of Oral Argument on 890726 in Bethesda,Md Re Disposal of accident-generated Water.Pp 1-65.Supporting Info Encl ML20247B7781989-07-18018 July 1989 Certificate of Svc.* Certifies Svc of Encl Gpu 890607 & 0628 Ltrs to NRC & Commonwealth of Pa,Respectively.W/Svc List ML20245D3651989-06-20020 June 1989 Notice of Oral Argument.* Oral Argument on Appeal of Susquehanna Valley Alliance & TMI Alert from ASLB 890202 Initial Decision Authorizing OL Amend,Will Be Heard on 890726 in Bethesda,Md.W/Certificate of Svc.Served on 890620 ML20245A5621989-06-14014 June 1989 Order.* Advises That Oral Argument on Appeal of Susquehanna Valley Alliance & TMI Alert from Board 890202 Initial Decision LBP-89-07 Authorizing OL Amend Will Be Heard on 890726 in Bethesda,Md.W/Certificate of Svc.Served on 890614 ML20247F3151989-05-22022 May 1989 NRC Staff Response to Appeal by Joint Intervenors Susquehanna Valley Alliance/Tmi Alert.* Appeal Should Be Denied Based on Failure to Identify Errors in Fact & Law Subj to Appeal.W/Certificate of Svc ML20246Q2971989-05-15015 May 1989 Comment Opposing Proposed Rule 10CFR50 Re Ensuring Effectiveness of Maint Programs for Nuclear Power Plants ML20246J6081989-05-12012 May 1989 Licensee Brief in Reply to Joint Intervenors Appeal from Final Initial Decision.* ASLB 890203 Final Initial Decision LBP-89-07 Re Deleting Prohibition on Disposal of accident- Generated Water Should Be Affirmed.W/Certificate of Svc ML20247D2761989-04-20020 April 1989 Transcript of 890420 Briefing in Rockville,Md on Status of TMI-2 Cleanup Activities.Pp 1-51.Related Info Encl ML20244C0361989-04-13013 April 1989 Order.* Commission Finds That ASLB Decision Resolving All Relevant Matters in Favor of Licensee & Granting Application for OL Amend,Should Become Effective Immediately.Certificate of Svc Encl.Served on 890413 ML20245A8381989-04-13013 April 1989 Transcript of Advisory Panel for Decontamination of TMI-2 890413 Meeting in Harrisburg,Pa.Pp 1-79.Supporting Info Encl ML20245A2961989-04-13013 April 1989 Transcript of 890413 Meeting in Rockville,Md Re Affirmation/Discussion & Vote ML20248H1811989-04-0606 April 1989 Valley Alliance/Tmi Alert Motion for Leave to File Appeal Brief out-of-time.* W/Certificate of Svc.Served on 890411.Granted for Aslab on 890410 ML20248G0151989-04-0606 April 1989 Valley Alliance/Tmi Alert Motion for Leave to File Appeal Brief out-of-time.* Requests to File Appeal Brief 1 Day Late Due to Person Typing Document Having Schedule Problems ML20248G0261989-04-0606 April 1989 Susguehanna Valley Alliance/Tmi Alert Brief in Support of Notification to File Appeal & Request for Oral Argument Re Appeal.* Certificate of Svc Encl ML20248D7211989-04-0404 April 1989 Memorandum & Order.* Intervenors Application for Stay Denied Due to Failure to Lack of Demonstrated Irreparable Injury & Any Showing of Certainty That Intervenors Will Prevail on Merits of Appeal.W/Certificate of Svc.Served on 890404 ML20247A4671989-03-23023 March 1989 Correction Notice.* Advises That Date of 891203 Appearing in Text of Commission 890322 Order Incorrect.Date Should Be 871203.Certificate of Svc Encl.Served on 890323 ML20246M2611989-03-22022 March 1989 Order.* Advises That Commission Currently Considering Question of Effectiveness,Pending Appellate Review of Final Initial Decision in Case Issued by ASLB in LBP-89-07. Certificate of Svc Encl.Served on 890322 ML20236D3821989-03-16016 March 1989 Valley Alliance & TMI Alert Motion for Extension of Time to File Brief in Support of Request for Appeal in Matter of 2.3 Million Gallons Of....* Certificate of Svc Encl.Served on 890316.Granted for Aslab on 890316 ML20236D3121989-03-15015 March 1989 Licensee Answer to Joint Intervenors Motion for Extension of Time to File Brief on Appeal.* Motion Opposed Based on Failure to Demonstrate Good Cause.W/Certificate of Svc ML20236D2901989-03-11011 March 1989 Valley Alliance/Tmi Alert Motion for Extension of Time to File Brief in Support of Request for Appeal in Matter of Disposal of 2.3 Million Gallons of Radioactive Water at Tmi,Unit 2.* Svc List Encl ML20236A3761989-03-0808 March 1989 Licensee Answer Opposing Joint Intervenors Motion for Stay.* Stay of Licensing Board Decision Pending Appeal Unwarranted Under NRC Stds.Stay Could Delay Safe,Expeditious Cleanup of Facility.Certificate of Svc Encl ML20236C2441989-03-0808 March 1989 NRC Staff Response in Opposition to Application for Stay Filed by Joint Intervenors.* Application for Stay of Effectiveness of Final Initial Decision LBP-89-07,dtd 890202 Should Be Denied.W/Certificate of Svc ML20235V2641989-03-0202 March 1989 Notice of Aslab Reconstitution.* TS Moore,Chairman,Cn Kohl & Ha Wilber,Members.Served on 890303.W/Certificate of Svc ML20235V2161989-02-25025 February 1989 Changes & Corrections to Susquehanna Valley Alliance/Three Mile Island Alert Documents Submitted on 890221.* Certificate of Svc Encl 1999-07-21
[Table view] Category:TRANSCRIPTS
MONTHYEARML20154G2941998-09-17017 September 1998 Transcript of 980917 Public Meeting in Rockville,Md Re License Transfer of TMI-1 from Gpu Nuclear,Inc to Amergen. Pp 1-41 ML20059J5171993-09-30030 September 1993 Transcript of 930923 Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-130.Related Documentation Encl ML20198E5581992-12-0101 December 1992 Transcript of Briefing by TMI-2 Advisory Panel on 921201 in Rockville,Md ML20059N5941990-10-0404 October 1990 Transcript of 900928 Public Meeting in Rockville,Md Re Studies of Cancer in Populations Near Nuclear Facilities, Including TMI ML20247G0361989-07-26026 July 1989 Transcript of Oral Argument on 890726 in Bethesda,Md Re Disposal of accident-generated Water.Pp 1-65.Supporting Info Encl ML20247D2761989-04-20020 April 1989 Transcript of 890420 Briefing in Rockville,Md on Status of TMI-2 Cleanup Activities.Pp 1-51.Related Info Encl ML20245A2961989-04-13013 April 1989 Transcript of 890413 Meeting in Rockville,Md Re Affirmation/Discussion & Vote ML20245A8381989-04-13013 April 1989 Transcript of Advisory Panel for Decontamination of TMI-2 890413 Meeting in Harrisburg,Pa.Pp 1-79.Supporting Info Encl ML20235N2161989-02-17017 February 1989 Follow-up Testimony Clarifying Position on Question of Disposition of Over 2 Million Gallons of Accident Generated Water.Related Documentation & Certificate of Svc Encl ML20235S9911989-02-16016 February 1989 Transcript of 890216 Public Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-119. Supporting Documentation Encl ML20206C9391988-11-0707 November 1988 Transcript of 881107 Hearing in Lancaster,Pa.Pp 1,122- 1,417.Witnesses:JA Auxier,Ji Fabrikant,Skolnik & Mather ML20235M7601988-11-0303 November 1988 Transcript of 881103 Public Hearing in Lancaster,Pa for Presentation of Limited Appearance Statements.Pp 998-1,121 ML20206C2801988-11-0303 November 1988 Transcript of 881103 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 859-997.Witnesses:JA Martin, SS Yaniv,F Skolnik,S Lewis & a Bhattacharyya ML20205Q6581988-11-0202 November 1988 Transcript of 881102 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 573-858.Supporting Documentation Encl.Witnesses:Gg Baker,Wj Cooper & L Munson ML20205Q6441988-11-0101 November 1988 Transcript of 881101 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 288-572.Supporting Info Encl. Witnesses:K Hofstetter,Kl Harner,L Thomas & M Masnik ML20205N5791988-10-31031 October 1988 Transcript of ASLB 881031 Meeting in Lancaster,Pa Re License Amend Application.Pp 87-287 ML20205P0451988-10-25025 October 1988 Transcript of 881025 Periodic Briefing by TMI-2 Advisory Panel in Rockville,Md.Pp 1-30 ML20205G1851988-10-25025 October 1988 Licensee Testimony of GG Baker & Wj Cooper on Dose Assessments & Microorganisms (Contentions 2,3 & 5d).* Supporting Documentation Encl.Related Correspondence ML20205E5021988-10-24024 October 1988 Licensee Rebuttal Testimony of Ji Fabrikant on Health Effects of Tritium (Contention 5d).* Related Correspondence ML20155H1751988-10-11011 October 1988 Licensee Testimony of GG Baker & Wj Cooper on Dose Assessments & Microorganisms (Contentions 2,3 & 5d).* Related Correspondence ML20155H1531988-10-11011 October 1988 Licensee Testimony of Ww Weaver on Accident Risks (Contention 2).* Related Correspondence ML20155H1901988-10-11011 October 1988 Licensee Testimony of Ja Auxier & Ji Fabrikant on Effects of Tritium (Contentions 3 & 5d).* Supporting Info Encl.Related Correpondence ML20155H1661988-10-11011 October 1988 Licensee Testimony of Kl Harner & Kj Hofstetter on Sampling & Analysis of accident-generated Water (Contentions 3 & 4b).* Related Correspondence ML20155H1401988-10-11011 October 1988 Licensee Testimony of Je Tarpinian on Occupational Dose Assessments (Contention 2).* Related Correspondence ML20155H1281988-10-11011 October 1988 Licensee Testimony of Dr Buchanan on Evaporation Proposal & Joint Intervenors Alternative (Contentions 2 & 3).* Related Correspondence ML20155H4751988-10-10010 October 1988 Testimony.* Discusses Environ Impact of Force Evaporation of 2.3 Million Gallons of accident-generated Water by Licensee. W/Certificate of Svc.Related Correspondence ML20155H4711988-10-10010 October 1988 Affidavit of Cw Huver (Contention 5):further Considerations of Biological Effects & Health Hazards of Tritium.* Copyrighted Matl Encl.Related Correspondence ML20154D5201988-09-0707 September 1988 Transcript of Advisory Panel for Decontamination of TMI-2 880907 Meeting in Harrisburg,Pa.Pp 1-109.Supporting Documentation Encl ML20151G6951988-07-14014 July 1988 Transcript of Advisory Panel for Decontamination of TMI-2 880714 Meeting in Harrisburg,Pa.Pp 1-140.Related Documentation Encl ML20196B6041988-05-26026 May 1988 Transcript of 880526 Advisory Panel Meeting in Harrisburg, PA to Discuss Decontamination of TMI-2.Pp 1-117.Supporting Documentation Encl ML20154N4101988-04-14014 April 1988 Transcript of 880414 Advisory Panel for Decontamination of TMI-2 Public Meeting in Lancaster,Pa.Related Info Encl. Pp 1-100 ML20148F2351988-03-17017 March 1988 Transcript of 880317 Briefing in Washington,Dc Re Status of TMI-2.Pp 1-51.Supporting Documentation Encl ML20236Y1061987-12-0808 December 1987 Transcript of Special Prehearing Conference on 871208 in Harrisburg,Pa Re Disposal of accident-generated Water. Pp 1-86 ML20238C6981987-10-0505 October 1987 Deposition of a Beach.* Transcript of 871005 Deposition in Washington,Dc Re R Parks Allegations.Pp 1-244.Supporting Documentation Encl ML20235J7071987-09-30030 September 1987 Transcript of 870930 Prehearing Conference in Bethesda,Md. Pp 225-343 ML20238D4641987-09-0909 September 1987 Transcript of 870909 Oral Argument in Bethesda,Md.Pp 1-57 ML20238C7531987-08-20020 August 1987 Vol II to Transcript of Hl Hofmann 870820 Deposition in San Francisco,Ca Re Civil Penalty.Pp 208-471 & 489-494. Supporting Documentation Encl ML20238C7891987-08-18018 August 1987 Deposition of Rd Parks.* Vol IV to Transcript of 870818 Deposition in San Francisco,Ca Re Civil Penalty.Pp 551-818. Supporting Documentation Encl ML20238C7651987-06-25025 June 1987 Deposition of Hl Hofmann.* Transcript of 870625 Deposition in San Francisco,Ca Re Civil Penalty.Pp 1-206 ML20238C8041987-06-24024 June 1987 Deposition of Rd Parks.* Vol III to Transcript of 870624 Deposition in Newport Beach,Ca Re Civil Penalty.Pp III-1 - III-89 ML20235J1271987-06-24024 June 1987 Deposition of Rd Parks.* Vols II & III of Transcript of Rd Parks 870624 Deposition.Related Correspondence ML20238C7981987-06-23023 June 1987 Deposition of Rd Parks.* Vol II to Transcript of 870623 Deposition in Newport Beach,Ca Re Civil Penalty.Pp II-1 - II-263.Supporting Documentation Encl ML20238C7941987-06-22022 June 1987 Deposition of Rd Parks.* Vol I to Transcript of 870622 Deposition in Newport Beach,Ca Re Civil Penalty.Pp 1-199. Supporting Documentation Encl ML20238C5921987-06-16016 June 1987 Deposition of R Meeks.* Transcript of 870616 Deposition in Washington,Dc Re Allegations of Harassment Against R Parks. Pp 1-198.Supporting Documentation Encl ML20238C6171987-06-16016 June 1987 Deposition of R Meeks.* Corrected Title Page of 870616 Deposition ML20215L2731987-05-0808 May 1987 Transcript of 870508 Prehearing Conference in Bethesda,Md.Pp 19-224.In Camera Session (Pp 101-138) Bound Separately ML20238C7331987-04-24024 April 1987 Deposition of Rc Arnold.* Transcript of 870424 Deposition in Washington,Dc Re Civil Penalty.Pp 1-224.Supporting Documentation Encl ML20212Q9801987-04-16016 April 1987 Transcript of 870416 Periodic Meeting W/Advisory Panel for Decontamination of TMI-2 in Washington,Dc.Pp 1-50.Supporting Documentation Encl ML20212Q8021987-04-15015 April 1987 Transcript of 870415 Briefing by DOE in Washington,Dc Re TMI-2 Core Exam Program.Pp 1-64.Viewgraphs Encl ML20238C6521987-04-10010 April 1987 Deposition of Bk Kanga.* Transcript of 870410 Deposition in Gaithersburg,Md Re R Parks.Pp 1-151.Supporting Documentation Encl 1998-09-17
[Table view] Category:DEPOSITIONS
MONTHYEARML20154G2941998-09-17017 September 1998 Transcript of 980917 Public Meeting in Rockville,Md Re License Transfer of TMI-1 from Gpu Nuclear,Inc to Amergen. Pp 1-41 ML20059J5171993-09-30030 September 1993 Transcript of 930923 Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-130.Related Documentation Encl ML20198E5581992-12-0101 December 1992 Transcript of Briefing by TMI-2 Advisory Panel on 921201 in Rockville,Md ML20059N5941990-10-0404 October 1990 Transcript of 900928 Public Meeting in Rockville,Md Re Studies of Cancer in Populations Near Nuclear Facilities, Including TMI ML20247G0361989-07-26026 July 1989 Transcript of Oral Argument on 890726 in Bethesda,Md Re Disposal of accident-generated Water.Pp 1-65.Supporting Info Encl ML20247D2761989-04-20020 April 1989 Transcript of 890420 Briefing in Rockville,Md on Status of TMI-2 Cleanup Activities.Pp 1-51.Related Info Encl ML20245A2961989-04-13013 April 1989 Transcript of 890413 Meeting in Rockville,Md Re Affirmation/Discussion & Vote ML20245A8381989-04-13013 April 1989 Transcript of Advisory Panel for Decontamination of TMI-2 890413 Meeting in Harrisburg,Pa.Pp 1-79.Supporting Info Encl ML20235N2161989-02-17017 February 1989 Follow-up Testimony Clarifying Position on Question of Disposition of Over 2 Million Gallons of Accident Generated Water.Related Documentation & Certificate of Svc Encl ML20235S9911989-02-16016 February 1989 Transcript of 890216 Public Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-119. Supporting Documentation Encl ML20206C9391988-11-0707 November 1988 Transcript of 881107 Hearing in Lancaster,Pa.Pp 1,122- 1,417.Witnesses:JA Auxier,Ji Fabrikant,Skolnik & Mather ML20235M7601988-11-0303 November 1988 Transcript of 881103 Public Hearing in Lancaster,Pa for Presentation of Limited Appearance Statements.Pp 998-1,121 ML20206C2801988-11-0303 November 1988 Transcript of 881103 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 859-997.Witnesses:JA Martin, SS Yaniv,F Skolnik,S Lewis & a Bhattacharyya ML20205Q6581988-11-0202 November 1988 Transcript of 881102 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 573-858.Supporting Documentation Encl.Witnesses:Gg Baker,Wj Cooper & L Munson ML20205Q6441988-11-0101 November 1988 Transcript of 881101 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 288-572.Supporting Info Encl. Witnesses:K Hofstetter,Kl Harner,L Thomas & M Masnik ML20205N5791988-10-31031 October 1988 Transcript of ASLB 881031 Meeting in Lancaster,Pa Re License Amend Application.Pp 87-287 ML20205P0451988-10-25025 October 1988 Transcript of 881025 Periodic Briefing by TMI-2 Advisory Panel in Rockville,Md.Pp 1-30 ML20205G1851988-10-25025 October 1988 Licensee Testimony of GG Baker & Wj Cooper on Dose Assessments & Microorganisms (Contentions 2,3 & 5d).* Supporting Documentation Encl.Related Correspondence ML20205E5021988-10-24024 October 1988 Licensee Rebuttal Testimony of Ji Fabrikant on Health Effects of Tritium (Contention 5d).* Related Correspondence ML20155H1751988-10-11011 October 1988 Licensee Testimony of GG Baker & Wj Cooper on Dose Assessments & Microorganisms (Contentions 2,3 & 5d).* Related Correspondence ML20155H1531988-10-11011 October 1988 Licensee Testimony of Ww Weaver on Accident Risks (Contention 2).* Related Correspondence ML20155H1901988-10-11011 October 1988 Licensee Testimony of Ja Auxier & Ji Fabrikant on Effects of Tritium (Contentions 3 & 5d).* Supporting Info Encl.Related Correpondence ML20155H1661988-10-11011 October 1988 Licensee Testimony of Kl Harner & Kj Hofstetter on Sampling & Analysis of accident-generated Water (Contentions 3 & 4b).* Related Correspondence ML20155H1401988-10-11011 October 1988 Licensee Testimony of Je Tarpinian on Occupational Dose Assessments (Contention 2).* Related Correspondence ML20155H1281988-10-11011 October 1988 Licensee Testimony of Dr Buchanan on Evaporation Proposal & Joint Intervenors Alternative (Contentions 2 & 3).* Related Correspondence ML20155H4751988-10-10010 October 1988 Testimony.* Discusses Environ Impact of Force Evaporation of 2.3 Million Gallons of accident-generated Water by Licensee. W/Certificate of Svc.Related Correspondence ML20155H4711988-10-10010 October 1988 Affidavit of Cw Huver (Contention 5):further Considerations of Biological Effects & Health Hazards of Tritium.* Copyrighted Matl Encl.Related Correspondence ML20154D5201988-09-0707 September 1988 Transcript of Advisory Panel for Decontamination of TMI-2 880907 Meeting in Harrisburg,Pa.Pp 1-109.Supporting Documentation Encl ML20151G6951988-07-14014 July 1988 Transcript of Advisory Panel for Decontamination of TMI-2 880714 Meeting in Harrisburg,Pa.Pp 1-140.Related Documentation Encl ML20196B6041988-05-26026 May 1988 Transcript of 880526 Advisory Panel Meeting in Harrisburg, PA to Discuss Decontamination of TMI-2.Pp 1-117.Supporting Documentation Encl ML20154N4101988-04-14014 April 1988 Transcript of 880414 Advisory Panel for Decontamination of TMI-2 Public Meeting in Lancaster,Pa.Related Info Encl. Pp 1-100 ML20148F2351988-03-17017 March 1988 Transcript of 880317 Briefing in Washington,Dc Re Status of TMI-2.Pp 1-51.Supporting Documentation Encl ML20236Y1061987-12-0808 December 1987 Transcript of Special Prehearing Conference on 871208 in Harrisburg,Pa Re Disposal of accident-generated Water. Pp 1-86 ML20238C6981987-10-0505 October 1987 Deposition of a Beach.* Transcript of 871005 Deposition in Washington,Dc Re R Parks Allegations.Pp 1-244.Supporting Documentation Encl ML20235J7071987-09-30030 September 1987 Transcript of 870930 Prehearing Conference in Bethesda,Md. Pp 225-343 ML20238D4641987-09-0909 September 1987 Transcript of 870909 Oral Argument in Bethesda,Md.Pp 1-57 ML20238C7531987-08-20020 August 1987 Vol II to Transcript of Hl Hofmann 870820 Deposition in San Francisco,Ca Re Civil Penalty.Pp 208-471 & 489-494. Supporting Documentation Encl ML20238C7891987-08-18018 August 1987 Deposition of Rd Parks.* Vol IV to Transcript of 870818 Deposition in San Francisco,Ca Re Civil Penalty.Pp 551-818. Supporting Documentation Encl ML20238C7651987-06-25025 June 1987 Deposition of Hl Hofmann.* Transcript of 870625 Deposition in San Francisco,Ca Re Civil Penalty.Pp 1-206 ML20238C8041987-06-24024 June 1987 Deposition of Rd Parks.* Vol III to Transcript of 870624 Deposition in Newport Beach,Ca Re Civil Penalty.Pp III-1 - III-89 ML20235J1271987-06-24024 June 1987 Deposition of Rd Parks.* Vols II & III of Transcript of Rd Parks 870624 Deposition.Related Correspondence ML20238C7981987-06-23023 June 1987 Deposition of Rd Parks.* Vol II to Transcript of 870623 Deposition in Newport Beach,Ca Re Civil Penalty.Pp II-1 - II-263.Supporting Documentation Encl ML20238C7941987-06-22022 June 1987 Deposition of Rd Parks.* Vol I to Transcript of 870622 Deposition in Newport Beach,Ca Re Civil Penalty.Pp 1-199. Supporting Documentation Encl ML20238C5921987-06-16016 June 1987 Deposition of R Meeks.* Transcript of 870616 Deposition in Washington,Dc Re Allegations of Harassment Against R Parks. Pp 1-198.Supporting Documentation Encl ML20238C6171987-06-16016 June 1987 Deposition of R Meeks.* Corrected Title Page of 870616 Deposition ML20215L2731987-05-0808 May 1987 Transcript of 870508 Prehearing Conference in Bethesda,Md.Pp 19-224.In Camera Session (Pp 101-138) Bound Separately ML20238C7331987-04-24024 April 1987 Deposition of Rc Arnold.* Transcript of 870424 Deposition in Washington,Dc Re Civil Penalty.Pp 1-224.Supporting Documentation Encl ML20212Q9801987-04-16016 April 1987 Transcript of 870416 Periodic Meeting W/Advisory Panel for Decontamination of TMI-2 in Washington,Dc.Pp 1-50.Supporting Documentation Encl ML20212Q8021987-04-15015 April 1987 Transcript of 870415 Briefing by DOE in Washington,Dc Re TMI-2 Core Exam Program.Pp 1-64.Viewgraphs Encl ML20238C6521987-04-10010 April 1987 Deposition of Bk Kanga.* Transcript of 870410 Deposition in Gaithersburg,Md Re R Parks.Pp 1-151.Supporting Documentation Encl 1998-09-17
[Table view] Category:NARRATIVE TESTIMONY
MONTHYEARML20154G2941998-09-17017 September 1998 Transcript of 980917 Public Meeting in Rockville,Md Re License Transfer of TMI-1 from Gpu Nuclear,Inc to Amergen. Pp 1-41 ML20059J5171993-09-30030 September 1993 Transcript of 930923 Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-130.Related Documentation Encl ML20198E5581992-12-0101 December 1992 Transcript of Briefing by TMI-2 Advisory Panel on 921201 in Rockville,Md ML20059N5941990-10-0404 October 1990 Transcript of 900928 Public Meeting in Rockville,Md Re Studies of Cancer in Populations Near Nuclear Facilities, Including TMI ML20247G0361989-07-26026 July 1989 Transcript of Oral Argument on 890726 in Bethesda,Md Re Disposal of accident-generated Water.Pp 1-65.Supporting Info Encl ML20247D2761989-04-20020 April 1989 Transcript of 890420 Briefing in Rockville,Md on Status of TMI-2 Cleanup Activities.Pp 1-51.Related Info Encl ML20245A2961989-04-13013 April 1989 Transcript of 890413 Meeting in Rockville,Md Re Affirmation/Discussion & Vote ML20245A8381989-04-13013 April 1989 Transcript of Advisory Panel for Decontamination of TMI-2 890413 Meeting in Harrisburg,Pa.Pp 1-79.Supporting Info Encl ML20235N2161989-02-17017 February 1989 Follow-up Testimony Clarifying Position on Question of Disposition of Over 2 Million Gallons of Accident Generated Water.Related Documentation & Certificate of Svc Encl ML20235S9911989-02-16016 February 1989 Transcript of 890216 Public Meeting of Advisory Panel for Decontamination of TMI-2 in Harrisburg,Pa.Pp 1-119. Supporting Documentation Encl ML20206C9391988-11-0707 November 1988 Transcript of 881107 Hearing in Lancaster,Pa.Pp 1,122- 1,417.Witnesses:JA Auxier,Ji Fabrikant,Skolnik & Mather ML20235M7601988-11-0303 November 1988 Transcript of 881103 Public Hearing in Lancaster,Pa for Presentation of Limited Appearance Statements.Pp 998-1,121 ML20206C2801988-11-0303 November 1988 Transcript of 881103 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 859-997.Witnesses:JA Martin, SS Yaniv,F Skolnik,S Lewis & a Bhattacharyya ML20205Q6581988-11-0202 November 1988 Transcript of 881102 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 573-858.Supporting Documentation Encl.Witnesses:Gg Baker,Wj Cooper & L Munson ML20205Q6441988-11-0101 November 1988 Transcript of 881101 Hearing in Lancaster,Pa Re TMI-2 License Amend Application.Pp 288-572.Supporting Info Encl. Witnesses:K Hofstetter,Kl Harner,L Thomas & M Masnik ML20205N5791988-10-31031 October 1988 Transcript of ASLB 881031 Meeting in Lancaster,Pa Re License Amend Application.Pp 87-287 ML20205P0451988-10-25025 October 1988 Transcript of 881025 Periodic Briefing by TMI-2 Advisory Panel in Rockville,Md.Pp 1-30 ML20205G1851988-10-25025 October 1988 Licensee Testimony of GG Baker & Wj Cooper on Dose Assessments & Microorganisms (Contentions 2,3 & 5d).* Supporting Documentation Encl.Related Correspondence ML20205E5021988-10-24024 October 1988 Licensee Rebuttal Testimony of Ji Fabrikant on Health Effects of Tritium (Contention 5d).* Related Correspondence ML20155H1751988-10-11011 October 1988 Licensee Testimony of GG Baker & Wj Cooper on Dose Assessments & Microorganisms (Contentions 2,3 & 5d).* Related Correspondence ML20155H1531988-10-11011 October 1988 Licensee Testimony of Ww Weaver on Accident Risks (Contention 2).* Related Correspondence ML20155H1901988-10-11011 October 1988 Licensee Testimony of Ja Auxier & Ji Fabrikant on Effects of Tritium (Contentions 3 & 5d).* Supporting Info Encl.Related Correpondence ML20155H1661988-10-11011 October 1988 Licensee Testimony of Kl Harner & Kj Hofstetter on Sampling & Analysis of accident-generated Water (Contentions 3 & 4b).* Related Correspondence ML20155H1401988-10-11011 October 1988 Licensee Testimony of Je Tarpinian on Occupational Dose Assessments (Contention 2).* Related Correspondence ML20155H1281988-10-11011 October 1988 Licensee Testimony of Dr Buchanan on Evaporation Proposal & Joint Intervenors Alternative (Contentions 2 & 3).* Related Correspondence ML20155H4751988-10-10010 October 1988 Testimony.* Discusses Environ Impact of Force Evaporation of 2.3 Million Gallons of accident-generated Water by Licensee. W/Certificate of Svc.Related Correspondence ML20155H4711988-10-10010 October 1988 Affidavit of Cw Huver (Contention 5):further Considerations of Biological Effects & Health Hazards of Tritium.* Copyrighted Matl Encl.Related Correspondence ML20154D5201988-09-0707 September 1988 Transcript of Advisory Panel for Decontamination of TMI-2 880907 Meeting in Harrisburg,Pa.Pp 1-109.Supporting Documentation Encl ML20151G6951988-07-14014 July 1988 Transcript of Advisory Panel for Decontamination of TMI-2 880714 Meeting in Harrisburg,Pa.Pp 1-140.Related Documentation Encl ML20196B6041988-05-26026 May 1988 Transcript of 880526 Advisory Panel Meeting in Harrisburg, PA to Discuss Decontamination of TMI-2.Pp 1-117.Supporting Documentation Encl ML20154N4101988-04-14014 April 1988 Transcript of 880414 Advisory Panel for Decontamination of TMI-2 Public Meeting in Lancaster,Pa.Related Info Encl. Pp 1-100 ML20148F2351988-03-17017 March 1988 Transcript of 880317 Briefing in Washington,Dc Re Status of TMI-2.Pp 1-51.Supporting Documentation Encl ML20236Y1061987-12-0808 December 1987 Transcript of Special Prehearing Conference on 871208 in Harrisburg,Pa Re Disposal of accident-generated Water. Pp 1-86 ML20238C6981987-10-0505 October 1987 Deposition of a Beach.* Transcript of 871005 Deposition in Washington,Dc Re R Parks Allegations.Pp 1-244.Supporting Documentation Encl ML20235J7071987-09-30030 September 1987 Transcript of 870930 Prehearing Conference in Bethesda,Md. Pp 225-343 ML20238D4641987-09-0909 September 1987 Transcript of 870909 Oral Argument in Bethesda,Md.Pp 1-57 ML20238C7531987-08-20020 August 1987 Vol II to Transcript of Hl Hofmann 870820 Deposition in San Francisco,Ca Re Civil Penalty.Pp 208-471 & 489-494. Supporting Documentation Encl ML20238C7891987-08-18018 August 1987 Deposition of Rd Parks.* Vol IV to Transcript of 870818 Deposition in San Francisco,Ca Re Civil Penalty.Pp 551-818. Supporting Documentation Encl ML20238C7651987-06-25025 June 1987 Deposition of Hl Hofmann.* Transcript of 870625 Deposition in San Francisco,Ca Re Civil Penalty.Pp 1-206 ML20238C8041987-06-24024 June 1987 Deposition of Rd Parks.* Vol III to Transcript of 870624 Deposition in Newport Beach,Ca Re Civil Penalty.Pp III-1 - III-89 ML20235J1271987-06-24024 June 1987 Deposition of Rd Parks.* Vols II & III of Transcript of Rd Parks 870624 Deposition.Related Correspondence ML20238C7981987-06-23023 June 1987 Deposition of Rd Parks.* Vol II to Transcript of 870623 Deposition in Newport Beach,Ca Re Civil Penalty.Pp II-1 - II-263.Supporting Documentation Encl ML20238C7941987-06-22022 June 1987 Deposition of Rd Parks.* Vol I to Transcript of 870622 Deposition in Newport Beach,Ca Re Civil Penalty.Pp 1-199. Supporting Documentation Encl ML20238C5921987-06-16016 June 1987 Deposition of R Meeks.* Transcript of 870616 Deposition in Washington,Dc Re Allegations of Harassment Against R Parks. Pp 1-198.Supporting Documentation Encl ML20238C6171987-06-16016 June 1987 Deposition of R Meeks.* Corrected Title Page of 870616 Deposition ML20215L2731987-05-0808 May 1987 Transcript of 870508 Prehearing Conference in Bethesda,Md.Pp 19-224.In Camera Session (Pp 101-138) Bound Separately ML20238C7331987-04-24024 April 1987 Deposition of Rc Arnold.* Transcript of 870424 Deposition in Washington,Dc Re Civil Penalty.Pp 1-224.Supporting Documentation Encl ML20212Q9801987-04-16016 April 1987 Transcript of 870416 Periodic Meeting W/Advisory Panel for Decontamination of TMI-2 in Washington,Dc.Pp 1-50.Supporting Documentation Encl ML20212Q8021987-04-15015 April 1987 Transcript of 870415 Briefing by DOE in Washington,Dc Re TMI-2 Core Exam Program.Pp 1-64.Viewgraphs Encl ML20238C6521987-04-10010 April 1987 Deposition of Bk Kanga.* Transcript of 870410 Deposition in Gaithersburg,Md Re R Parks.Pp 1-151.Supporting Documentation Encl 1998-09-17
[Table view] |
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February 16, 1983 UNITED STATES OF AMERICA NUCLEAR REGULATORY COMMISSION BEFORE THE ATOM 2"C SAFETY AND LICENSING APPEAL BOARD In the Matter of )
)
METROPOLITAN EDISON COMPANY ) Docket No. 50-289
) (Restart)
(Three Mile Island Nuclear )
Station, Unit No. 1) )
LICENSEE'S TESTIMONY OF ROBERT C. JONES, JR., AND LOUIS C. LANESE IN RESPONSE TO ALAB-708 ISSUE NO. 9 (RELIANCE ON FEED AND BLEED COOLING) 8302220381 830226 (DRADOCK 05000289 PDR
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SUMMARY
l This testimony is in response to the Appeal Board's request that Licensee and the Staff set forth the ponditions for which feed and bleed cooling will be relied upon at TMI-1.
The testimony confirms Licensee's previously stated position that feed and bleed cooling is only required for those beyond design basis events involving an extended loss of both main and emergency feedwater. This testimony also shows that the TMI-1 l- safety valves are capable of successfully relieving two-phase flow.
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INTRODUCTION 1
This testimony, by Robert C. Jones, Jr., Supervisory 2
Engineer, Operational Analysis Unit, Babcock & Wilcox Company, 3
and Louis C. Lanese, Senior Safety Analysis and Plant Control 4
Engineer, GPU Nuclear Corporation, is addressed to Issue No. 9 5
f the Appeal Board's Memorandum and Order of December 29, 1982 6
(ALAB-708), which states:
7
- 9. Whether and under what circumstances reliance 8
on feed and bleed is necessary at TMI-l (from g the licensee and the staff).
10 This testimony will also respond to the concerns expressed by 11 the Appeal Board at page 39 of ALAB-708, regarding the ability 12 f the TMI-l pressurizer safety valves to successfully pass two-phase flow, and the resultant effects on feed and bleed 13 cooling capability.
14 15 RESPONSE TO ISSUE NO. 9 16 BY WITNESS JONES:
17 The feed and bleed method of providing core cooling --
18 utilizing the High Pressure Injection System (HPI) to " feed" 19 water to the Reactor Coolant System (RCS) and " bleeding" the 20 water from the RCS through the pressurizer relief (PORV) and/or 21 safety valves -- is an additional method of providing forced 22 cooling which would be used as a defense in depth procedure for 23 events beyond the design basis.
24 25 26
. l In the event of a loss of main feedwater transient, with 1
or without a concurrent small-break LOCA, actuation of emer-2 gency feedwater (resulting in automatic actuation of HPI) or 3
actuation of HPI within approximately 20 minutes will assure 4
adequate heat removal througP the steam generators.1/ It is 5
only for those beyond-design-basis events, involving an 6
extended loss of both main and emergency feedwater, that feed 7
and bleed would be required to remove decay heat from the 8
primary system.2/
9 The feed and bleed mode of core cooling has been thor-10 oughly analyzed by B&W in conjunction with the additional 11 small-break LOCA analyses performed following the TMI-2 12 accident. The scenarios analyzed included: (a) a loss of all 13 feedwater (main and emergency) with a single failure in the HPI 14 system, (b) a loss of all feedwater coincident with small 15 breaks of various sizes (0.07 ft2, 0.02 ft2, 0.01 ft2), and (c) 16 a loss of all feedwater with t very small break (0.01 ft2) and 17 with a subsequent PORV failure. (These analyses are summarized 18 19 1/ For small-break LOCAs greater than approximately 0.02 ft2, secondary side heat removal is not required, as the break 20 itself is large enough to remove the core decay heat. In addi-tion, automatic actuation of HPI will occur for these break 21 sizes.
22 2/ In this case, the inventory injected by the HPI is used to assure the core is covered by liquid coolant or a two-phase 23 mixture and thus adequately cooled, while the water discharged through the PORV or safety valves removes the energy added to 24 the primary system by the core.
25 26 in Tables 2, 3 and 8 of Licensee's Testimony of Robert C.
1 Jones, Jr., and T. Gary Broughton in Response to UCS Contention 2
No. 8 and ECNP Contention No. 1(e), ff. Tr. 5038, and at Tr.
3 5064-73, 5074-87 and 5103-04 (Jones).) Initiation of HPI --
4 and thereby initiation of the feed and bleed mode -- within 5
approximately 20 minutes (for those cases where the ESFAS 6
setpoint is not reached) assure:s the provision of adequate core 7
cooling.
8 g BY WITNESS LANESE:
10 At page 39 of ALAB-708, the Appeal Board has requested 11 inf rmation concerning the ability of the TMI-1 safety valves 12 to pass two-phase flow and the effect that this ability may 13 have upon the TMI-1 plant's capability to achieve feed and bleed cooling. GPU Nuclear, in conjunction with other partici-14 15 pating utilities, sponsored a program to test safety and relief valves. The test program was conducted through the Electric 16 Power Research Institute (EPRI). The valves tested included the same model Dresser safety and relief valves used at TMI-1.
18 g The EPRI test program was the subject of testimony presented before the Licensing Board in response to Board Questions on UCS Contention 6. See Correa, et al., ff. Tr. 8746, and Zudans, ff. Tr. 8824.
The results of those tests showed that the pressurizer relief valve was acceptab.'e for the range of operation at l
25 l 26 i
l
1 TMI-1, including feed and bleed cooling under both steam and 1
liquid relief conditions. The safety valves were shown to be 2
acceptable under all modes of operation after certain modifica-3 tions were made.
4 First, the safety valve inlet piping has been changed from 5
a long inlet to a short inlet arrangement. Test results 6
indicated that valve instabilities could occur for the long 7
inlet arrangement in situations where the valve was discharging 8
water from the loop seal.
9 Second, the TMI-1 safety valve settings were revised to 10 allow blowdown of no more than 20% (versus the previous 11 blowdown of 3%). This increased blowdown eliminates valve 12 instabilities that were detected for both steam and water flow 13 situations.
14 Four tests were performed in which the TMI-1 model safety 15 valves were required to relieve liquid. One test was a 16 transition from steam to liquid, and three tests were liquid 17 flow tests. In the transition case and two liquid flow cases, IO the valve flow rate met the test acceptance criteria. In the 19 final liquid flow case, pressure in the test loop was not 20 controlled by the valve; however, the valve flow rate (550,000 21 lbm/hr) achieved during the test exceeded the requirements for 22 controlling pressure and cooling the core at TMI-1. All four 23 cases demonstrated that the pressurizer safety valves are 24 suitable for operation in the feed and bleed mode of cooling at 25 26 _4_
TMI-1. Moreover, the results confirmed the analysis provided 1
in Licensee Exhibit 9 (the B&W analysis of feed and ble.ed 2
cooling).
3 4
5 6
7 81 9
10 11 12 13 14 15 16 17 18 19 20 1
l 21 22 l 23 24 l
25 26 I
ROBERT C. JONES, JR.
Business Address: Babcock & Wilcox Company Nuclear Power Generation Division Post Office Box 1260 Lynchburg, Virginia 24505 Education: B.S., Nuclear Engine'ering, Pennsylvania State University, 1971. Post Graduate Courses in Physics, Lynchburg College.
Experience: July 1982 to present; Supervisory Engineer, Operational Analysis Unit, B&W. Responsible for the performance of plant transient analyses and analyses used in the development of operator guidelines. During this period, has continued as Project Engineer for B&W analyses performed in response to NUREG-0737 Item II.K.3.30.
June 1975 to July 1982: Acting Supervisory Engineer and Supervisory Engineer, ECCS Analysis Unit, B&W. Responsible for calculation of large and small break ECCS evaluations, evaluations of mass and energy releases to the containment during a LOCA, and performance of best estimate pretest predictions of LOCA experiments as part of the NRC Standard Problem Program. Involved in the pre-paration of operator guidelines for small-break LOCA's and inadequate core cooling mitigation.
June 1971 to June 1975: Engineer, ECCS Analysis Unit, B&W. Performed both large and small break ECCS analyses under both the Interim Acceptance l Criteria and the present Acceptance Criteria of 10 CFR 50.46 and Appendix K.
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, . , - . . - c. - . - - . r g. g. ., -z.-
e LOUIS C. LANESE Business Address: GPU Nuclear Corporation 100 Interpace Parkway Parsippany, New Jersey 07054 Education: B.S., Engineering Science, Newark College of Engineering, 1970, M.E., Nuclear Engineering, New York University, 1972. Nuclear Engineering courses, Polytechnic Institute of New York, 1975 to 1980. Com-pleted course work for Degree of Engineer.
Experience: Senior Safety Analysis and Plant Control Engineer, GPU Nuclear Corporation, 1979 to present. Responsi-bilities include the performance of the TMI-l Restart Safety Analysis; TMI-l Emergency Feedwater design, design review of TMI-l restart and long-term modifications. Member of TMI-2 Generation
. Review Committee (GRC), 1979 through June 198.2.
Member of TMI'-l GRC, 1979 to present.
Chairman of the Babcock & Wilcox Owners Group Analysis Subcommittee from May 1981 to July 1982.
Currently a member of the Analysis Subcommittee.
Member of the GPUNC inhouse committee responsible for implementing the Abncrmal Transient Operating Guidelines (ATOG) at TMI-1. Currently working on improvement of steam generator tube rupture emer-gency procedures,* including analyses of tube rupture events using the RETRAN computer code. Working with EPRI in benchmarking RETRAN with RELAP 5 for tube rupture events. Independent safety reviewer for emergency procedures from-August 1982 to present.
Control and Safety Analysis Engineer, GPU Service Corporation, 1978 to 1979. Responsibilities included the performance of containment analyses in support of plant operation; developing analyses in support of the TMI-2 feedwater system modifica-tion; preparation of the TMI-l restart safety analysis.
Lead Nuclear Licensing Engineer, GPU Service Corporation, 1977 to 1978. Primary responsibility for TMI-2 licensing activities and for licensing matters involving generic safety issues affecting all GPU system plants.
LOUIS C. LANESE Page Two Safety and Licensing Engineer, GPU Service Corporation, 1974 to 1977. Responsibilities included technical resolution of TMI-2 licensing open items; conformance of Forked River systems design to licensing criteria; and, safety review of Oyster Creek radwaste facility.
Assistant Safety and Licensing Engineer, Ebasco Services, Inc., Performed licensing and safety review of St. Lucie Units 1 and 2 Safety Analysis Report pertaining to instrumentation and power systems; cooling water and HVAC systems, radwaste systems; and, accident analysis. Performed dose analyses and developed secondary system source terms.
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