ML19351E894: Difference between revisions
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{{#Wiki_filter:l l | {{#Wiki_filter:l l | ||
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w@ S :s ) | w@ S :s ) | ||
* l l | |||
* l | l s . . . | ||
s . . . | |||
CPEZAT:NC DATA RI?CR" , | CPEZAT:NC DATA RI?CR" , | ||
, . 1 DCC:C7NO. 50-316 1 DATI 12-3 A0 l W.T. G111ett | , . 1 DCC:C7NO. 50-316 1 DATI 12-3 A0 l W.T. G111ett COMPL.. ; y, f 7" ".*fCNI 616-465-5901 l l | ||
CP!aAT"NG 5"ATCS . | |||
COMPL.. ; y, f 7" ".*fCNI 616-465-5901 l | |||
Donald C. Cook 2 No:= | Donald C. Cook 2 No:= | ||
g - | g - | ||
Novem0er 1980 | Novem0er 1980 | ||
: g ,,4 pg . 3391 | : g ,,4 pg . 3391 l | ||
l | |||
~ | ~ | ||
: 3. L.sansedThs==al?swer(MWt): 1133 | : 3. L.sansedThs==al?swer(MWt): 1133 | ||
: 4. Namesiase As:i=g (Csess 50Ve): f l 1100 | : 4. Namesiase As:i=g (Csess 50Ve): f l 1100 | ||
: 5. Design "*W R::ing(Mes SDVe): | : 5. Design "*W R::ing(Mes SDVe): | ||
1110 l | 1110 l | ||
: 6. hum Dependshte Capaci:y (Cross 11Weg ) | : 6. hum Dependshte Capaci:y (Cross 11Weg ) | ||
| Line 58: | Line 41: | ||
: 5. If Champs ce=stin Capaci:7 Razf=gs (Itar=: Nu=ser 3 Th:ougi: 7) Sisca L::: Reper:. C;ve Ruscas: 1 | : 5. If Champs ce=stin Capaci:7 Razf=gs (Itar=: Nu=ser 3 Th:ougi: 7) Sisca L::: Reper:. C;ve Ruscas: 1 | ||
. l i | . l i | ||
: 9. ?mver Level To Mi=h 2ar=- R If Any (Not 3Cve): | : 9. ?mver Level To Mi=h 2ar=- R If Any (Not 3Cve): | ||
: 10. Ransons For ?"-d- IfAsy: | : 10. Ransons For ?"-d- IfAsy: | ||
l | l 1 | ||
Y to.Cata Cu:=n!= rave j This51oash . | |||
k 720 8,040 25,560 . | k 720 8,040 25,560 . | ||
l | l | ||
| Line 84: | Line 61: | ||
- 0 71.6 | - 0 71.6 | ||
::. Unit Capaczy 7:snar(Using >lDC.Wr) 70.4 66.0 0 l | ::. Unit Capaczy 7:snar(Using >lDC.Wr) 70.4 66.0 0 l | ||
::. Unis Caa city F:c:or(Using CER Nect 15.6 14.6 | ::. Unis Caa city F:c:or(Using CER Nect 15.6 14.6 100 | ||
100 | |||
: 23. Unic Forend Cu=ge Rac, . | : 23. Unic Forend Cu=ge Rac, . | ||
: 24. Shutdowns M '"tu CverNex: 6 Ston:hs(Type. Oste.:sd Cic=: ion of E:ci::: | : 24. Shutdowns M '"tu CverNex: 6 Ston:hs(Type. Oste.:sd Cic=: ion of E:ci::: | ||
| Line 93: | Line 67: | ||
Foreast Achieved . | Foreast Achieved . | ||
. 25. Caits is Tes: Sc: s IP:ior to C -=arci:1 Ops;:: font: | . 25. Caits is Tes: Sc: s IP:ior to C -=arci:1 Ops;:: font: | ||
INITIA L C?.!TICALITY .. . , , | INITIA L C?.!TICALITY .. . , , | ||
INiTZAL I*a ..a. 07:"f CO.*:*.:ZZC A :. C.*ER.GCN | INiTZAL I*a ..a. 07:"f CO.*:*.:ZZC A :. C.*ER.GCN | ||
($8(~71 | ($8(~71 8012T9000$ | ||
8012T9000$ | |||
- - , _ _ . - - - , y--,_, - -._,-,,y._w,, , , , - , , , ..m,_,-,,,,u,,,m,,, ,,-cy,y ,-,, , , , ,....,__,w-m.....,,_,,__,,,..,y,,... - | - - , _ _ . - - - , y--,_, - -._,-,,y._w,, , , , - , , , ..m,_,-,,,,u,,,m,,, ,,-cy,y ,-,, , , , ,....,__,w-m.....,,_,,__,,,..,y,,... - | ||
v..- - . , , , , , , , _ , . . _ - , , . _ . , .- | v..- - . , , , , , , , _ , . . _ - , , . _ . , .- | ||
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-316 UNIT 2 DATE 12-3-80 COMPLETED BY W.T. Gillett TELEPHONE 616-465-5901 MONTH November 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net) (MWe-Net) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 , | |||
AVERAGE DAILY UNIT POWER LEVEL | |||
DOCKET NO. 50-316 UNIT 2 DATE 12-3-80 COMPLETED BY W.T. Gillett TELEPHONE 616-465-5901 MONTH November 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net) (MWe-Net) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 , | |||
l 6 0 22 0 l | l 6 0 22 0 l | ||
7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 , | 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 , | ||
! 14 0 30 0 | ! 14 0 30 0 15 0 31 0 16 0 1 | ||
i INSTRUCTIONS On this famat list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whola megawatt. | i INSTRUCTIONS On this famat list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whola megawatt. | ||
l | l | ||
I ' ' | I ' ' | ||
.t . | .t . | ||
. I ' i . . - | . I ' i . . - | ||
! ; | ! ; | ||
; , | ; , | ||
| Line 134: | Line 91: | ||
CohlPLiclED uy 8. A. Svensson l | CohlPLiclED uy 8. A. Svensson l | ||
! ' i HEPORT &'lONill November, 1980 j ! | ! ' i HEPORT &'lONill November, 1980 j ! | ||
lEl.LPilONE (616) 465-5901 | lEl.LPilONE (616) 465-5901 w | ||
w | |||
''Le ' | ''Le ' | ||
e - | e - | ||
.h 2 I ICensee U$. g"1. | .h 2 I ICensee U$. g"1. | ||
g Cause & Cossc(sive No. Date | g Cause & Cossc(sive No. Date | ||
;; $h livent g,? 3 | ;; $h livent g,? 3 | ||
{ | { | ||
Attiam to | Attiam to 9; g s' o s se gU l | ||
P a6 gE w@ Hepois # La O Psevent Hecuencenc | |||
a6 gE w@ Hepois # La O Psevent Hecuencenc | |||
) 0 1 . | ) 0 1 . | ||
89 | 89 | ||
; | ; | ||
Cont'd. 801018 F 720 A 3 N.A. IIA GENERA Electrical generator repair outage continued from previous month. The unit remained out of service at the | Cont'd. 801018 F 720 A 3 N.A. IIA GENERA Electrical generator repair outage continued from previous month. The unit remained out of service at the end of the month. Return to service i | ||
end of the month. Return to service i | |||
is scheduled for the week of December | is scheduled for the week of December | ||
; . 8, 1980. | ; . 8, 1980. | ||
: CcE2) | : CcE2) | ||
- GEED | - GEED | ||
: W e) 1 2 3 4 1;: Fenced S: Stliedulcil Heason: | : W e) 1 2 3 4 1;: Fenced S: Stliedulcil Heason: | ||
A-l'ilnipmens Failmo(1.nplain) hictinal: | A-l'ilnipmens Failmo(1.nplain) hictinal: | ||
l-blannal lixhibit G . Instantitons for Psepasation of Data | l-blannal lixhibit G . Instantitons for Psepasation of Data Il blalutenance oi Test 2 Manual Sciam, lintiy Slicens fm 1.icensee g C Hefueling 3 Automatic Sciam. Event l<cpust (I IIH) I'de INIIRIE -_- | ||
Il blalutenance oi Test 2 Manual Sciam, lintiy Slicens fm 1.icensee g C Hefueling 3 Automatic Sciam. Event l<cpust (I IIH) I'de INIIRIE -_- | |||
D Hegulaimy itestsiclion I!-Opesato l'eahdng& License lixaminallon 4-Oilies (E xpl.iin) 0161) pg F Administrative G Opesasional llenos (lixplain) 5 | D Hegulaimy itestsiclion I!-Opesato l'eahdng& License lixaminallon 4-Oilies (E xpl.iin) 0161) pg F Administrative G Opesasional llenos (lixplain) 5 | ||
'lisinbis 1 - S.sme Soma M | 'lisinbis 1 - S.sme Soma M | ||
y | y l'l/17) ll Othes (Emplain) | ||
l'l/17) ll Othes (Emplain) | |||
V | V | ||
~ | ~ | ||
Docket No.: 50-316 Unit Nama: D. C. Cook Unit #2 Completed By: R. S. Keith Telephone: (616) 465-5901 Date: December 12, 1980 Page: 1 of 1 MONTHLY OPERATING ACTIVITIES - NOVEMBER, 1980 Highlights: | |||
Docket No.: 50-316 | |||
Unit Nama: D. C. Cook Unit #2 Completed By: R. S. Keith Telephone: (616) 465-5901 Date: December 12, 1980 Page: 1 of 1 MONTHLY OPERATING ACTIVITIES - NOVEMBER, 1980 Highlights: | |||
The unplanned outage that started October 18, 1980 with a Generator trip from 1007. power continued the entire month. | The unplanned outage that started October 18, 1980 with a Generator trip from 1007. power continued the entire month. | ||
The Unit was in Mode 5 the entire month with the Reactor Coolant System at-the loop level for modification to the Peactor Coolant Pump Motor Oil System. | The Unit was in Mode 5 the entire month with the Reactor Coolant System at-the loop level for modification to the Peactor Coolant Pump Motor Oil System. | ||
Summary: | Summary: | ||
Major repair work performed during this report period included: | Major repair work performed during this report period included: | ||
| Line 191: | Line 128: | ||
~ ~~ | ~ ~~ | ||
f) Inspection of Moisture Separator. | f) Inspection of Moisture Separator. | ||
g) Installed new fasteners in Reactor Coolant Pump fire | g) Installed new fasteners in Reactor Coolant Pump fire protection casings. | ||
protection casings | |||
h) Numerous repairs to correct packing gland and body l to bonnet leaks on steam system valves. | h) Numerous repairs to correct packing gland and body l to bonnet leaks on steam system valves. | ||
'~~ | '~~ | ||
i) Installed additional grating in all low pressure turbine | i) Installed additional grating in all low pressure turbine | ||
:__ condensers. | :__ condensers. | ||
- m. * , - * , . - r , - - - . . , 7 g ey g- | - m. * , - * , . - r , - - - . . , 7 g ey g- | ||
DOCKET NO. 50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 12-11-80 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE NOVEMBER, 1980 M-1 The steam inlet flange to the auxiliary feedpump turbine was leaking. Replaced the flexitallic gasket. Studs were checked for cracks by ncndestructive examination. | DOCKET NO. 50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 12-11-80 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE NOVEMBER, 1980 M-1 The steam inlet flange to the auxiliary feedpump turbine was leaking. Replaced the flexitallic gasket. Studs were checked for cracks by ncndestructive examination. | ||
M-2 No. 4 steam generator power operated relief valve, MRV-243 was leaking by. Replaced the cage and disc and machined,the pilot disc. Proper valve operation was verified. | M-2 No. 4 steam generator power operated relief valve, MRV-243 was leaking by. Replaced the cage and disc and machined,the pilot disc. Proper valve operation was verified. | ||
| Line 210: | Line 140: | ||
M-4 Containment spray header drain isolation valve, 2-CTS-123E was leaking by. A new valve was installed. Necessary NDE was per-formed. | M-4 Containment spray header drain isolation valve, 2-CTS-123E was leaking by. A new valve was installed. Necessary NDE was per-formed. | ||
C&I-l MRV-223, steam generator No. 2 power operated relief valve could only be opened 50% when controlled by the hand / auto station in the control room. The valve's positioner was repaired and the calibration was performed. | C&I-l MRV-223, steam generator No. 2 power operated relief valve could only be opened 50% when controlled by the hand / auto station in the control room. The valve's positioner was repaired and the calibration was performed. | ||
C&I-2 The low alarm for the AB diesel generator intake air filter was periodically received. The transmation thermostat control for the heater had failed. A failed capacitor was replaced. The | C&I-2 The low alarm for the AB diesel generator intake air filter was periodically received. The transmation thermostat control for the heater had failed. A failed capacitor was replaced. The thermostat and alarm unit were calibrated and returned _to ser vice. | ||
thermostat and alarm unit were calibrated and returned _to ser vice. | |||
m--e- w we | m--e- w we | ||
-*Me''*w-e eg-N* *' ad=mm M- -D- N- g +==-- eww ege wegee | -*Me''*w-e eg-N* *' ad=mm M- -D- N- g +==-- eww ege wegee | ||
_sy}} | _sy}} | ||
Revision as of 22:43, 30 January 2020
| ML19351E894 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 12/03/1980 |
| From: | Gillett W INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | |
| Shared Package | |
| ML19351E889 | List: |
| References | |
| NUDOCS 8012190505 | |
| Download: ML19351E894 (6) | |
Text
l l
-' g w w. bg o 0 .
w@ S :s )
- l l
l s . . .
CPEZAT:NC DATA RI?CR" ,
, . 1 DCC:C7NO. 50-316 1 DATI 12-3 A0 l W.T. G111ett COMPL.. ; y, f 7" ".*fCNI 616-465-5901 l l
CP!aAT"NG 5"ATCS .
Donald C. Cook 2 No:=
g -
Novem0er 1980
- g ,,4 pg . 3391 l
~
- 3. L.sansedThs==al?swer(MWt): 1133
- 4. Namesiase As:i=g (Csess 50Ve): f l 1100
- 5. Design "*W R::ing(Mes SDVe):
1110 l
- 6. hum Dependshte Capaci:y (Cross 11Weg )
1082
- 7. '.fazunan D-~~'* <*---~y (Nec Mwe):
l
- 5. If Champs ce=stin Capaci:7 Razf=gs (Itar=: Nu=ser 3 Th:ougi: 7) Sisca L::: Reper:. C;ve Ruscas: 1
. l i
- 9. ?mver Level To Mi=h 2ar=- R If Any (Not 3Cve):
- 10. Ransons For ?"-d- IfAsy:
l 1
Y to.Cata Cu:=n!= rave j This51oash .
k 720 8,040 25,560 .
l
- 11. ha.-s Is Rapor:iss Ped 6,160.4- 17,240.3 0
- 12. Nwasar Cf Esa:s Ranc:or w:C" s r 0 0 0 i
0 -
1.' Eoans C-m Ca.L*ns 0 0 0 I
- 15. U=ic Raserve Shardown Eat =s 19.906.4 % 52.130.876 0
- 16. Censs Thennal!===3y c- d OtwH) 6.457,370 16.611.780 ,
0 __,,
- 17. Cros EInc=fc=1Isargy C-~d G.twH) 6.228,971 15,996,383 l 0
ts. Nec :t i Isargy c -,' g.:wE) 71.9 0 75.5- l
- 19. Unit Service8se:or 75.5 71.9 l 0
- 23. Unic Ar ilmoi!Ly 7:c:or 66.7 ;
- 0 71.6
- . Unit Capaczy 7:snar(Using >lDC.Wr) 70.4 66.0 0 l
- . Unis Caa city F:c:or(Using CER Nect 15.6 14.6 100
- 23. Unic Forend Cu=ge Rac, .
- 24. Shutdowns M '"tu CverNex: 6 Ston:hs(Type. Oste.:sd Cic=: ion of E:ci:::
- 25. If Sh:: Cown At End Cr Repore ?sriod. I::ussed Oste of $cs.-==:
Foreast Achieved .
. 25. Caits is Tes: Sc: s IP:ior to C -=arci:1 Ops;:: font:
INITIA L C?.!TICALITY .. . , ,
INiTZAL I*a ..a. 07:"f CO.*:*.:ZZC A :. C.*ER.GCN
($8(~71 8012T9000$
- - , _ _ . - - - , y--,_, - -._,-,,y._w,, , , , - , , , ..m,_,-,,,,u,,,m,,, ,,-cy,y ,-,, , , , ,....,__,w-m.....,,_,,__,,,..,y,,... -
v..- - . , , , , , , , _ , . . _ - , , . _ . , .-
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-316 UNIT 2 DATE 12-3-80 COMPLETED BY W.T. Gillett TELEPHONE 616-465-5901 MONTH November 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net) (MWe-Net) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 ,
l 6 0 22 0 l
7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 ,
! 14 0 30 0 15 0 31 0 16 0 1
i INSTRUCTIONS On this famat list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whola megawatt.
l
I ' '
.t .
. I ' i . . -
! ;
- ,
l DOCKETNO.
50 - 316 . .
!, UNIT SilU1 DOWNS AND POWE:H REI)UCTIONS UNil' N AhlE D.C. Cook - Unit 2 I DATE 12-11-80
' i ,
CohlPLiclED uy 8. A. Svensson l
! ' i HEPORT &'lONill November, 1980 j !
lEl.LPilONE (616) 465-5901 w
Le '
e -
.h 2 I ICensee U$. g"1.
g Cause & Cossc(sive No. Date
- $h livent g,? 3
{
Attiam to 9; g s' o s se gU l
P a6 gE w@ Hepois # La O Psevent Hecuencenc
) 0 1 .
89
Cont'd. 801018 F 720 A 3 N.A. IIA GENERA Electrical generator repair outage continued from previous month. The unit remained out of service at the end of the month. Return to service i
is scheduled for the week of December
- . 8, 1980.
- CcE2)
- GEED
- W e) 1 2 3 4 1;: Fenced S: Stliedulcil Heason:
A-l'ilnipmens Failmo(1.nplain) hictinal:
l-blannal lixhibit G . Instantitons for Psepasation of Data Il blalutenance oi Test 2 Manual Sciam, lintiy Slicens fm 1.icensee g C Hefueling 3 Automatic Sciam. Event l<cpust (I IIH) I'de INIIRIE -_-
D Hegulaimy itestsiclion I!-Opesato l'eahdng& License lixaminallon 4-Oilies (E xpl.iin) 0161) pg F Administrative G Opesasional llenos (lixplain) 5
'lisinbis 1 - S.sme Soma M
y l'l/17) ll Othes (Emplain)
V
~
Docket No.: 50-316 Unit Nama: D. C. Cook Unit #2 Completed By: R. S. Keith Telephone: (616) 465-5901 Date: December 12, 1980 Page: 1 of 1 MONTHLY OPERATING ACTIVITIES - NOVEMBER, 1980 Highlights:
The unplanned outage that started October 18, 1980 with a Generator trip from 1007. power continued the entire month.
The Unit was in Mode 5 the entire month with the Reactor Coolant System at-the loop level for modification to the Peactor Coolant Pump Motor Oil System.
Summary:
Major repair work performed during this report period included:
a) Replace 4 bars in main generator stator, b) Modification to main turbine bearing #2 housing.
c) Inspection of Main Transformer instrumentation.
d) Ice Condenser Ice Basket Weighing.
e) Repairs to "A" Low Pressure Turbine Stop and Intercept Valves.
~ ~~
f) Inspection of Moisture Separator.
g) Installed new fasteners in Reactor Coolant Pump fire protection casings.
h) Numerous repairs to correct packing gland and body l to bonnet leaks on steam system valves.
'~~
i) Installed additional grating in all low pressure turbine
- __ condensers.
- m. * , - * , . - r , - - - . . , 7 g ey g-
DOCKET NO. 50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 12-11-80 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE NOVEMBER, 1980 M-1 The steam inlet flange to the auxiliary feedpump turbine was leaking. Replaced the flexitallic gasket. Studs were checked for cracks by ncndestructive examination.
M-2 No. 4 steam generator power operated relief valve, MRV-243 was leaking by. Replaced the cage and disc and machined,the pilot disc. Proper valve operation was verified.
M-3 East containment spray heat exchanger inlet isolation valve, CTS-121E was leaking by. Machined valve seats and reassembled with new gaskets.
M-4 Containment spray header drain isolation valve, 2-CTS-123E was leaking by. A new valve was installed. Necessary NDE was per-formed.
C&I-l MRV-223, steam generator No. 2 power operated relief valve could only be opened 50% when controlled by the hand / auto station in the control room. The valve's positioner was repaired and the calibration was performed.
C&I-2 The low alarm for the AB diesel generator intake air filter was periodically received. The transmation thermostat control for the heater had failed. A failed capacitor was replaced. The thermostat and alarm unit were calibrated and returned _to ser vice.
m--e- w we
-*Me*w-e eg-N* *' ad=mm M- -D- N- g +==-- eww ege wegee
_sy