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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II SAM NUNN ATLANTA FEDERAL CENTER 61 FORSYTH STREET, SW, SUITE 23T85 ATLANTA, GEORGIA 30303-8931
{{#Wiki_filter:UNITED STATES
  March 31, 2010  
                                NUCLEAR REGULATORY COMMISSION
 
                                                REGION II
Mr. Regis T. Repko Vice President Duke Power Company, LLC d/b/a Duke Energy Carolinas, LLC McGuire Nuclear Station  
                                  SAM NUNN ATLANTA FEDERAL CENTER
MG01VP/12700 Hagers Ferry Road Huntersville, NC 28078  
                                  61 FORSYTH STREET, SW, SUITE 23T85
SUBJECT: MCGUIRE NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTION REPORT 05000369/2010007 AND 05000370/2010007  
                                      ATLANTA, GEORGIA 30303-8931
Dear Mr. Repko:  
                                            March 31, 2010
Mr. Regis T. Repko
Vice President
Duke Power Company, LLC
d/b/a Duke Energy Carolinas, LLC
McGuire Nuclear Station
MG01VP/12700 Hagers Ferry Road
Huntersville, NC 28078
SUBJECT:       MCGUIRE NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTION
                REPORT 05000369/2010007 AND 05000370/2010007
Dear Mr. Repko:
On March 9, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed a supplemental
inspection pursuant to Inspection Procedure 95001, Inspection for One or Two White Inputs in
a Strategic Performance Area, at your McGuire Nuclear Station, Units 1 and 2. The enclosed
inspection report documents the inspection results, which were discussed at the exit meeting on
March 9, 2010, with Mr. Steven D. Capps and other members of your staff.
As required by the NRC Reactor Oversight Process Action Matrix, this supplemental inspection
was performed because a finding of low to moderate safety significance (White) was identified
in the third quarter of 2008 for failure to correct a significant condition adverse to quality related
to macro-fouling of the nuclear service water (RN) system strainers. This finding was
documented previously in NRC Inspection Report 05000369,370/2008009 and resulted in
Violation (VIO) 05000369,370/2008009-01, Failure to Take Adequate Corrective Action for
Implementation of Safety-Related RN Strainer Backwash. The NRC was informed of your
readiness for the inspection on January 11, 2010.
The objectives of this supplemental inspection were to provide assurance that: (1) the root
causes and the contributing causes for the risk-significant issues were understood; (2) the
extent of condition and extent of cause of the issues were identified; and (3) corrective actions
were or will be sufficient to address and preclude repetition of the root and contributing causes.
This inspection examined activities conducted under your license as they related to safety and
compliance with the Commission's rules and regulations, and with the conditions of your
license. The inspector reviewed the root cause determination report, selected procedures and
records, and interviewed personnel.


On March 9, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed a supplemental inspection pursuant to Inspection Procedure 95001, "Inspection for One or Two White Inputs in a Strategic Performance Area," at your McGuire Nuclear Station, Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed at the exit meeting on  
DEC                                            2
March 9, 2010, with Mr. Steven D. Capps and other members of your staff. 
The inspector determined that your staff, in general, performed an adequate evaluation of the
As required by the NRC Reactor Oversight Process Action Matrix, this supplemental inspection was performed because a finding of low to moderate safety significance (White) was identified in the third quarter of 2008 for failure to correct a significant condition adverse to quality related
White finding. Your staffs evaluation determined that the root cause of the issue was changing
to macro-fouling of the nuclear service water (RN) system strainers. This finding was documented previously in NRC Inspection Report 05000369,370/2008009 and resulted in Violation (VIO) 05000369,370/2008009-01, Failure to Take Adequate Corrective Action for Implementation of Safety-Related RN Strainer Backwash. The NRC was informed of your readiness for the inspection on January 11, 2010.
the configuration of the plant without a total understanding of the design and licensing bases for
the RN system strainers during accident conditions, which resulted in the inability to conduct
manual strainer backwashes during certain plant conditions.
Your staff also identified that this lack of understanding of design and licensing bases was not
limited to the RN strainers, but to the RN system in general and has taken corrective actions to
ensure the system design basis documents accurately reflect current licensing bases. The
inspector determined that the corrective actions taken and planned will restore the RN strainer
to full compliance with the licensing basis. In addition, the inspector found that corrective
actions taken or planned appear reasonable and will correct the causes that led to the non-
compliance and prevent recurrence. However, the inspector had several observations
regarding specific aspects of the root cause evaluation and corrective actions that warranted
additional consideration by your staff. These observations were discussed with your staff at the
exit meeting and are included in the report.
Based on the results of this supplemental inspection, no findings of significance were identified.
In accordance with the Code of Federal Regulations 10 CFR 2.390 of the NRCs Rules of
Practice, a copy of this letter, its enclosure, and your response (if any) will be available
electronically for public inspection in the NRC Public Document Room or from the Publicly
Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is
accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public
Electronic Reading Room).
                                                Sincerely,
                                                /RA/
                                                Jonathan H. Bartley, Chief
                                                Reactor Projects Branch 1
                                                Division of Reactor Projects
Docket Nos.: 50-369, 50-370
License Nos.: NPF-9, NPF-17
Enclosure: NRC Integrated Inspection Report 05000369/2010007 and 05000370/2010007
            w/Attachment - Supplemental Information
cc w/encl: (See page 3)


The objectives of this supplemental inspection were to provide assurance that:  (1) the root causes and the contributing causes for the risk-significant issues were understood; (2) the extent of condition and extent of cause of the issues were identified; and (3) corrective actions were or will be sufficient to address and preclude repetition of the root and contributing causes.   
This inspection examined activities conducted under your license as they related to safety and
compliance with the Commission's rules and regulations, and with the conditions of your license.  The inspector reviewed the root cause determination report, selected procedures and records, and interviewed personnel. 
DEC 2  The inspector determined that your staff, in general, performed an adequate evaluation of the White finding.  Your staff's evaluation determined that the root cause of the issue was changing the configuration of the plant without a total understanding of the design and licensing bases for the RN system strainers during accident conditions, which resulted in the inability to conduct
manual strainer backwashes during certain plant conditions. 
Your staff also identified that this lack of understanding of design and licensing bases was not limited to the RN strainers, but to the RN system in general and has taken corrective actions to ensure the system design basis documents accurately reflect current licensing bases.  The
inspector determined that the corrective actions taken and planned will restore the RN strainer to full compliance with the licensing basis.  In addition, the inspector found that corrective actions taken or planned appear reasonable and will correct the causes that led to the non-compliance and prevent recurrence.  However, the inspector had several observations regarding specific aspects of the root cause evaluation and corrective actions that warranted additional consideration by your staff.  These observations were discussed with your staff at the exit meeting and are included in the report.


  Based on the results of this supplemental inspection, no findings of significance were identified.    
  _                                          X SUNSI REVIEW COMPLETE JHB
  In accordance with the Code of Federal Regulations 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available
OFFICE              RII:DRP          RII:DRP        RII:DRP
electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
SIGNATURE          KJK /RA/        JBB /RA/        JHB /RA/
Sincerely, /RA/  
NAME                KKorth          JBrady          JBartley
  Jonathan H. Bartley, Chief  Reactor Projects Branch 1  Division of Reactor Projects
DATE                  03/31/2010      03/31/2010      03/31/2010
Docket Nos.: 50-369, 50-370  
E-MAIL COPY?          YES      NO  YES        NO  YES        NO  YES      NO   YES      NO  YES        NO  YES  NO
License Nos.: NPF-9, NPF-17  
   
Enclosure: NRC Integrated Inspection Report 05000369/2010007 and 05000370/2010007     w/Attachment - Supplemental Information
DEC                                          3
cc w/encl: (See page 3)
cc w/encl:                                    Dhiaa M. Jamil
Steven D. Capps                                Group Executive and Chief Nuclear Officer
Station Manager                                Duke Energy Carolinas, LLC
Duke Energy Carolinas, LLC                    Electronic Mail Distribution
Electronic Mail Distribution
Scotty L. Bradshaw
Training Manager
Duke Energy Carolinas, LLC
Electronic Mail Distribution
Kenneth L. Ashe
Regulatory Compliance Manager
Duke Energy Carolinas, LLC
Electronic Mail Distribution
R. L. Gill, Jr.
Manager
Nuclear Regulatory Issues & Industry Affairs
Duke Energy Carolinas, LLC
Electronic Mail Distribution
Lisa F. Vaughn
Associate General Counsel
Duke Energy Corporation
526 South Church Street-EC07H
Charlotte, NC 28202
Kathryn B. Nolan
Senior Counsel
Duke Energy Corporation
526 South Church Street-EC07H
Charlotte, NC 28202
David A. Repka
Winston Strawn LLP
Electronic Mail Distribution
County Manager of Mecklenburg County
720 East Fourth Street
Charlotte, NC 28202
W. Lee Cox, III
Section Chief
Radiation Protection Section
N.C. Department of Environmental
Commerce & Natural Resources
Electronic Mail Distribution
 
DEC                                        4
Letter to Regis T. Repko from Jonathan H. Bartley dated March 31, 2010
SUBJECT: MCGUIRE NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTION REPORT
              05000369/2010007 AND 05000370/2010007
Distribution w/encl:
C. Evans, RII
L. Slack, RII
OE Mail
RIDSNRRDIRS
PUBLIC
RidsNrrPMMcGuire Resource
 
          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION II
Docket Nos.:       50-369, 50-370
License Nos.:       NPF-9, NPF-17
Report Nos.:       05000369/2010007, 05000370/2010007
Licensee:          Duke Energy Carolinas, LLC
Facility:          McGuire Nuclear Station, Units 1 and 2
Location:          Huntersville, NC 28078
Dates:              March 1, 2010, through March 9, 2010
Inspectors:        K. Korth, Resident Inspector Browns Ferry Nuclear Plant
Approved by:       Jonathan H. Bartley, Chief
                    Reactor Projects Branch 1
                    Division of Reactor Projects
                                                                  Enclosure


_                              X  SUNSI REVIEW COMPLETE  JHB
                                      SUMMARY OF FINDINGS
OFFICE RII:DRP RII:DRP RII:DRP    SIGNATURE KJK /RA/ JBB /RA/ JHB /RA/    NAME KKorth JBrady JBartley    DATE 03/31/2010 03/31/2010 03/31/2010    E-MAIL COPY?    YES NO  YES NO  YES NO  YES NO  YES NO  YES NO  YES NO 
IR 05000369/2010007, 05000370/2010007; 03/01/2010 - 03/09/2010; McGuire Nuclear Station,
DEC      3
Units 1 and 2; Supplemental Inspection IP 95001 in response to a White inspection finding for
cc w/encl: Steven D. Capps Station Manager Duke Energy Carolinas, LLC
failure to correct a significant condition adverse to quality related to macro-fouling of the nuclear
Electronic Mail Distribution
service water (RN) system strainers.
Scotty L. Bradshaw Training Manager Duke Energy Carolinas, LLC Electronic Mail Distribution
This inspection was conducted by a resident inspector. No findings of significance were
identified. The NRCs program for overseeing the safe operation of commercial nuclear power
Kenneth L. Ashe Regulatory Compliance Manager Duke Energy Carolinas, LLC Electronic Mail Distribution
reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated
R. L. Gill, Jr. Manager
December 2006.
Nuclear Regulatory Issues & Industry Affairs Duke Energy Carolinas, LLC Electronic Mail Distribution
Cornerstone: Mitigating Systems
Lisa F. Vaughn
This supplemental inspection was performed in accordance with Inspection Procedure (IP)
Associate General Counsel Duke Energy Corporation 526 South Church Street-EC07H Charlotte, NC  28202
95001, Inspection for One or Two White Inputs in a Strategic Performance Area, to assess the
Kathryn B. Nolan Senior Counsel
licensee's evaluation associated with a White inspection finding involving with the inability to
Duke Energy Corporation 526 South Church Street-EC07H Charlotte, NC  28202
perform manual backwash on the Nuclear Service Water (RN) strainers identified in August of
David A. Repka
2007. The NRC staff previously characterized this issue as having low to moderate safety
Winston Strawn LLP Electronic Mail Distribution
significance (White) as documented in NRC IR 05000369,370/2008009.
County Manager of Mecklenburg County 720 East Fourth Street Charlotte, NC  28202
During this supplemental inspection, the inspector determined that, in general, the licensee
performed an adequate evaluation of the White finding. The licensees evaluation determined
W. Lee Cox, III Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources
that the root cause of the issue was changing the configuration of the plant without a total
Electronic Mail Distribution
understanding of the design. The RN strainer backwash system had been modified to replace
Dhiaa M. Jamil Group Executive and Chief Nuclear Officer Duke Energy Carolinas, LLC Electronic Mail Distribution
RN strainer backwash outlet manual valves with air-operated valves that could not be manually
DEC      4
over-ridden. This root cause, along with four other contributing causes, led to operation of the
Letter to Regis T. Repko from Jonathan H. Bartley dated March 31, 2010
system from 2000/2001 to 2007 without having the capability to manually backwash the
SUBJECT: MCGUIRE NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTION REPORT 05000369/2010007 AND 05000370/2010007
strainers following a loss of instrument air (VI). The licensee also identified that this lack of
Distribution w/encl
understanding of design and licensing bases was not limited to the RN strainers, but to the RN
: C. Evans, RII L. Slack, RII OE Mail RIDSNRRDIRS PUBLIC
system in general and has taken corrective actions to ensure the system design basis
RidsNrrPMMcGuire Resource 
documents accurately reflect current licensing bases. The inspector determined that the
Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II
corrective actions taken and planned will restore the RN strainer to full compliance with the
licensing basis. In addition, the inspector found that corrective actions taken or planned appear
 
reasonable and will correct the causes that led to the non-compliance and prevent recurrence.
Docket Nos.:  50-369, 50-370
However, the inspector had the following observations regarding specific aspects of the root
  License Nos.:  NPF-9, NPF-17
cause evaluation (RCE) and corrective actions that warranted additional consideration by the
  Report Nos.:  05000369/2010007, 05000370/2010007
licensee. The RCE did not fully document the organizational and programmatic weaknesses
  Licensee:  Duke Energy Carolinas, LLC
that led to the condition, or the reasons that multiple opportunities were missed for earlier
  Facility:  McGuire Nuclear Station, Units 1 and 2
discovery (section 02.02.b). The licensee did not revise the RCE when new information was
  Location:  Huntersville, NC 28078
discovered or when additional reviews of the RCE were conducted (section 02.02.b).
  Dates:  March 1, 2010, through March 9, 2010
Weakness of the original extent of condition and extent of cause evaluations resulted in delays
 
in conducting a thorough review, some aspects of which were still in progress at the time of the
Inspectors:  K. Korth, Resident Inspector Browns Ferry Nuclear Plant
inspection (section 02.02.d). The RCE did not specifically consider the safety culture
  Approved by:  Jonathan H. Bartley, Chief Reactor Projects Branch 1
components of Inspection Manual Chapter 0305 (section 02.02.e). The root cause and
Division of Reactor Projects
contributing causes were not well linked to the associated corrective actions (section 02.03.a).
   
The quantitative and qualitative measures of success for determining the effectiveness of the
 
                                                                                            Enclosure
Enclosure SUMMARY OF FINDINGS
 
IR 05000369/2010007, 05000370/2010007; 03/01/2010 - 03/09/2010; McGuire Nuclear Station, Units 1 and 2; Supplemental Inspection IP 95001 in response to a White inspection finding for failure to correct a significant condition adverse to quality related to macro-fouling of the nuclear
                                              3
service water (RN) system strainers.  
corrective actions to preclude repetition were not well established (section 02.03.d). Based on
This inspection was conducted by a resident inspector.  No findings of significance were identified.  The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated
the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate the quality of root
December 2006.  
cause evaluations.
Cornerstone:  Mitigating Systems
Given the licensees acceptable performance in addressing the non-compliance of the RN
  This supplemental inspection was performed in accordance with Inspection Procedure (IP) 95001, "Inspection for One or Two White Inputs in a Strategic Performance Area," to assess the licensee's evaluation associated with a White inspection finding involving with the inability to
strainer with its licensing bases, the White finding associated with this issue is being closed and
perform manual backwash on the Nuclear Service Water (RN) strainers identified in August of 2007. The NRC staff previously characterized this issue as having low to moderate safety significance (White) as documented in NRC IR 05000369,370/2008009.  
will only be considered in assessing plant performance until the end of this quarter in
During this supplemental inspection, the inspector determined that, in general, the licensee performed an adequate evaluation of the White finding. The licensee's evaluation determined that the root cause of the issue was changing the configuration of the plant without a total understanding of the design. The RN strainer backwash system had been modified to replace RN strainer backwash outlet manual valves with air-operated valves that could not be manually over-ridden. This root cause, along with four other contributing causes, led to operation of the system from 2000/2001 to 2007 without having the capability to manually backwash the strainers following a loss of instrument air (VI). The licensee also identified that this lack of understanding of design and licensing bases was not limited to the RN strainers, but to the RN system in general and has taken corrective actions to ensure the system design basis documents accurately reflect current licensing bases.  The inspector determined that the  
accordance with the guidance in IMC 0305, Operating Reactor Assessment Program. Since
corrective actions taken and planned will restore the RN strainer to full compliance with the licensing basis. In addition, the inspector found that corrective actions taken or planned appear reasonable and will correct the causes that led to the non-compliance and prevent recurrence. 
many of the corrective actions have not been completed, the implementation and effectiveness
However, the inspector had the following observations regarding specific aspects of the root
of the licensees corrective actions will be reviewed during future inspections.
cause evaluation (RCE) and corrective actions that warranted additional consideration by the licensee.  The RCE did not fully document the organizational and programmatic weaknesses that led to the condition, or the reasons that multiple opportunities were missed for earlier discovery (section 02.02.b).  The licensee did not revise the RCE when new information was discovered or when additional reviews of the RCE were conducted (section 02.02.b).  Weakness of the original extent of condition and extent of cause evaluations resulted in delays in conducting a thorough review, some aspects of which were still in progress at the time of the
                                                                                          Enclosure
inspection (section 02.02.d).  The RCE did not specifically consider the safety culture components of Inspection Manual Chapter 0305 (section 02.02.e). The root cause and contributing causes were not well linked to the associated corrective actions (section 02.03.a). The quantitative and qualitative measures of success for determining the effectiveness of the
 
3  Enclosure corrective actions to preclude repetition were not well established (section 02.03.d).  Based on the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate the quality of root cause evaluations.
                                      REPORT DETAILS
4.   OTHER ACTIVITIES
Given the licensee's acceptable performance in addressing the non-compliance of the RN strainer with its licensing bases, the White finding associated with this issue is being closed and will only be considered in assessing plant performance until the end of this quarter in accordance with the guidance in IMC 0305, "Operating Reactor Assessment Program."  Since many of the corrective actions have not been completed, the implementation and effectiveness
4OA4 Supplemental Inspection
of the licensee's corrective actions will be reviewed during future inspections. 
.01 Inspection Scope
Enclosure REPORT DETAILS
    The NRC staff performed this supplemental inspection in accordance with IP 95001 to
4. OTHER ACTIVITIES
    assess the licensees evaluation of a White finding which affected the Mitigating
4OA4 Supplemental Inspection
    Systems cornerstone in the Reactor Safety strategic performance area. The inspection
  .01 Inspection Scope
    objectives were to:
  The NRC staff performed this supplemental inspection in accordance with IP 95001 to assess the licensee's evaluation of a White finding which affected the Mitigating
    * provide assurance that the root and contributing causes of risk-significant issues were
Systems cornerstone in the Reactor Safety strategic performance area.  The inspection objectives were to:
        understood;
  * provide assurance that the root and contributing causes of risk-significant issues were understood;
    * provide assurance that the extent of condition and extent of cause of risk-significant
* provide assurance that the extent of condition and extent of cause of risk-significant issues were identified; and
        issues were identified; and
* provide assurance that the licensee's corrective actions for risk-significant issues were or will be sufficient to address the root and contributing causes and to preclude repetition.  
    * provide assurance that the licensees corrective actions for risk-significant issues
The licensee entered the Regulatory Response Column of the NRC's Action Matrix in the third quarter of 2008 as a result of one inspection finding of low to moderate safety significance (White).  The finding was associated with the failure to take adequate corrective actions related to implementation of a safety-related RN strainer backwash system.  On August 6, 2007, the "A" Train of the RN system was declared inoperable
        were or will be sufficient to address the root and contributing causes and to preclude
when the licensee discovered that manually backwashing RN strainers was not always possible during design basis accidents.  In 2000 on Unit 2 and in 2001 on Unit 1, a modification had been implemented to replace strainer backwash outlet manual valves with air-operated valves that could not be manually over-ridden. The Station Instrument Air (VI) system was non-safety-related and could not be relied upon to manually
        repetition.
backwash the RN strainers during or following design basis accidents.  The finding was characterized as having low to moderate safety significance (White) based on the results of a Phase 3 risk analysis performed by a region-based senior reactor analyst (SRA), as discussed in NRC Inspection Report (IR) 05000369,370/2008009.  
    The licensee entered the Regulatory Response Column of the NRCs Action Matrix in
    the third quarter of 2008 as a result of one inspection finding of low to moderate safety
As a result of identifying this non-conformance, the licensee made some plant modifications, including a modification to allow operation of the RN strainer backwash outlet valves without reliance on VI, and took other measures to compensate for this condition until full compliance with the design and licensing bases can be restored through additional planned modifications.  The licensee conducted a root cause
    significance (White). The finding was associated with the failure to take adequate
evaluation (RCE), as documented in Problem Investigation Process report (PIP) M-07-4313, to identify weaknesses that existed in various organizations which allowed for a risk-significant finding and to determine the organizational attributes that resulted in the White finding.  Subsequently, a number of events and additional reviews impacted the corrective actions associated with the original RCE. During the February 13, 2008, 
    corrective actions related to implementation of a safety-related RN strainer backwash
5  Enclosure meeting of the Nuclear Safety Review Board (NSRB), the board challenged the depth of the original extent of condition and extent of cause evaluations (PIP M-08-1574). Testing of the backwash system on May 27, 2008, to evaluate a potential piping modification revealed the system had inadequate pressure to provide RN strainer
    system. On August 6, 2007, the "A" Train of the RN system was declared inoperable
backwash flow to the normal discharge path to the Condenser Circulating Water (RC) system and that at high RN flow rates, a negative pressure was created in the strainers making backwash discharge flow to the ground water (WZ) sump unavailable (PIP M-08-3371). On April 27, 2009, during testing of the RN system at high flow rates, the strainers became clogged with corrosion products from the suction piping which was a
    when the licensee discovered that manually backwashing RN strainers was not always
new macro-fouling source not previously identified (PIP M-09-2216).  All of these events and reviews resulted in changes to or additions of corrective actions to the original RCE. 
    possible during design basis accidents. In 2000 on Unit 2 and in 2001 on Unit 1, a
The licensee staff informed the NRC staff on January 11, 2010, that they were ready for the supplemental inspection.  From January 25, 2010, to February 4, 2010, in preparation for this inspection, the licensee conducted an in-depth readiness review of the original RCE report using the inspection attributes of IP 95001.  As a result of that
    modification had been implemented to replace strainer backwash outlet manual valves
self-critical readiness assessment, the licensee issued several additional PIPs and added additional corrective actions to the original PIP M-07-4313. 
    with air-operated valves that could not be manually over-ridden. The Station Instrument
The inspector reviewed the RCE associated with PIP M-07-4313, along with several other evaluations that were conducted in support of or that impacted the corrective
    Air (VI) system was non-safety-related and could not be relied upon to manually
actions for the root cause determination.  The inspector reviewed the licensee's extent of condition and extent of cause evaluations to ensure they were sufficient in breadth.  The inspector reviewed the corrective actions that were taken or planned to address the identified causes.  The inspector also held discussions with licensee personnel to ensure that the root and contributing causes, as well as the contribution of safety culture
    backwash the RN strainers during or following design basis accidents. The finding was
components, were understood and that corrective actions taken or planned were appropriate to address the causes and preclude repetition.
    characterized as having low to moderate safety significance (White) based on the results
.02 Evaluation of the Inspection Requirements
    of a Phase 3 risk analysis performed by a region-based senior reactor analyst (SRA), as
 
    discussed in NRC Inspection Report (IR) 05000369,370/2008009.
    As a result of identifying this non-conformance, the licensee made some plant
    modifications, including a modification to allow operation of the RN strainer backwash
    outlet valves without reliance on VI, and took other measures to compensate for this
    condition until full compliance with the design and licensing bases can be restored
    through additional planned modifications. The licensee conducted a root cause
    evaluation (RCE), as documented in Problem Investigation Process report (PIP) M-07-
    4313, to identify weaknesses that existed in various organizations which allowed for a
    risk-significant finding and to determine the organizational attributes that resulted in the
    White finding. Subsequently, a number of events and additional reviews impacted the
    corrective actions associated with the original RCE. During the February 13, 2008,
                                                                                        Enclosure
 
                                              5
      meeting of the Nuclear Safety Review Board (NSRB), the board challenged the depth of
      the original extent of condition and extent of cause evaluations (PIP M-08-1574).
      Testing of the backwash system on May 27, 2008, to evaluate a potential piping
      modification revealed the system had inadequate pressure to provide RN strainer
      backwash flow to the normal discharge path to the Condenser Circulating Water (RC)
      system and that at high RN flow rates, a negative pressure was created in the strainers
      making backwash discharge flow to the ground water (WZ) sump unavailable (PIP M-08-
      3371). On April 27, 2009, during testing of the RN system at high flow rates, the
      strainers became clogged with corrosion products from the suction piping which was a
      new macro-fouling source not previously identified (PIP M-09-2216). All of these events
      and reviews resulted in changes to or additions of corrective actions to the original RCE.
      The licensee staff informed the NRC staff on January 11, 2010, that they were ready for
      the supplemental inspection. From January 25, 2010, to February 4, 2010, in
      preparation for this inspection, the licensee conducted an in-depth readiness review of
      the original RCE report using the inspection attributes of IP 95001. As a result of that
      self-critical readiness assessment, the licensee issued several additional PIPs and
      added additional corrective actions to the original PIP M-07-4313.
      The inspector reviewed the RCE associated with PIP M-07-4313, along with several
      other evaluations that were conducted in support of or that impacted the corrective
      actions for the root cause determination. The inspector reviewed the licensees extent of
      condition and extent of cause evaluations to ensure they were sufficient in breadth. The
      inspector reviewed the corrective actions that were taken or planned to address the
      identified causes. The inspector also held discussions with licensee personnel to ensure
      that the root and contributing causes, as well as the contribution of safety culture
      components, were understood and that corrective actions taken or planned were
      appropriate to address the causes and preclude repetition.
.02  Evaluation of the Inspection Requirements
02.01 Problem Identification
02.01 Problem Identification
    a. IP 95001 requires that the inspection staff determine that the licensee's evaluation of the issue documents who identified the issue (i.e., licensee-identified, self-revealing, or NRC-identified) and the conditions under which the issue was identified.  
  a. IP 95001 requires that the inspection staff determine that the licensees evaluation of the
The inspector determined that the event evaluations were sufficiently detailed to identify who and under what conditions the issue was identified. The issue was identified on August 6, 2007, by the licensee during the investigation of an abnormally high number of RN strainer automatic backwashes (PIP M-07-4177).   
      issue documents who identified the issue (i.e., licensee-identified, self-revealing, or
    b. IP 95001 requires that the inspection staff determine that the licensee's evaluation of the issue documents how long the issue existed and prior opportunities for identification.  
      NRC-identified) and the conditions under which the issue was identified.
The licensee's root cause documented that the condition had existed since the implementation of a modification that replaced the RN strainer backwash outlet manual valves with air-operated valves on Unit 2 in 2000 (MM-8444) and on Unit 1 in 2001 (MM-  
      The inspector determined that the event evaluations were sufficiently detailed to identify
6 Enclosure 11224). However, subsequent testing in May 2008 revealed that there was no strainer backwash discharge flow when aligned to the RC system and that strainer discharge flow to the WZ sump was not possible at high RN flow rates (PIP M-08-3371). Based on this information, the operability determination was revised, as were the interim and long  
      who and under what conditions the issue was identified. The issue was identified on
term actions to correct the condition. This additional time where backwash was unavailable did not impact the NRC's significance determination of the condition since no credit for strainer backwash was given and the duration used in the evaluation was over a one year period.  
      August 6, 2007, by the licensee during the investigation of an abnormally high number of
      RN strainer automatic backwashes (PIP M-07-4177).
The licensee's root cause documented multiple missed opportunities to identify the issue. Opportunities to recognize that manual backwash relied on non-safety related VI, which could be unavailable following an accident, included the evaluation of the need to upgrade the system to meet safety related requirements (PIP M-02-2427), design and implementation of the modification that upgraded the system to meet safety related requirements (MGMM-14403), evaluation of a variance to the modification to add the ability to manually operate the strainer backwash outlet valves using an air supply  
   b. IP 95001 requires that the inspection staff determine that the licensees evaluation of the
bypass valve, and revisions to the procedures to manually backwash the strainers.  
      issue documents how long the issue existed and prior opportunities for identification.
The inspector determined that the licensee's evaluation was adequate with respect to identifying how long the issue existed and prior opportunities for identification.  
      The licensees root cause documented that the condition had existed since the
    c. IP 95001 requires that the inspection staff determine that the licensee's evaluation of the issue documents the plant-specific risk consequence, as applicable, and compliance concerns associated with the issue.  
      implementation of a modification that replaced the RN strainer backwash outlet manual
The NRC determined this issue was a White finding, as documented in NRC IR  
      valves with air-operated valves on Unit 2 in 2000 (MM-8444) and on Unit 1 in 2001 (MM-
05000369,370/2008009. The root cause evaluation did not qualitatively assess the increased risk associated with this condition, but the LER submitted by the licensee (LER 05000369/2007-004) stated that based on a preliminary PRA evaluation, the conditional core damage probability (CCDP) associated with this condition was greater than 1E-6. At the Regulatory Conference held at the Region II offices on September 18,  
                                                                                        Enclosure
2008, the licensee presented the results of their revised evaluation of CCDP as approximately 4.7 E-7. However, the licensee did not contest the violation or its categorization as having low to moderate safety significance.  
 
The root cause evaluation appropriately documented the condition as a non-compliance  
                                          6
with their licensing bases and took appropriate compensatory actions, including plant and procedural modifications to allow manual backwash without instrument air. Full compliance will be restored when all corrective actions associated with this issue are completed.  
  11224). However, subsequent testing in May 2008 revealed that there was no strainer
The inspector concluded that the licensee appropriately documented the risk consequences and compliance concerns associated with the issue.  
  backwash discharge flow when aligned to the RC system and that strainer discharge
    d. Findings
  flow to the WZ sump was not possible at high RN flow rates (PIP M-08-3371). Based on
  No findings of significance were identified.  
  this information, the operability determination was revised, as were the interim and long
 
  term actions to correct the condition. This additional time where backwash was
7 Enclosure 02.02 Root Cause, Extent-of-Condition, and Extent-of-Cause Evaluation
  unavailable did not impact the NRCs significance determination of the condition since
    a. IP 95001 requires that the inspection staff determine that the licensee evaluated the issue using a systematic methodology to identify the root and contributing causes.  
  no credit for strainer backwash was given and the duration used in the evaluation was
The licensee used the following systematic methods to complete PIP M-07-4313 problem evaluation:  
  over a one year period.
* data gathering through interviews and document review;  
  The licensees root cause documented multiple missed opportunities to identify the
* timeline construction;  
  issue. Opportunities to recognize that manual backwash relied on non-safety related VI,
* events and causal factor charting; and  
  which could be unavailable following an accident, included the evaluation of the need to
* barrier analysis.  
  upgrade the system to meet safety related requirements (PIP M-02-2427), design and
The inspector determined that the licensee evaluated the issue using a systematic methodology to identify root and contributing causes.  
  implementation of the modification that upgraded the system to meet safety related
    b. IP 95001 requires that the inspection staff determine that the licensee's RCE was conducted to a level of detail commensurate with the significance of the issue.  
  requirements (MGMM-14403), evaluation of a variance to the modification to add the
The licensee's RCE included an extensive timeline of events, as well as an event and causal factors (E&CF) chart as discussed in the previous section. Using a multidisciplinary team, the licensee identified a single root cause as changing the plant  
  ability to manually operate the strainer backwash outlet valves using an air supply
configuration (i.e., manual valves on the RN strainer backwash outlet were replaced with air-operated valves) without a total understanding of the design and licensing bases. In addition, the RCE identified four contributing causes (CC) stemming from inappropriate actions identified on the E&CF chart.  
  bypass valve, and revisions to the procedures to manually backwash the strainers.
CC1: Design study conducted in 1990 to evaluate the RN strainer design bases (MGDS-224) missed the UFSAR requirement for manual backwash following a  
  The inspector determined that the licensees evaluation was adequate with respect to
LOCA. CC2: Modifications made in 1993-1994 that downgraded the strainer backwash function to non-safety related (MGMM-3794) were completed without a 10 CFR 50.59 evaluation as an editorial minor modification.  
  identifying how long the issue existed and prior opportunities for identification.
CC3: An assessment completed in 1993 (SITA-93-01) on the operational readiness and functionality of the RN system found issues with the system design including the need for safety related instrumentation for strainer backwash initiation, but the PIP that was generated had no evaluation and no corrective actions.  
c. IP 95001 requires that the inspection staff determine that the licensees evaluation of the
CC4: The corrective actions from PIP M-02-2427 generated in 2002 for engineering to evaluate the safety classification of the RN strainers based on past strainer fouling events, did not correct the condition. The resulting modification that upgraded the strainer to safety related requirements (MMGM-14403) did not consider the ability  
  issue documents the plant-specific risk consequence, as applicable, and compliance
to manually backwash the strainers following a loss of VI.  
  concerns associated with the issue.
 
  The NRC determined this issue was a White finding, as documented in NRC IR
8 Enclosure The RCE did not fully document the organizational and programmatic weaknesses that led to the condition, nor the reasons that multiple opportunities were missed for earlier discovery. For example, the reason(s) why there was not a clear understanding of the design bases of the system or why the design change/50.59 process failed to identify the  
  05000369,370/2008009. The root cause evaluation did not qualitatively assess the
USFAR requirement for manual backwash were not fully explored. This was identified by the licensee during their 95001 readiness review (M-SAG-SA-10-11) and PIP M-10-1208 was initiated to evaluate the reasons why the design bases were not fully understood. It concluded that the licensee did not know the UFSAR was the Current Licensing Basis (CLB) source at the time of the modification and that the Design and  
  increased risk associated with this condition, but the LER submitted by the licensee
Licensing ownership had moved from the General Office to the site in the 1992 to 1996 timeframe.  
  (LER 05000369/2007-004) stated that based on a preliminary PRA evaluation, the
Contributing to the apparent lack of detailed documentation of the causes of the event was that the licensee did not revise the RCE when new information was discovered (M-08-3371 and M-09-2261) or when additional review of the RCE was conducted.
  conditional core damage probability (CCDP) associated with this condition was greater
  The inspector identified that Nuclear System Directive (NSD) 212, Cause Analysis, indicated that in the event further information becomes available that potentially affects the results of a root cause evaluation, the root cause should be reevaluated to determine if a revision was required. The operability determination was revised and numerous corrective actions were added or revised, however the evaluation portion of the PIP was not changed. This resulted in cases where the critical thinking on why a corrective  
  than 1E-6. At the Regulatory Conference held at the Region II offices on September 18,
action was added was not documented and made the linkage between the root and contributing causes and the associated CAs to address the causes difficult. Additionally, the original RCE did not identify that the failure to conduct testing to ensure that the backwash system functioned as designed was a contributor to this event. This was identified in the corrective actions for PIP M-08-3371, but the original RCE was never  
  2008, the licensee presented the results of their revised evaluation of CCDP as
updated.
  approximately 4.7 E-7. However, the licensee did not contest the violation or its
However, the inspector determined that the organizational and programmatic weaknesses that caused this event, even if not specifically documented in the RCE, were ultimately addressed in the corrective actions for this PIP and in other related PIPs.
  categorization as having low to moderate safety significance.
For example, the corrective actions addressed weaknesses in the design bases documentation (e.g., DBD and UFSAR), in the design change process, in the 50.59 process and in the knowledge and skills of engineering personnel and 10 CFR 50.59 qualified evaluators and screeners. Based on the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate the quality of root cause evaluations, including  
  The root cause evaluation appropriately documented the condition as a non-compliance
determining the reasons PIP M-07-4313 did not apply the "why" staircase sufficiently to determine what process weaknesses needed to be corrected and the reasons the RCE was not revised when additional information was uncovered.  
  with their licensing bases and took appropriate compensatory actions, including plant
    c. IP 95001 requires that the inspection staff determine that the licensee's RCE include a consideration of prior occurrences of the problem and knowledge of prior operating experience.  
  and procedural modifications to allow manual backwash without instrument air. Full
The licensee's RCE included a review of both internal and external operating experience (OE). A search of the McGuire PIP database was conducted for previous events assigned cause codes of F1b (Unplanned entry into TS LCO) and J1e (Risks and Consequences associated with change not adequately reviewed). No previous events
  compliance will be restored when all corrective actions associated with this issue are
Enclosure were identified. However, these specific cause codes were not assigned to the root or contributing causes for this evaluation. This was identified by the licensee in their IP 95001 readiness review (M-SAG-SA-10-11) and a subsequent search using the appropriate codes did not identify any prior occurrences. Based on the licensee's
  completed.
evaluation and conclusions, the inspector determined that the licensee's RCE included a consideration of prior occurrences of the problem and knowledge of prior OE.  
  The inspector concluded that the licensee appropriately documented the risk
    d. IP 95001 requires that the inspection staff determine that the licensee's RCE addresses the extent of condition and the extent of cause of the issue.  
  consequences and compliance concerns associated with the issue.
To address the extent of condition issue, the licensee's RCE contained a review of air-operated valves (AOVs) that receive safety signals that may need to be repositioned from their safety position following an accident. Based on recommendations from the McGuire NSRB meeting on February 13, 2008, additional corrective actions were added to expand the scope of the AOVs that were reviewed and to include instrumentation that is required post-accident that relied on instrument air (VI). No additional valves were  
d. Findings
found that required VI post-accident and some procedure changes were made to identify alternate indications that could be used for instrumentation that would be unavailable following a loss of VI. During the IP 95001 readiness review a deficiency was identified with the extent of condition. The team found that the extent of condition corrective actions (CAs) should address motive forces other than air (e.g., power-operated  
  No findings of significance were identified.
components) and other systems containing safety related/non-safety related interfaces should be sampled and evaluated to ensure no similar issues with other safety related systems exist (PIP M-10-1210). At the time of the inspection, the extent of condition review of safety/non-safety system interactions was still in progress.  
                                                                                      Enclosure
 
To address the extent of cause the RCE reviewed other areas where engineering may not have a clear understanding of design bases prior to changing plant configuration. Specifically, a corrective action was created to review the design basis document (DBD) for the entire RN system and the Design Basis Accident DBD to ensure they adequately reflect the current licensing basis. In addition, engineering personnel and 10 CFR 50.59  
                                            7
qualified personnel were trained on this event and on the use of licensing basis documents during the design change process. During the IP 95001 readiness review a deficiency was identified with the extent of cause. The team found that the extent of cause CAs should be expanded to include the 10 CFR 50.59 process (program changes, effectiveness reviews and examples) and the Engineering  
02.02 Root Cause, Extent-of-Condition, and Extent-of-Cause Evaluation
Change/Engineering Change Approval process (program changes, effectiveness reviews and examples) to ensure current processes would prevent similar events (PIP M-10-1211). This PIP determined that recent 10 CFR 50.59 process changes provide confidence in the current processes such that a similar failure of the program, as documented under PIP M-07-4313, would not occur. Likewise, the current modification process related toward editorial changes process provides sufficient barriers to prevent design and implementation of a non-editorial modification under the editorial process. In  
  a. IP 95001 requires that the inspection staff determine that the licensee evaluated the
addition, PIP M-10-1240 was initiated to perform detailed design bases impact reviews for historical modifications, which were deemed to have potentially similar attributes to the historical modification which improperly downgraded RN strainer safety classification. At the time of the inspection, this review was still in progress.  
      issue using a systematic methodology to identify the root and contributing causes.
 
      The licensee used the following systematic methods to complete PIP M-07-4313
10 Enclosure As stated earlier, the original RCE did not identify that the failure to conduct testing to ensure that the backwash system functioned as designed was a contributor to this event. However, this was identified following the discovery that backwash to the RC system was not possible and that backwash to the WZ sump could not be performed at high RN  
      problem evaluation:
flow rates (PIP M-08-3371). Subsequently an extent of cause was conducted that sampled several other safety systems to ensure that all safety functions have been adequately functionally tested and/or monitored (PIP M-08-4602).
      *   data gathering through interviews and document review;
The inspector concluded that the licensee has ultimately addressed the extent of  
      *   timeline construction;
condition and the extent of cause of the issue. However, weakness of the original extent of condition and extent of cause evaluations resulted in delays in conducting a thorough review, some aspects of which were still in progress at the time of the inspection.  
      *   events and causal factor charting; and
    e. IP 95001 requires that the inspection staff determine that the licensee's root cause evaluation, extent of condition, and extent of cause appropriately considered the safety culture components as described in IMC 0305.  
      *   barrier analysis.
As part of the RCE, the licensee did not specifically consider the safety culture components of IMC 0305, but did reference some safety culture components in their cause determination. Specifically, CC3 was assigned a cause code of "previous industry or in-house operating experience was not effectively used to prevent problems" (safety  
      The inspector determined that the licensee evaluated the issue using a systematic
culture component of operating experience) and CC4 was assigned a cause code of "corrective actions from previously identified problems or previous event causes were not adequate to prevent recurrence" (safety culture component of problem identification and resolution). The failure to consider safety culture components in the RCE was recognized by the IP 95001 readiness review team (M-SAG-SA-10-11). A corrective  
      methodology to identify root and contributing causes.
action was created in PIP M-07-4313 to conduct an assessment of the safety culture components and a corrective action to PIP M-10-1205 was created for the Safety Assurance/Performance Improvement (SA/PI) Manager to review the current processes and McGuire site understanding of requirements for considering safety culture components.
  b. IP 95001 requires that the inspection staff determine that the licensees RCE was
  The safety culture component evaluation that was conducted as a result of the readiness review team recommendation concluded that there were no aspects of the RCE that would indicate that the organizations or individuals involved exhibited behavior indicative of a weakness in safety culture, even though the cause codes assigned to two of the contributing causes directly relate to safety culture components. This further demonstrated the lack of specific guidance on considering safety culture components  
      conducted to a level of detail commensurate with the significance of the issue.
during root cause evaluations.  
      The licensees RCE included an extensive timeline of events, as well as an event and
Based on the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate the quality of root cause evaluations, including addressing the lack of guidance on considering safety culture components during root cause evaluations.  
      causal factors (E&CF) chart as discussed in the previous section. Using a
    f. Findings
      multidisciplinary team, the licensee identified a single root cause as changing the plant
  No findings of significance were identified.  
      configuration (i.e., manual valves on the RN strainer backwash outlet were replaced with
11 Enclosure 02.03 Corrective Actions
      air-operated valves) without a total understanding of the design and licensing bases. In
    a. IP 95001 requires that the inspection staff determine that: (1) the licensee specified appropriate corrective actions for each root and/or contributing cause; or (2) an  
      addition, the RCE identified four contributing causes (CC) stemming from inappropriate
evaluation that states no actions are necessary is adequate.  
      actions identified on the E&CF chart.
The root cause and contributing causes 1 and 2 were linked to corrective actions. However contributing causes 3 and 4 were not linked to specific corrective actions. This was identified in the IP 95001 readiness review and PIP M-10-1214 was initiated to  
      CC1: Design study conducted in 1990 to evaluate the RN strainer design bases
correct this oversight.  
            (MGDS-224) missed the UFSAR requirement for manual backwash following a
The inspector reviewed the corrective actions taken for PIP M-07-4313 and determined that, although not well linked, adequate corrective actions have been or will be taken to address the causes of this condition.  
            LOCA.
    b. IP 95001 requires that the inspection staff determine that the licensee prioritized corrective actions with consideration of risk significance and regulatory compliance.  
      CC2: Modifications made in 1993-1994 that downgraded the strainer backwash function
The licensee took immediate corrective actions to compensate for the inability to manually backwash the RN strainers following a loss of instrument air by modifying the strainer backwash outlet valves to provide a manual means to open the valves without  
            to non-safety related (MGMM-3794) were completed without a 10 CFR 50.59
relying on VI. These compensatory actions and associated operability determination were later modified following the discovery that backwash flow path to the RC system was unavailable and that a negative pressure was created in the strainer during high RN flow rates (PIP M-08-3717). This led to procedure changes that provided guidance on aligning strainer backwash flow, if needed, to the WZ sump only and to throttle RN flow  
            evaluation as an editorial minor modification.
to the Component Cooling Water (KC) heat exchangers if strainer pressure was inadequate for sump discharge. These compensatory actions and the associated operability determination were modified again following the discovery of additional macro-fouling sources (PIP M-09-2216). On November 6, 2009, the NRC requested the licensee provide an explanation addressing what compensatory or other measures were  
      CC3: An assessment completed in 1993 (SITA-93-01) on the operational readiness and
in place to assure the operability of the RN system in case strainer macro-fouling does occur until full compliance is restored. In their response dated December 7, 2009, the licensee stated that a dedicated operator was stationed to perform time-critical actions to initiate backwash supply flow to the strainers on a loss of instrument air and listed several modifications and procedural changes that have been made. The response only  
            functionality of the RN system found issues with the system design including the
addressed macro-fouling from soft debris that could be crushed in the strainer and passed through the system and did not reference the procedure to align backwash outlet flow to the WZ sump or the potential need to throttle RN flow to the KC heat exchangers to achieve adequate strainer pressure for backwash operation. The licensee committed to supplement their December 7, 2009 response by April 12, 2010, to more completely describe their interim compensatory measures, including those that would mitigate all design basis type macro-fouling mechanisms that could impact the RN system during  
            need for safety related instrumentation for strainer backwash initiation, but the PIP
design basis events.         These events also impacted the corrective actions needed to restore the system to full compliance. The licensee determined that the preferred approach to restore compliance would be to implement a series of modifications including installation of safety related
            that was generated had no evaluation and no corrective actions.
12 Enclosure strainer backwash discharge pumps to provide the motive force to direct backwash flow to the RN return header. In a letter dated October 1, 2009, the licensee changed their original commitment of submitting a license amendment to resolve the NOV, to completing these modifications by December 2012. On November 6, 2009, the NRC  
      CC4: The corrective actions from PIP M-02-2427 generated in 2002 for engineering to
requested the licensee provide a discussion on why the proposed completion date represented the first available opportunity to restore compliance. In their response dated December 7, 2009, the licensee provided the justification for the proposed durations for modification implementation. The inspector reviewed the reasons provided for the projected completion dates for the modifications and found them to be reasonable given  
            evaluate the safety classification of the RN strainers based on past strainer fouling
the magnitude of the modifications.
            events, did not correct the condition. The resulting modification that upgraded the
  The corrective action to prevent recurrence for the root cause was to revise the DBD for the RN system. This action was appropriately prioritized and has been completed. Based upon the appropriate prioritization of the DBD revision and the review of the implementation schedule for the modifications needed to restore full compliance of the system, the inspector determined that the corrective actions were prioritized with  
            strainer to safety related requirements (MMGM-14403) did not consider the ability
consideration of the risk significance and regulatory compliance.  
            to manually backwash the strainers following a loss of VI.
    c. IP 95001 requires that the inspection staff determine that the licensee established a schedule for implementing and completing the corrective actions.  
                                                                                        Enclosure
The inspector determined that all of the corrective actions listed in the RCE have been either scheduled or completed and that the schedule was consistent with the licensee's commitments made to resolve the violation as clarified in their December 7, 2009 response for additional information.
 
    d. IP 95001 requires that the inspection staff determine that the licensee developed quantitative and qualitative measures of success for determining the effectiveness of the corrective actions to preclude repetition.  
                                          8
As documented in PIP M-07-4313, the licensee established measures for determining  
  The RCE did not fully document the organizational and programmatic weaknesses that
the effectiveness of the corrective actions. These measures included the following:  
  led to the condition, nor the reasons that multiple opportunities were missed for earlier
* Conduct an independent review of the RN DBD to ensure that it clearly provides design and licensing bases of the RN Strainer and meets the actual design; and  
  discovery. For example, the reason(s) why there was not a clear understanding of the
* Perform an effective review six to nine months following completion of the modifications to RN strainer backwash system using the effectiveness review template.  
  design bases of the system or why the design change/50.59 process failed to identify the
The licensee's corrective action program only requires effectiveness reviews to be conducted on corrective actions to prevent recurrence (CAPR) and does not provide explicit guidance on how to conduct the reviews. The licensee uses a template posted on their performance improvement website as guidance for these reviews. It consists of a series of five questions: 1) Have the CAPR(s) been properly implemented; 2) Were CAPR(s) implemented per the latest approved schedule; 3) Have the CAPR(s) been challenged adequately; 4) Were the CAPR(s) successful in preventing recurrence; and  
  USFAR requirement for manual backwash were not fully explored. This was identified
5) Have the CAPR(s) prevented the same or similar events?  
  by the licensee during their 95001 readiness review (M-SAG-SA-10-11) and PIP M-10-
13 Enclosure The independent review of the revised DBD merely verifies that the action was completed adequately and does not evaluate whether the revision prevented recurrence of improper design changes. The effectiveness of the modifications to restore compliance will be demonstrated during the post-modification testing. The action was  
  1208 was initiated to evaluate the reasons why the design bases were not fully
initiated to correct the condition, not to prevent recurrence for the causes of the event. Since no other actions were designated as CAPRs, no additional reviews of effectiveness to prevent recurrence are required by the CAP process. This was recognized by the IP 95001 readiness review team (M-SAG-SA-10-11). A corrective action on PIP M-10-1205 was created for the SA/PI Manager to review the current  
  understood. It concluded that the licensee did not know the UFSAR was the Current
processes and McGuire site understanding of requirements for evaluating CAPR effectiveness.  
  Licensing Basis (CLB) source at the time of the modification and that the Design and
    e. IP 95001 requires that the inspection staff determine that the licensee's planned or taken corrective actions adequately address a Notice of Violation (NOV) that was the basis for the supplemental inspection, if applicable.  
  Licensing ownership had moved from the General Office to the site in the 1992 to 1996
The NRC issued the NOV to the licensee on October 27, 2008. The licensee provided the NRC a written response to the NOV on November 25, 2008. The licensee's response described: 1) the reasons for the violation; 2) corrective steps which have been taken and the results achieved; 3) corrective steps which will be taken to avoid further violations; and 4) the date when full compliance will be achieved. However, the  
  timeframe.
licensee revised their commitments contained in the response to the NOV in a letter dated October 1, 2009. The licensee had originally planned to submit a license amendment to request that the NRC accept the non-conforming condition as is, however following a detailed review the licensee determined a preferred approach would be to implement plant changes to bring the system into full compliance. These changes will  
  Contributing to the apparent lack of detailed documentation of the causes of the event
be implemented in three phases. Phase 1 will add an assured air supply to the strainer backwash inlet valves. Phase 2 will improve the piping layout from the strainer backwash outlets to the WZ sump to reduce head loss when conducting backwash operation to the sump. Phase 3 will install safety related strainer backwash discharge pumps to provide the motive force to discharge backwash effluent to the RN return  
  was that the licensee did not revise the RCE when new information was discovered (M-
header and will remove the air-operated strainer backwash outlet valves.  
  08-3371 and M-09-2261) or when additional review of the RCE was conducted. The
During this inspection, the inspector reviewed the preliminary designs for these modifications and associated calculations. The inspector determined that when Phase 1 and 3 are completed the system will be restored to full compliance and that the  
  inspector identified that Nuclear System Directive (NSD) 212, Cause Analysis, indicated
licensee's planned and taken corrective actions addressed the NOV. However, the inspector was unable to determine if the Phase 2 modification would be acceptable due to incomplete design and associated calculations; and the potential reliance on throttling RN flow to achieve the necessary strainer pressure for backwash operations to the WZ sump. Since these corrective actions have not been completed, the implementation and effectiveness of the licensee's corrective actions will be reviewed during future inspections.  
  that in the event further information becomes available that potentially affects the results
    f. Findings
  of a root cause evaluation, the root cause should be reevaluated to determine if a
  No findings of significance were identified.  
  revision was required. The operability determination was revised and numerous
 
  corrective actions were added or revised, however the evaluation portion of the PIP was
14 Enclosure 4OA6 Exit Meeting
  not changed. This resulted in cases where the critical thinking on why a corrective
  On March 9, 2010, the inspector presented the results of the supplemental inspection to Mr. Steven D. Capps and other members of licensee management and staff. The  
  action was added was not documented and made the linkage between the root and
inspector confirmed that no proprietary information was provided or examined during the inspection.  
  contributing causes and the associated CAs to address the causes difficult. Additionally,
  ATTACHMENT: SUPPLEMENTAL INFORMATION  
  the original RCE did not identify that the failure to conduct testing to ensure that the
  backwash system functioned as designed was a contributor to this event. This was
  identified in the corrective actions for PIP M-08-3371, but the original RCE was never
  updated.
  However, the inspector determined that the organizational and programmatic
  weaknesses that caused this event, even if not specifically documented in the RCE,
  were ultimately addressed in the corrective actions for this PIP and in other related PIPs.
  For example, the corrective actions addressed weaknesses in the design bases
  documentation (e.g., DBD and UFSAR), in the design change process, in the 50.59
  process and in the knowledge and skills of engineering personnel and 10 CFR 50.59
  qualified evaluators and screeners. Based on the results of the inspection, the licensee
  initiated PIP M-10-1516 to evaluate the quality of root cause evaluations, including
  determining the reasons PIP M-07-4313 did not apply the why staircase sufficiently to
  determine what process weaknesses needed to be corrected and the reasons the RCE
  was not revised when additional information was uncovered.
c. IP 95001 requires that the inspection staff determine that the licensees RCE include a
  consideration of prior occurrences of the problem and knowledge of prior operating
  experience.
  The licensees RCE included a review of both internal and external operating experience
  (OE). A search of the McGuire PIP database was conducted for previous events
  assigned cause codes of F1b (Unplanned entry into TS LCO) and J1e (Risks and
  Consequences associated with change not adequately reviewed). No previous events
                                                                                      Enclosure
 
                                          9
  were identified. However, these specific cause codes were not assigned to the root or
  contributing causes for this evaluation. This was identified by the licensee in their IP
  95001 readiness review (M-SAG-SA-10-11) and a subsequent search using the
  appropriate codes did not identify any prior occurrences. Based on the licensees
  evaluation and conclusions, the inspector determined that the licensees RCE included a
  consideration of prior occurrences of the problem and knowledge of prior OE.
d. IP 95001 requires that the inspection staff determine that the licensees RCE addresses
  the extent of condition and the extent of cause of the issue.
  To address the extent of condition issue, the licensees RCE contained a review of air-
  operated valves (AOVs) that receive safety signals that may need to be repositioned
  from their safety position following an accident. Based on recommendations from the
  McGuire NSRB meeting on February 13, 2008, additional corrective actions were added
  to expand the scope of the AOVs that were reviewed and to include instrumentation that
  is required post-accident that relied on instrument air (VI). No additional valves were
  found that required VI post-accident and some procedure changes were made to identify
  alternate indications that could be used for instrumentation that would be unavailable
  following a loss of VI. During the IP 95001 readiness review a deficiency was identified
  with the extent of condition. The team found that the extent of condition corrective
  actions (CAs) should address motive forces other than air (e.g., power-operated
  components) and other systems containing safety related/non-safety related interfaces
  should be sampled and evaluated to ensure no similar issues with other safety related
  systems exist (PIP M-10-1210). At the time of the inspection, the extent of condition
  review of safety/non-safety system interactions was still in progress.
  To address the extent of cause the RCE reviewed other areas where engineering may
  not have a clear understanding of design bases prior to changing plant configuration.
  Specifically, a corrective action was created to review the design basis document (DBD)
  for the entire RN system and the Design Basis Accident DBD to ensure they adequately
  reflect the current licensing basis. In addition, engineering personnel and 10 CFR 50.59
  qualified personnel were trained on this event and on the use of licensing basis
  documents during the design change process. During the IP 95001 readiness review a
  deficiency was identified with the extent of cause. The team found that the extent of
  cause CAs should be expanded to include the 10 CFR 50.59 process (program
  changes, effectiveness reviews and examples) and the Engineering
  Change/Engineering Change Approval process (program changes, effectiveness
  reviews and examples) to ensure current processes would prevent similar events (PIP
  M-10-1211). This PIP determined that recent 10 CFR 50.59 process changes provide
  confidence in the current processes such that a similar failure of the program, as
  documented under PIP M-07-4313, would not occur. Likewise, the current modification
  process related toward editorial changes process provides sufficient barriers to prevent
  design and implementation of a non-editorial modification under the editorial process. In
  addition, PIP M-10-1240 was initiated to perform detailed design bases impact reviews
  for historical modifications, which were deemed to have potentially similar attributes to
  the historical modification which improperly downgraded RN strainer safety
  classification. At the time of the inspection, this review was still in progress.
                                                                                    Enclosure
 
                                        10
  As stated earlier, the original RCE did not identify that the failure to conduct testing to
  ensure that the backwash system functioned as designed was a contributor to this event.
  However, this was identified following the discovery that backwash to the RC system
  was not possible and that backwash to the WZ sump could not be performed at high RN
  flow rates (PIP M-08-3371). Subsequently an extent of cause was conducted that
  sampled several other safety systems to ensure that all safety functions have been
  adequately functionally tested and/or monitored (PIP M-08-4602).
  The inspector concluded that the licensee has ultimately addressed the extent of
  condition and the extent of cause of the issue. However, weakness of the original extent
  of condition and extent of cause evaluations resulted in delays in conducting a thorough
  review, some aspects of which were still in progress at the time of the inspection.
e. IP 95001 requires that the inspection staff determine that the licensees root cause
  evaluation, extent of condition, and extent of cause appropriately considered the safety
  culture components as described in IMC 0305.
  As part of the RCE, the licensee did not specifically consider the safety culture
  components of IMC 0305, but did reference some safety culture components in their
  cause determination. Specifically, CC3 was assigned a cause code of previous industry
  or in-house operating experience was not effectively used to prevent problems (safety
  culture component of operating experience) and CC4 was assigned a cause code of
  corrective actions from previously identified problems or previous event causes were
  not adequate to prevent recurrence (safety culture component of problem identification
  and resolution). The failure to consider safety culture components in the RCE was
  recognized by the IP 95001 readiness review team (M-SAG-SA-10-11). A corrective
  action was created in PIP M-07-4313 to conduct an assessment of the safety culture
  components and a corrective action to PIP M-10-1205 was created for the Safety
  Assurance/Performance Improvement (SA/PI) Manager to review the current processes
  and McGuire site understanding of requirements for considering safety culture
  components. The safety culture component evaluation that was conducted as a result of
  the readiness review team recommendation concluded that there were no aspects of the
  RCE that would indicate that the organizations or individuals involved exhibited behavior
  indicative of a weakness in safety culture, even though the cause codes assigned to two
  of the contributing causes directly relate to safety culture components. This further
  demonstrated the lack of specific guidance on considering safety culture components
  during root cause evaluations.
  Based on the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate
  the quality of root cause evaluations, including addressing the lack of guidance on
  considering safety culture components during root cause evaluations.
f. Findings
  No findings of significance were identified.
                                                                                      Enclosure
 
                                            11
02.03 Corrective Actions
  a. IP 95001 requires that the inspection staff determine that: (1) the licensee specified
      appropriate corrective actions for each root and/or contributing cause; or (2) an
      evaluation that states no actions are necessary is adequate.
      The root cause and contributing causes 1 and 2 were linked to corrective actions.
      However contributing causes 3 and 4 were not linked to specific corrective actions. This
      was identified in the IP 95001 readiness review and PIP M-10-1214 was initiated to
      correct this oversight.
      The inspector reviewed the corrective actions taken for PIP M-07-4313 and determined
      that, although not well linked, adequate corrective actions have been or will be taken to
      address the causes of this condition.
  b. IP 95001 requires that the inspection staff determine that the licensee prioritized
      corrective actions with consideration of risk significance and regulatory compliance.
      The licensee took immediate corrective actions to compensate for the inability to
      manually backwash the RN strainers following a loss of instrument air by modifying the
      strainer backwash outlet valves to provide a manual means to open the valves without
      relying on VI. These compensatory actions and associated operability determination
      were later modified following the discovery that backwash flow path to the RC system
      was unavailable and that a negative pressure was created in the strainer during high RN
      flow rates (PIP M-08-3717). This led to procedure changes that provided guidance on
      aligning strainer backwash flow, if needed, to the WZ sump only and to throttle RN flow
      to the Component Cooling Water (KC) heat exchangers if strainer pressure was
      inadequate for sump discharge. These compensatory actions and the associated
      operability determination were modified again following the discovery of additional
      macro-fouling sources (PIP M-09-2216). On November 6, 2009, the NRC requested the
      licensee provide an explanation addressing what compensatory or other measures were
      in place to assure the operability of the RN system in case strainer macro-fouling does
      occur until full compliance is restored. In their response dated December 7, 2009, the
      licensee stated that a dedicated operator was stationed to perform time-critical actions to
      initiate backwash supply flow to the strainers on a loss of instrument air and listed
      several modifications and procedural changes that have been made. The response only
      addressed macro-fouling from soft debris that could be crushed in the strainer and
      passed through the system and did not reference the procedure to align backwash outlet
      flow to the WZ sump or the potential need to throttle RN flow to the KC heat exchangers
      to achieve adequate strainer pressure for backwash operation. The licensee committed
      to supplement their December 7, 2009 response by April 12, 2010, to more completely
      describe their interim compensatory measures, including those that would mitigate all
      design basis type macro-fouling mechanisms that could impact the RN system during
      design basis events.
      These events also impacted the corrective actions needed to restore the system to full
      compliance. The licensee determined that the preferred approach to restore compliance
      would be to implement a series of modifications including installation of safety related
                                                                                        Enclosure
 
                                        12
  strainer backwash discharge pumps to provide the motive force to direct backwash flow
  to the RN return header. In a letter dated October 1, 2009, the licensee changed their
  original commitment of submitting a license amendment to resolve the NOV, to
  completing these modifications by December 2012. On November 6, 2009, the NRC
  requested the licensee provide a discussion on why the proposed completion date
  represented the first available opportunity to restore compliance. In their response dated
  December 7, 2009, the licensee provided the justification for the proposed durations for
  modification implementation. The inspector reviewed the reasons provided for the
  projected completion dates for the modifications and found them to be reasonable given
  the magnitude of the modifications.
  The corrective action to prevent recurrence for the root cause was to revise the DBD for
  the RN system. This action was appropriately prioritized and has been completed.
  Based upon the appropriate prioritization of the DBD revision and the review of the
  implementation schedule for the modifications needed to restore full compliance of the
  system, the inspector determined that the corrective actions were prioritized with
  consideration of the risk significance and regulatory compliance.
c. IP 95001 requires that the inspection staff determine that the licensee established a
  schedule for implementing and completing the corrective actions.
  The inspector determined that all of the corrective actions listed in the RCE have been
  either scheduled or completed and that the schedule was consistent with the licensees
  commitments made to resolve the violation as clarified in their December 7, 2009
  response for additional information.
d. IP 95001 requires that the inspection staff determine that the licensee developed
  quantitative and qualitative measures of success for determining the effectiveness of the
  corrective actions to preclude repetition.
  As documented in PIP M-07-4313, the licensee established measures for determining
  the effectiveness of the corrective actions. These measures included the following:
  *   Conduct an independent review of the RN DBD to ensure that it clearly provides
      design and licensing bases of the RN Strainer and meets the actual design; and
  *   Perform an effective review six to nine months following completion of the
      modifications to RN strainer backwash system using the effectiveness review
      template.
  The licensees corrective action program only requires effectiveness reviews to be
  conducted on corrective actions to prevent recurrence (CAPR) and does not provide
  explicit guidance on how to conduct the reviews. The licensee uses a template posted
  on their performance improvement website as guidance for these reviews. It consists of
  a series of five questions: 1) Have the CAPR(s) been properly implemented; 2) Were
  CAPR(s) implemented per the latest approved schedule; 3) Have the CAPR(s) been
  challenged adequately; 4) Were the CAPR(s) successful in preventing recurrence; and
  5) Have the CAPR(s) prevented the same or similar events?
                                                                                    Enclosure
 
                                          13
  The independent review of the revised DBD merely verifies that the action was
  completed adequately and does not evaluate whether the revision prevented recurrence
  of improper design changes. The effectiveness of the modifications to restore
  compliance will be demonstrated during the post-modification testing. The action was
  initiated to correct the condition, not to prevent recurrence for the causes of the event.
  Since no other actions were designated as CAPRs, no additional reviews of
  effectiveness to prevent recurrence are required by the CAP process. This was
  recognized by the IP 95001 readiness review team (M-SAG-SA-10-11). A corrective
  action on PIP M-10-1205 was created for the SA/PI Manager to review the current
  processes and McGuire site understanding of requirements for evaluating CAPR
  effectiveness.
e. IP 95001 requires that the inspection staff determine that the licensees planned or taken
  corrective actions adequately address a Notice of Violation (NOV) that was the basis for
  the supplemental inspection, if applicable.
  The NRC issued the NOV to the licensee on October 27, 2008. The licensee provided
  the NRC a written response to the NOV on November 25, 2008. The licensees
  response described: 1) the reasons for the violation; 2) corrective steps which have
  been taken and the results achieved; 3) corrective steps which will be taken to avoid
  further violations; and 4) the date when full compliance will be achieved. However, the
  licensee revised their commitments contained in the response to the NOV in a letter
  dated October 1, 2009. The licensee had originally planned to submit a license
  amendment to request that the NRC accept the non-conforming condition as is, however
  following a detailed review the licensee determined a preferred approach would be to
  implement plant changes to bring the system into full compliance. These changes will
  be implemented in three phases. Phase 1 will add an assured air supply to the strainer
  backwash inlet valves. Phase 2 will improve the piping layout from the strainer
  backwash outlets to the WZ sump to reduce head loss when conducting backwash
  operation to the sump. Phase 3 will install safety related strainer backwash discharge
  pumps to provide the motive force to discharge backwash effluent to the RN return
  header and will remove the air-operated strainer backwash outlet valves.
  During this inspection, the inspector reviewed the preliminary designs for these
  modifications and associated calculations. The inspector determined that when Phase 1
  and 3 are completed the system will be restored to full compliance and that the
  licensees planned and taken corrective actions addressed the NOV. However, the
  inspector was unable to determine if the Phase 2 modification would be acceptable due
  to incomplete design and associated calculations; and the potential reliance on throttling
  RN flow to achieve the necessary strainer pressure for backwash operations to the WZ
  sump. Since these corrective actions have not been completed, the implementation and
  effectiveness of the licensees corrective actions will be reviewed during future
  inspections.
f. Findings
  No findings of significance were identified.
                                                                                      Enclosure
 
                                        14
4OA6 Exit Meeting
    On March 9, 2010, the inspector presented the results of the supplemental inspection to
    Mr. Steven D. Capps and other members of licensee management and staff. The
    inspector confirmed that no proprietary information was provided or examined during the
    inspection.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                                                                  Enclosure


 
                                SUPPLEMENTAL INFORMATION
Attachment SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
  KEY POINTS OF CONTACT  
Licensee Personnel
Licensee Personnel
R. Abbott, Regulatory Compliance Engineer
R. Abbott, Regulatory Compliance Engineer K. Ashe, Regulatory Compliance Manager D. Brewer, Safety Assurance Manager M. Broome, Electrical and I&C Engineer S. Capps, Station Manager  
K. Ashe, Regulatory Compliance Manager
K. Crane, Regulatory Compliance Engineer C. Curry, Engineering Manager R. Harris, Modifications Engineer G. Holbrooks, Project Management S. Heuertz, Performance Improvement Team S. Karriker, Balance of Plant Engineering Supervisor G. Kent, Duke Energy Regulatory Compliance Engineer  
D. Brewer, Safety Assurance Manager
M. Leisure, Regulatory Compliance Engineer W. Leggette, Nuclear Operations Support J. Nolin, Mechanical and Civil Engineering Manager R. Pacetti, Performance Improvement Team Manager T. Pederson, RN System Engineer  
M. Broome, Electrical and I&C Engineer
R. Repko, Site Vice President F. Twogood, Engineering Consultant R. Weathers, RN System Engineer M. Weiner, Nuclear Operations Support  
S. Capps, Station Manager
K. Crane, Regulatory Compliance Engineer
C. Curry, Engineering Manager
R. Harris, Modifications Engineer
G. Holbrooks, Project Management
S. Heuertz, Performance Improvement Team
S. Karriker, Balance of Plant Engineering Supervisor
G. Kent, Duke Energy Regulatory Compliance Engineer
M. Leisure, Regulatory Compliance Engineer
W. Leggette, Nuclear Operations Support
J. Nolin, Mechanical and Civil Engineering Manager
R. Pacetti, Performance Improvement Team Manager
T. Pederson, RN System Engineer
R. Repko, Site Vice President
F. Twogood, Engineering Consultant
R. Weathers, RN System Engineer
M. Weiner, Nuclear Operations Support
NRC Personnel
NRC Personnel
J. Brady, Senior Resident Inspector - McGuire J. Bartley, Chief, Reactor Projects Branch 1  
J. Brady, Senior Resident Inspector - McGuire
ITEMS OPENED, CLOSED AND DISCUSSED
J. Bartley, Chief, Reactor Projects Branch 1
  Closed 05000369,370/2008009-01 VIO Failure to Take Adequate Corrective Action for Implementation of Safety-Related RN  
                        ITEMS OPENED, CLOSED AND DISCUSSED
Strainer Backwash (Section 4OA4)  
Closed
  LIST OF DOCUMENTS REVIEWED  
05000369,370/2008009-01               VIO         Failure to Take Adequate Corrective Action
                                                  for Implementation of Safety-Related RN
                                                  Strainer Backwash (Section 4OA4)
                              LIST OF DOCUMENTS REVIEWED
Procedures
Procedures
 
AP/1/A/5500/22, Loss of VI Abnormal Procedure, Rev. 28
AP/1/A/5500/22, Loss of VI Abnormal Procedure, Rev. 28 AP/2/A/5500/22, Loss of VI Abnormal Procedure, Rev. 25 OP/1/A/6400/006, Nuclear Service Water System, Rev. 180 OP/2/A/6400/006, Nuclear Service Water System, Rev. 136 OP/1/A/6100/010 M, Annunciator Response for Panel 1 AD-12, Rev. 47  
AP/2/A/5500/22, Loss of VI Abnormal Procedure, Rev. 25
2 Attachment OP/2/A/6100/010 M, Annunciator Response for Panel 2 AD-12, Rev. 31 RP/0/A/5700/006, Natural Disaster, Rev. 22  
OP/1/A/6400/006, Nuclear Service Water System, Rev. 180
EDM-601, Engineering Change, Rev. 10  
OP/2/A/6400/006, Nuclear Service Water System, Rev. 136
NSD 201, Reporting Requirements, Rev. 21 NSD 202, Reportability, Rev. 21 NSD 203, Operability/Functionality, Rev. 21 NSD 208, Problem Investigation Process (PIP), Rev. 31 NSD 209, 10CFR 50.59 Process, Rev. 14  
OP/1/A/6100/010 M, Annunciator Response for Panel 1 AD-12, Rev. 47
NSD-212, Cause Analysis, Rev. 16 NSD-228, Applicability Determination, Rev. 5 NSD-301, Engineering Change Process, Rev. 34  
                                                                                  Attachment
PIPs M-89-0290, Design Engineering Evaluate Safety Classification of RN Strainers
 
M-93-0297, Viability of RN Strainers M-00-3122, RN strainer backwash valve modification MGMM8444 does not incorporate adequate provisions for Operations to perform manual strainer backwash M-02-2427, Re-evaluation of RN Strainer Filtration Function (Safety or Non-Safety Related) M-07-4177, 1B and 2B RN strainer experienced numerous Hi D/P backwashes  
                                              2
M-07-4313, Inability to manually backwash RN strainers during post-accident conditions M-07-5978, Evaluate Compliance with Design Basis for RN Strainer Backwash System Utilizing Non-Safety Related Equipment M-08-1574, McGuire NSRB Meeting Minutes from February 13, 2008 M-08-3371, RN Strainer Backwash Return Flow Direction is from RC (Lake) to the Strainer Instead of from the Strainer to RC (Lake) M-08-3668, Assess Functionality of Groundwater Level Monitoring System Based on RN Strainer Backwash Flow to WZ Sump M-08-4602, Engineering Management Discussion on Extent of Condition M-08-3371 Problem Evaluation M-08-4911, NRC Issuance of a Preliminary Greater then Green Finding M-08-7507, NRC Issuance of Violation (VIO) 08-09-01 M-09-2216, 2A RN Strainer Fouled During High RN Flow Testing per TT Procedure M-09-2341, During Loss of Instrument Air (VI) Events, RN A Train Pump Flow May Self-Limit Based on Suction Pressure Limits When Aligned to the SNSWP M-10-1145, engineering Review of SITA 93-01 Audit M-10-1205, Assessment M-SAG-SA-10-11: NRC IP 95001 Supplemental Inspection Readiness Review - RN System White Finding.   M-10-1208, Assessment M-SAG-SA-10-11 Deficiency #1 (M-07-4313 Root Cause Evaluation lacks development) M-10-1209, Assessment M-SAG-SA-10-11 Deficiency #2 (No evaluation was performed to reconcile the difference between the M-07-4313 Root Cause and the NRC NOV EA-08-220) M-10-1210, Assessment M-SAG-SA-10-11 Deficiency #3 (M-07-4313 Root Cause Extent of Condition evaluation and corrective actions are fragmented and inadequate) M-10-1211, Assessment M-SAG-SA-10-11 Deficiency #4 (M-07-4313 Extent of Cause evaluation corrective actions are inadequate and not all-encompassing)  
OP/2/A/6100/010 M, Annunciator Response for Panel 2 AD-12, Rev. 31
 
RP/0/A/5700/006, Natural Disaster, Rev. 22
3 Attachment M-10-1212, Assessment M-SAG-SA-10-11 Deficiency #5 (M-07-4313 Root Cause is not adequately addressed by the CAPRs) M-10-1214, Assessment M-SAG-SA-10-11 Deficiency #6 (There are no CAs for M-07-4313 Root Cause Evaluation Contributing Cause 3 (CC-3) or Contributing Cause 4 (CC-4)) M-10-1217, Assessment M-SAG-SA-10-11 Deficiency #7 (several situations noted in PIP M-07-4313 wherein the individual performing the corrective action and the approver were the same person) M-10-1240, Perform Detailed Design Bases Impact Review for Historical Modifications Similar to Modification to Downgrade RN Strainer Safety Classification  
EDM-601, Engineering Change, Rev. 10
Miscellaneous
NSD 201, Reporting Requirements, Rev. 21
  MCS-1465.00-00-0004, Design Basis Specification for Loss of VI, Rev. 1 MCS-1465.00-00-0005, Design Basis Specification for Design Events, Rev. 4 MCS-1574.RN-00-0001, Design Basis Specification for Nuclear Service Water (RN) System, Rev. 28 MCS-1581.WZ-00-0001, Design Basis Specification for the WZ System, Rev. 9 MGDS-224, McGuire Design Study to Document the Design Basis for the RN Pump Strainer, 7/11/1990 M-SAG-SA-10-11, NRC IP 95001 Supplemental Inspection Readiness Review-RN System White Finding SITA-93-01, operational readiness and functionality of McGuire's Nuclear Service Water (RN) System Licensee Event Report (LER) 05000369/2007-004-00, Procedure Deficiency identified for Performing a Manual Backwash of Nuclear Service Water (RN) Strainers due to Reliance on Non-Safety Instrument Air UFSAR Section 9.2.2, Nuclear Service Water System and Ultimate Heat Sink TS 3.7.7, Nuclear Service Water System (NSWS), Amendment Nos. 184/166, & Bases B3.7.7, Rev. 0 A/R 00302781, 10CFR50.59 Screen for Modifications to Add Safety Related Air Supply to the RN Strainer Backwash Inlet valves A/R 00302920, 10CFR50.59 Screen for Modifications to Reroute the Backwash Effluent Line to the Auxiliary Building Groundwater Sump (WZ) A/R 00302925, 10CFR50.59 Screen for Modifications to Incorporate New Pressure Transmitters and New Backwash Discharge Pumps A/R 00302927, 10CFR50.59 Evaluation for Modifications to Incorporate New Pressure Transmitters and New Backwash Discharge Pumps  A/R 00303967, 10CFR50.59 Screen for Modifications to Incorporate New Pressure Transmitters and New Backwash Discharge Pumps A/R 00303869, 10CFR50.59 Evaluation for Modifications to Incorporate New Pressure Transmitters and New Backwash Discharge Pumps A/R 00304335, 10CFR50.59 Screen for OP/1(2)/A/6400/006, Nuclear Service Water Revisions 202/158 A/R 00304336, 10CFR50.59 Screen for OP/1(2)/A/6400/006, Nuclear Service Water Revisions 203/159 OMP 12-1, Dedicated RN Strainer Backwash Operator is Required, Rev. 2 dated 5/6/2009 SOMP 01-13, Designated RN Back-Flush Operator for Loss of VI, Rev. 1 dated 6/22/2009  
NSD 202, Reportability, Rev. 21
 
NSD 203, Operability/Functionality, Rev. 21
4 Attachment Modifications
NSD 208, Problem Investigation Process (PIP), Rev. 31
  MGMM-3794, Editorial Minor Modification to Allow Downgrade of the function of the RN Strainers, 8/12/1993 MGMM-8444, Install New ITT Diaphragm valves at Outlet of RN Strainers on Unit 2, 4/18/2001 MGMM-11224, Install New ITT Diaphragm valves at Outlet of RN Strainers on Unit 1, 9/7/2001 MGMM-14403, Reclassify RN Strainers as QA-1 due to Recent Macro-Fouling Events, 8/11/2003 MD101360, Temporary Modification to Install Ball Thrust Bearing on 1RN0022A and Mechanical Gag on 1RN0023, 8/8/2007 MD101361, Temporary Modification to Install Ball Thrust Bearing on 1RN0026B and Mechanical Gag on 1RN0027, 8/8/2007 MD201362, Temporary Modification to Install Ball Thrust Bearing on 2RN0022A and Mechanical Gag on 2RN0023, 8/8/2007 MD201363, Temporary Modification to Install Ball Thrust Bearing on 2RN0026A and Mechanical Gag on 2RN0027, 8/8/2007 MD102035, Permanently Install Ball Thrust Bearing on 1RN0022A/26B and Remove Mechanical Gag on 1RN0023/27, 11/5/2008 MD202037, Permanently Install Ball Thrust Bearing on 1RN0022A/26B and Remove Mechanical Gag on 1RN0023/27, 11/5/2008 MD501561 - LLI macrofouling barrier  
NSD 209, 10CFR 50.59 Process, Rev. 14
MD101813 - RN Strainer 1A Backwash Instrumentation MD101624 - RN Strainer 1B Backwash Instrumentation MD201814 - RN Strainer 2A Backwash Instrumentation MD201629 - RN Strainer 2B Backwash Instrumentation EC 101543, Installation of an Assured Air Supply for 1-RN-21A  
NSD-212, Cause Analysis, Rev. 16
EC 101545, Installation of an Assured Air Supply for 1-RN-25B EC 101544, Installation of an Assured Air Supply for 2-RN-21A EC 101546, Installation of an Assured Air Supply for 2-RN-25B EC 101547, Improved Piping Layout for Manual Strainer Backwash from 1A RN Strainer to WZ Sump EC 101549, Improved Piping Layout for Manual Strainer Backwash from 1B RN Strainer to WZ Sump EC 101548, Improved Piping Layout for Manual Strainer Backwash from 2A RN Strainer to WZ Sump EC 101550, Improved Piping Layout for Manual Strainer Backwash from 2B RN Strainer to WZ Sump EC 102477, Installation of RN Strainer Backwash Discharge Pump for 1A RN Strainer EC 102478, Installation of RN Strainer Backwash Discharge Pump for 1B RN Strainer EC 102479, Installation of RN Strainer Backwash Discharge Pump for 2A RN Strainer EC 102482, Installation of RN Strainer Backwash Discharge Pump for 2B RN Strainer ECR 2081, Provide Remote Throttling Capability to Unit 1 KC HX Supply Isolation Valves ECR 2087, Provide Remote Throttling Capability to Unit 2 KC HX Supply Isolation Valves  
NSD-228, Applicability Determination, Rev. 5
NSD-301, Engineering Change Process, Rev. 34
PIPs
M-89-0290, Design Engineering Evaluate Safety Classification of RN Strainers
M-93-0297, Viability of RN Strainers
M-00-3122, RN strainer backwash valve modification MGMM8444 does not incorporate
  adequate provisions for Operations to perform manual strainer backwash
M-02-2427, Re-evaluation of RN Strainer Filtration Function (Safety or Non-Safety Related)
M-07-4177, 1B and 2B RN strainer experienced numerous Hi D/P backwashes
M-07-4313, Inability to manually backwash RN strainers during post-accident conditions
M-07-5978, Evaluate Compliance with Design Basis for RN Strainer Backwash System Utilizing
  Non-Safety Related Equipment
M-08-1574, McGuire NSRB Meeting Minutes from February 13, 2008
M-08-3371, RN Strainer Backwash Return Flow Direction is from RC (Lake) to the Strainer
  Instead of from the Strainer to RC (Lake)
M-08-3668, Assess Functionality of Groundwater Level Monitoring System Based on RN
  Strainer Backwash Flow to WZ Sump
M-08-4602, Engineering Management Discussion on Extent of Condition M-08-3371 Problem
  Evaluation
M-08-4911, NRC Issuance of a Preliminary Greater then Green Finding
M-08-7507, NRC Issuance of Violation (VIO) 08-09-01
M-09-2216, 2A RN Strainer Fouled During High RN Flow Testing per TT Procedure
M-09-2341, During Loss of Instrument Air (VI) Events, RN A Train Pump Flow May Self-Limit
  Based on Suction Pressure Limits When Aligned to the SNSWP
M-10-1145, engineering Review of SITA 93-01 Audit
M-10-1205, Assessment M-SAG-SA-10-11: NRC IP 95001 Supplemental Inspection Readiness
  Review - RN System White Finding.
M-10-1208, Assessment M-SAG-SA-10-11 Deficiency #1 (M-07-4313 Root Cause Evaluation
  lacks development)
M-10-1209, Assessment M-SAG-SA-10-11 Deficiency #2 (No evaluation was performed to
  reconcile the difference between the M-07-4313 Root Cause and the NRC NOV EA-08-220)
M-10-1210, Assessment M-SAG-SA-10-11 Deficiency #3 (M-07-4313 Root Cause Extent of
  Condition evaluation and corrective actions are fragmented and inadequate)
M-10-1211, Assessment M-SAG-SA-10-11 Deficiency #4 (M-07-4313 Extent of Cause
  evaluation corrective actions are inadequate and not all-encompassing)
                                                                                    Attachment
 
                                              3
M-10-1212, Assessment M-SAG-SA-10-11 Deficiency #5 (M-07-4313 Root Cause is not
  adequately addressed by the CAPRs)
M-10-1214, Assessment M-SAG-SA-10-11 Deficiency #6 (There are no CAs for M-07-4313
  Root Cause Evaluation Contributing Cause 3 (CC-3) or Contributing Cause 4 (CC-4))
M-10-1217, Assessment M-SAG-SA-10-11 Deficiency #7 (several situations noted in PIP M-07-
  4313 wherein the individual performing the corrective action and the approver were the
  same person)
M-10-1240, Perform Detailed Design Bases Impact Review for Historical Modifications Similar
  to Modification to Downgrade RN Strainer Safety Classification
Miscellaneous
MCS-1465.00-00-0004, Design Basis Specification for Loss of VI, Rev. 1
MCS-1465.00-00-0005, Design Basis Specification for Design Events, Rev. 4
MCS-1574.RN-00-0001, Design Basis Specification for Nuclear Service Water (RN) System,
  Rev. 28
MCS-1581.WZ-00-0001, Design Basis Specification for the WZ System, Rev. 9
MGDS-224, McGuire Design Study to Document the Design Basis for the RN Pump Strainer,
  7/11/1990
M-SAG-SA-10-11, NRC IP 95001 Supplemental Inspection Readiness Review-RN System
  White Finding
SITA-93-01, operational readiness and functionality of McGuires Nuclear Service Water (RN)
  System
Licensee Event Report (LER) 05000369/2007-004-00, Procedure Deficiency identified for
  Performing a Manual Backwash of Nuclear Service Water (RN) Strainers due to Reliance on
  Non-Safety Instrument Air
UFSAR Section 9.2.2, Nuclear Service Water System and Ultimate Heat Sink
TS 3.7.7, Nuclear Service Water System (NSWS), Amendment Nos. 184/166, & Bases B3.7.7,
  Rev. 0
A/R 00302781, 10CFR50.59 Screen for Modifications to Add Safety Related Air Supply to the
  RN Strainer Backwash Inlet valves
A/R 00302920, 10CFR50.59 Screen for Modifications to Reroute the Backwash Effluent Line to
  the Auxiliary Building Groundwater Sump (WZ)
A/R 00302925, 10CFR50.59 Screen for Modifications to Incorporate New Pressure Transmitters
  and New Backwash Discharge Pumps
A/R 00302927, 10CFR50.59 Evaluation for Modifications to Incorporate New Pressure
  Transmitters and New Backwash Discharge Pumps
  A/R 00303967, 10CFR50.59 Screen for Modifications to Incorporate New Pressure
  Transmitters and New Backwash Discharge Pumps
A/R 00303869, 10CFR50.59 Evaluation for Modifications to Incorporate New Pressure
  Transmitters and New Backwash Discharge Pumps
A/R 00304335, 10CFR50.59 Screen for OP/1(2)/A/6400/006, Nuclear Service Water Revisions
  202/158
A/R 00304336, 10CFR50.59 Screen for OP/1(2)/A/6400/006, Nuclear Service Water Revisions
  203/159
OMP 12-1, Dedicated RN Strainer Backwash Operator is Required, Rev. 2 dated 5/6/2009
SOMP 01-13, Designated RN Back-Flush Operator for Loss of VI, Rev. 1 dated 6/22/2009
                                                                                    Attachment
 
                                              4
Modifications
MGMM-3794, Editorial Minor Modification to Allow Downgrade of the function of the RN
  Strainers, 8/12/1993
MGMM-8444, Install New ITT Diaphragm valves at Outlet of RN Strainers on Unit 2, 4/18/2001
MGMM-11224, Install New ITT Diaphragm valves at Outlet of RN Strainers on Unit 1, 9/7/2001
MGMM-14403, Reclassify RN Strainers as QA-1 due to Recent Macro-Fouling Events,
  8/11/2003
MD101360, Temporary Modification to Install Ball Thrust Bearing on 1RN0022A and Mechanical
  Gag on 1RN0023, 8/8/2007
MD101361, Temporary Modification to Install Ball Thrust Bearing on 1RN0026B and Mechanical
  Gag on 1RN0027, 8/8/2007
MD201362, Temporary Modification to Install Ball Thrust Bearing on 2RN0022A and Mechanical
  Gag on 2RN0023, 8/8/2007
MD201363, Temporary Modification to Install Ball Thrust Bearing on 2RN0026A and Mechanical
  Gag on 2RN0027, 8/8/2007
MD102035, Permanently Install Ball Thrust Bearing on 1RN0022A/26B and Remove
  Mechanical Gag on 1RN0023/27, 11/5/2008
MD202037, Permanently Install Ball Thrust Bearing on 1RN0022A/26B and Remove
  Mechanical Gag on 1RN0023/27, 11/5/2008
MD501561 - LLI macrofouling barrier
MD101813 - RN Strainer 1A Backwash Instrumentation
MD101624 - RN Strainer 1B Backwash Instrumentation
MD201814 - RN Strainer 2A Backwash Instrumentation
MD201629 - RN Strainer 2B Backwash Instrumentation
EC 101543, Installation of an Assured Air Supply for 1-RN-21A
EC 101545, Installation of an Assured Air Supply for 1-RN-25B
EC 101544, Installation of an Assured Air Supply for 2-RN-21A
EC 101546, Installation of an Assured Air Supply for 2-RN-25B
EC 101547, Improved Piping Layout for Manual Strainer Backwash from 1A RN Strainer to WZ
  Sump
EC 101549, Improved Piping Layout for Manual Strainer Backwash from 1B RN Strainer to WZ
  Sump
EC 101548, Improved Piping Layout for Manual Strainer Backwash from 2A RN Strainer to WZ
  Sump
EC 101550, Improved Piping Layout for Manual Strainer Backwash from 2B RN Strainer to WZ
  Sump
EC 102477, Installation of RN Strainer Backwash Discharge Pump for 1A RN Strainer
EC 102478, Installation of RN Strainer Backwash Discharge Pump for 1B RN Strainer
EC 102479, Installation of RN Strainer Backwash Discharge Pump for 2A RN Strainer
EC 102482, Installation of RN Strainer Backwash Discharge Pump for 2B RN Strainer
ECR 2081, Provide Remote Throttling Capability to Unit 1 KC HX Supply Isolation Valves
ECR 2087, Provide Remote Throttling Capability to Unit 2 KC HX Supply Isolation Valves
                                                                                  Attachment


 
                                              5
5  Attachment Calculations
Calculations
  MCC-1223.24-00-00P1, Mechanical/ Civil Design Inputs for Assured Air Supply for Strainer Backwash Valves, Rev. 0 MCC-1223.24-00-00P2, Mechanical/ Civil Design Inputs for Piping Layoout for Manual Strainer Backwash, Rev. 0 MCC-1223.24-00-00P3, Mechanical/ Civil Design Inputs for RN Strainer Backwash Discharge Pumps, Rev. 0 MCC-1223.24-00-0096, RN System Flow Balance Acceptance Criteria Calculation, Rev. 4  
MCC-1223.24-00-00P1, Mechanical/ Civil Design Inputs for Assured Air Supply for Strainer
MCC-1223.24-00-0100, FMEA of RN Strainer Modifications MD101813, MD101624, MD201814, and MD201629, Rev. 1 MCC-1223.24-00-0102, RN Pump NPSH Calculation, Rev. 3 MCC-1223.24-00-0103, RN Strainer Macrofouling Source Calculation, Rev. 3 MCC-1223.24-00-0107, FMEA of RN Strainer Backwash Discharge Modifications, Rev. 3 MCC-1223.31-00-0010, Groundwater Drainage System Flow Analysis, Rev. 3 MCC-1331.16-00-0410, Electrical Discipline Design Inputs for EC 101543, EC 101544, EC 101545, EC 101546, Rev. 0 MCC-1331.16-00-0411, Electrical Discipline Design Inputs for EC 102477, EC 102478, EC 102479, EC 102482, Rev. 1  
  Backwash Valves, Rev. 0
PIPs generated as a result of this inspection
MCC-1223.24-00-00P2, Mechanical/ Civil Design Inputs for Piping Layoout for Manual Strainer
  PIP M-10-1429, NRC Inspector Questioned Basis and Conclusion of the Applicability Determination for Procedure Change That Allowed Throttling of KC Flow PIP M-10-1430, NRC Inspector Questioned Classification of Strainer Backwash as a Functional Failure PIP M-10-1448, NRC 95001 Supplemental Inspection Items to be Resolved PIP M-10-1516, Evaluate the Quality of Root Cause Evaluations and Associated Process Guidance Based on NRC 95001 Supplemental Inspection Results
  Backwash, Rev. 0
MCC-1223.24-00-00P3, Mechanical/ Civil Design Inputs for RN Strainer Backwash Discharge
  Pumps, Rev. 0
MCC-1223.24-00-0096, RN System Flow Balance Acceptance Criteria Calculation, Rev. 4
MCC-1223.24-00-0100, FMEA of RN Strainer Modifications MD101813, MD101624,
  MD201814, and MD201629, Rev. 1
MCC-1223.24-00-0102, RN Pump NPSH Calculation, Rev. 3
MCC-1223.24-00-0103, RN Strainer Macrofouling Source Calculation, Rev. 3
MCC-1223.24-00-0107, FMEA of RN Strainer Backwash Discharge Modifications, Rev. 3
MCC-1223.31-00-0010, Groundwater Drainage System Flow Analysis, Rev. 3
MCC-1331.16-00-0410, Electrical Discipline Design Inputs for EC 101543, EC 101544, EC
  101545, EC 101546, Rev. 0
MCC-1331.16-00-0411, Electrical Discipline Design Inputs for EC 102477, EC 102478, EC
  102479, EC 102482, Rev. 1
PIPs generated as a result of this inspection
PIP M-10-1429, NRC Inspector Questioned Basis and Conclusion of the Applicability
  Determination for Procedure Change That Allowed Throttling of KC Flow
PIP M-10-1430, NRC Inspector Questioned Classification of Strainer Backwash as a Functional
  Failure
PIP M-10-1448, NRC 95001 Supplemental Inspection Items to be Resolved
PIP M-10-1516, Evaluate the Quality of Root Cause Evaluations and Associated Process
  Guidance Based on NRC 95001 Supplemental Inspection Results
                                                                                  Attachment
}}
}}

Revision as of 20:16, 13 November 2019

IR 05000369-10-007, 05000370-10-007, on 03/01/2010 - 03/09/2010; McGuire Nuclear Station, Units 1 and 2; Supplemental Inspection IP 95001 in Response to a White Inspection Finding for Failure to Correct a Significant Condition Adverse to Qu
ML100900384
Person / Time
Site: Mcguire, McGuire  
Issue date: 03/31/2010
From: Bartley J
NRC/RGN-II/DRP/RPB1
To: Repko R
Duke Energy Carolinas, Duke Power Co
References
IR-10-007
Download: ML100900384 (24)


See also: IR 05000369/2010007

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

SAM NUNN ATLANTA FEDERAL CENTER

61 FORSYTH STREET, SW, SUITE 23T85

ATLANTA, GEORGIA 30303-8931

March 31, 2010

Mr. Regis T. Repko

Vice President

Duke Power Company, LLC

d/b/a Duke Energy Carolinas, LLC

McGuire Nuclear Station

MG01VP/12700 Hagers Ferry Road

Huntersville, NC 28078

SUBJECT: MCGUIRE NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTION

REPORT 05000369/2010007 AND 05000370/2010007

Dear Mr. Repko:

On March 9, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed a supplemental

inspection pursuant to Inspection Procedure 95001, Inspection for One or Two White Inputs in

a Strategic Performance Area, at your McGuire Nuclear Station, Units 1 and 2. The enclosed

inspection report documents the inspection results, which were discussed at the exit meeting on

March 9, 2010, with Mr. Steven D. Capps and other members of your staff.

As required by the NRC Reactor Oversight Process Action Matrix, this supplemental inspection

was performed because a finding of low to moderate safety significance (White) was identified

in the third quarter of 2008 for failure to correct a significant condition adverse to quality related

to macro-fouling of the nuclear service water (RN) system strainers. This finding was

documented previously in NRC Inspection Report 05000369,370/2008009 and resulted in

Violation (VIO) 05000369,370/2008009-01, Failure to Take Adequate Corrective Action for

Implementation of Safety-Related RN Strainer Backwash. The NRC was informed of your

readiness for the inspection on January 11, 2010.

The objectives of this supplemental inspection were to provide assurance that: (1) the root

causes and the contributing causes for the risk-significant issues were understood; (2) the

extent of condition and extent of cause of the issues were identified; and (3) corrective actions

were or will be sufficient to address and preclude repetition of the root and contributing causes.

This inspection examined activities conducted under your license as they related to safety and

compliance with the Commission's rules and regulations, and with the conditions of your

license. The inspector reviewed the root cause determination report, selected procedures and

records, and interviewed personnel.

DEC 2

The inspector determined that your staff, in general, performed an adequate evaluation of the

White finding. Your staffs evaluation determined that the root cause of the issue was changing

the configuration of the plant without a total understanding of the design and licensing bases for

the RN system strainers during accident conditions, which resulted in the inability to conduct

manual strainer backwashes during certain plant conditions.

Your staff also identified that this lack of understanding of design and licensing bases was not

limited to the RN strainers, but to the RN system in general and has taken corrective actions to

ensure the system design basis documents accurately reflect current licensing bases. The

inspector determined that the corrective actions taken and planned will restore the RN strainer

to full compliance with the licensing basis. In addition, the inspector found that corrective

actions taken or planned appear reasonable and will correct the causes that led to the non-

compliance and prevent recurrence. However, the inspector had several observations

regarding specific aspects of the root cause evaluation and corrective actions that warranted

additional consideration by your staff. These observations were discussed with your staff at the

exit meeting and are included in the report.

Based on the results of this supplemental inspection, no findings of significance were identified.

In accordance with the Code of Federal Regulations 10 CFR 2.390 of the NRCs Rules of

Practice, a copy of this letter, its enclosure, and your response (if any) will be available

electronically for public inspection in the NRC Public Document Room or from the Publicly

Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is

accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Jonathan H. Bartley, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Docket Nos.: 50-369, 50-370

License Nos.: NPF-9, NPF-17

Enclosure: NRC Integrated Inspection Report 05000369/2010007 and 05000370/2010007

w/Attachment - Supplemental Information

cc w/encl: (See page 3)

_ X SUNSI REVIEW COMPLETE JHB

OFFICE RII:DRP RII:DRP RII:DRP

SIGNATURE KJK /RA/ JBB /RA/ JHB /RA/

NAME KKorth JBrady JBartley

DATE 03/31/2010 03/31/2010 03/31/2010

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

DEC 3

cc w/encl: Dhiaa M. Jamil

Steven D. Capps Group Executive and Chief Nuclear Officer

Station Manager Duke Energy Carolinas, LLC

Duke Energy Carolinas, LLC Electronic Mail Distribution

Electronic Mail Distribution

Scotty L. Bradshaw

Training Manager

Duke Energy Carolinas, LLC

Electronic Mail Distribution

Kenneth L. Ashe

Regulatory Compliance Manager

Duke Energy Carolinas, LLC

Electronic Mail Distribution

R. L. Gill, Jr.

Manager

Nuclear Regulatory Issues & Industry Affairs

Duke Energy Carolinas, LLC

Electronic Mail Distribution

Lisa F. Vaughn

Associate General Counsel

Duke Energy Corporation

526 South Church Street-EC07H

Charlotte, NC 28202

Kathryn B. Nolan

Senior Counsel

Duke Energy Corporation

526 South Church Street-EC07H

Charlotte, NC 28202

David A. Repka

Winston Strawn LLP

Electronic Mail Distribution

County Manager of Mecklenburg County

720 East Fourth Street

Charlotte, NC 28202

W. Lee Cox, III

Section Chief

Radiation Protection Section

N.C. Department of Environmental

Commerce & Natural Resources

Electronic Mail Distribution

DEC 4

Letter to Regis T. Repko from Jonathan H. Bartley dated March 31, 2010

SUBJECT: MCGUIRE NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTION REPORT

05000369/2010007 AND 05000370/2010007

Distribution w/encl:

C. Evans, RII

L. Slack, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMMcGuire Resource

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-369, 50-370

License Nos.: NPF-9, NPF-17

Report Nos.: 05000369/2010007, 05000370/2010007

Licensee: Duke Energy Carolinas, LLC

Facility: McGuire Nuclear Station, Units 1 and 2

Location: Huntersville, NC 28078

Dates: March 1, 2010, through March 9, 2010

Inspectors: K. Korth, Resident Inspector Browns Ferry Nuclear Plant

Approved by: Jonathan H. Bartley, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000369/2010007, 05000370/2010007; 03/01/2010 - 03/09/2010; McGuire Nuclear Station,

Units 1 and 2; Supplemental Inspection IP 95001 in response to a White inspection finding for

failure to correct a significant condition adverse to quality related to macro-fouling of the nuclear

service water (RN) system strainers.

This inspection was conducted by a resident inspector. No findings of significance were

identified. The NRCs program for overseeing the safe operation of commercial nuclear power

reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated

December 2006.

Cornerstone: Mitigating Systems

This supplemental inspection was performed in accordance with Inspection Procedure (IP) 95001, Inspection for One or Two White Inputs in a Strategic Performance Area, to assess the

licensee's evaluation associated with a White inspection finding involving with the inability to

perform manual backwash on the Nuclear Service Water (RN) strainers identified in August of

2007. The NRC staff previously characterized this issue as having low to moderate safety

significance (White) as documented in NRC IR 05000369,370/2008009.

During this supplemental inspection, the inspector determined that, in general, the licensee

performed an adequate evaluation of the White finding. The licensees evaluation determined

that the root cause of the issue was changing the configuration of the plant without a total

understanding of the design. The RN strainer backwash system had been modified to replace

RN strainer backwash outlet manual valves with air-operated valves that could not be manually

over-ridden. This root cause, along with four other contributing causes, led to operation of the

system from 2000/2001 to 2007 without having the capability to manually backwash the

strainers following a loss of instrument air (VI). The licensee also identified that this lack of

understanding of design and licensing bases was not limited to the RN strainers, but to the RN

system in general and has taken corrective actions to ensure the system design basis

documents accurately reflect current licensing bases. The inspector determined that the

corrective actions taken and planned will restore the RN strainer to full compliance with the

licensing basis. In addition, the inspector found that corrective actions taken or planned appear

reasonable and will correct the causes that led to the non-compliance and prevent recurrence.

However, the inspector had the following observations regarding specific aspects of the root

cause evaluation (RCE) and corrective actions that warranted additional consideration by the

licensee. The RCE did not fully document the organizational and programmatic weaknesses

that led to the condition, or the reasons that multiple opportunities were missed for earlier

discovery (section 02.02.b). The licensee did not revise the RCE when new information was

discovered or when additional reviews of the RCE were conducted (section 02.02.b).

Weakness of the original extent of condition and extent of cause evaluations resulted in delays

in conducting a thorough review, some aspects of which were still in progress at the time of the

inspection (section 02.02.d). The RCE did not specifically consider the safety culture

components of Inspection Manual Chapter 0305 (section 02.02.e). The root cause and

contributing causes were not well linked to the associated corrective actions (section 02.03.a).

The quantitative and qualitative measures of success for determining the effectiveness of the

Enclosure

3

corrective actions to preclude repetition were not well established (section 02.03.d). Based on

the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate the quality of root

cause evaluations.

Given the licensees acceptable performance in addressing the non-compliance of the RN

strainer with its licensing bases, the White finding associated with this issue is being closed and

will only be considered in assessing plant performance until the end of this quarter in

accordance with the guidance in IMC 0305, Operating Reactor Assessment Program. Since

many of the corrective actions have not been completed, the implementation and effectiveness

of the licensees corrective actions will be reviewed during future inspections.

Enclosure

REPORT DETAILS

4. OTHER ACTIVITIES

4OA4 Supplemental Inspection

.01 Inspection Scope

The NRC staff performed this supplemental inspection in accordance with IP 95001 to

assess the licensees evaluation of a White finding which affected the Mitigating

Systems cornerstone in the Reactor Safety strategic performance area. The inspection

objectives were to:

  • provide assurance that the root and contributing causes of risk-significant issues were

understood;

  • provide assurance that the extent of condition and extent of cause of risk-significant

issues were identified; and

  • provide assurance that the licensees corrective actions for risk-significant issues

were or will be sufficient to address the root and contributing causes and to preclude

repetition.

The licensee entered the Regulatory Response Column of the NRCs Action Matrix in

the third quarter of 2008 as a result of one inspection finding of low to moderate safety

significance (White). The finding was associated with the failure to take adequate

corrective actions related to implementation of a safety-related RN strainer backwash

system. On August 6, 2007, the "A" Train of the RN system was declared inoperable

when the licensee discovered that manually backwashing RN strainers was not always

possible during design basis accidents. In 2000 on Unit 2 and in 2001 on Unit 1, a

modification had been implemented to replace strainer backwash outlet manual valves

with air-operated valves that could not be manually over-ridden. The Station Instrument

Air (VI) system was non-safety-related and could not be relied upon to manually

backwash the RN strainers during or following design basis accidents. The finding was

characterized as having low to moderate safety significance (White) based on the results

of a Phase 3 risk analysis performed by a region-based senior reactor analyst (SRA), as

discussed in NRC Inspection Report (IR) 05000369,370/2008009.

As a result of identifying this non-conformance, the licensee made some plant

modifications, including a modification to allow operation of the RN strainer backwash

outlet valves without reliance on VI, and took other measures to compensate for this

condition until full compliance with the design and licensing bases can be restored

through additional planned modifications. The licensee conducted a root cause

evaluation (RCE), as documented in Problem Investigation Process report (PIP) M-07-

4313, to identify weaknesses that existed in various organizations which allowed for a

risk-significant finding and to determine the organizational attributes that resulted in the

White finding. Subsequently, a number of events and additional reviews impacted the

corrective actions associated with the original RCE. During the February 13, 2008,

Enclosure

5

meeting of the Nuclear Safety Review Board (NSRB), the board challenged the depth of

the original extent of condition and extent of cause evaluations (PIP M-08-1574).

Testing of the backwash system on May 27, 2008, to evaluate a potential piping

modification revealed the system had inadequate pressure to provide RN strainer

backwash flow to the normal discharge path to the Condenser Circulating Water (RC)

system and that at high RN flow rates, a negative pressure was created in the strainers

making backwash discharge flow to the ground water (WZ) sump unavailable (PIP M-08-

3371). On April 27, 2009, during testing of the RN system at high flow rates, the

strainers became clogged with corrosion products from the suction piping which was a

new macro-fouling source not previously identified (PIP M-09-2216). All of these events

and reviews resulted in changes to or additions of corrective actions to the original RCE.

The licensee staff informed the NRC staff on January 11, 2010, that they were ready for

the supplemental inspection. From January 25, 2010, to February 4, 2010, in

preparation for this inspection, the licensee conducted an in-depth readiness review of

the original RCE report using the inspection attributes of IP 95001. As a result of that

self-critical readiness assessment, the licensee issued several additional PIPs and

added additional corrective actions to the original PIP M-07-4313.

The inspector reviewed the RCE associated with PIP M-07-4313, along with several

other evaluations that were conducted in support of or that impacted the corrective

actions for the root cause determination. The inspector reviewed the licensees extent of

condition and extent of cause evaluations to ensure they were sufficient in breadth. The

inspector reviewed the corrective actions that were taken or planned to address the

identified causes. The inspector also held discussions with licensee personnel to ensure

that the root and contributing causes, as well as the contribution of safety culture

components, were understood and that corrective actions taken or planned were

appropriate to address the causes and preclude repetition.

.02 Evaluation of the Inspection Requirements

02.01 Problem Identification

a. IP 95001 requires that the inspection staff determine that the licensees evaluation of the

issue documents who identified the issue (i.e., licensee-identified, self-revealing, or

NRC-identified) and the conditions under which the issue was identified.

The inspector determined that the event evaluations were sufficiently detailed to identify

who and under what conditions the issue was identified. The issue was identified on

August 6, 2007, by the licensee during the investigation of an abnormally high number of

RN strainer automatic backwashes (PIP M-07-4177).

b. IP 95001 requires that the inspection staff determine that the licensees evaluation of the

issue documents how long the issue existed and prior opportunities for identification.

The licensees root cause documented that the condition had existed since the

implementation of a modification that replaced the RN strainer backwash outlet manual

valves with air-operated valves on Unit 2 in 2000 (MM-8444) and on Unit 1 in 2001 (MM-

Enclosure

6

11224). However, subsequent testing in May 2008 revealed that there was no strainer

backwash discharge flow when aligned to the RC system and that strainer discharge

flow to the WZ sump was not possible at high RN flow rates (PIP M-08-3371). Based on

this information, the operability determination was revised, as were the interim and long

term actions to correct the condition. This additional time where backwash was

unavailable did not impact the NRCs significance determination of the condition since

no credit for strainer backwash was given and the duration used in the evaluation was

over a one year period.

The licensees root cause documented multiple missed opportunities to identify the

issue. Opportunities to recognize that manual backwash relied on non-safety related VI,

which could be unavailable following an accident, included the evaluation of the need to

upgrade the system to meet safety related requirements (PIP M-02-2427), design and

implementation of the modification that upgraded the system to meet safety related

requirements (MGMM-14403), evaluation of a variance to the modification to add the

ability to manually operate the strainer backwash outlet valves using an air supply

bypass valve, and revisions to the procedures to manually backwash the strainers.

The inspector determined that the licensees evaluation was adequate with respect to

identifying how long the issue existed and prior opportunities for identification.

c. IP 95001 requires that the inspection staff determine that the licensees evaluation of the

issue documents the plant-specific risk consequence, as applicable, and compliance

concerns associated with the issue.

The NRC determined this issue was a White finding, as documented in NRC IR

05000369,370/2008009. The root cause evaluation did not qualitatively assess the

increased risk associated with this condition, but the LER submitted by the licensee

(LER 05000369/2007-004) stated that based on a preliminary PRA evaluation, the

conditional core damage probability (CCDP) associated with this condition was greater

than 1E-6. At the Regulatory Conference held at the Region II offices on September 18,

2008, the licensee presented the results of their revised evaluation of CCDP as

approximately 4.7 E-7. However, the licensee did not contest the violation or its

categorization as having low to moderate safety significance.

The root cause evaluation appropriately documented the condition as a non-compliance

with their licensing bases and took appropriate compensatory actions, including plant

and procedural modifications to allow manual backwash without instrument air. Full

compliance will be restored when all corrective actions associated with this issue are

completed.

The inspector concluded that the licensee appropriately documented the risk

consequences and compliance concerns associated with the issue.

d. Findings

No findings of significance were identified.

Enclosure

7

02.02 Root Cause, Extent-of-Condition, and Extent-of-Cause Evaluation

a. IP 95001 requires that the inspection staff determine that the licensee evaluated the

issue using a systematic methodology to identify the root and contributing causes.

The licensee used the following systematic methods to complete PIP M-07-4313

problem evaluation:

  • data gathering through interviews and document review;
  • timeline construction;
  • events and causal factor charting; and
  • barrier analysis.

The inspector determined that the licensee evaluated the issue using a systematic

methodology to identify root and contributing causes.

b. IP 95001 requires that the inspection staff determine that the licensees RCE was

conducted to a level of detail commensurate with the significance of the issue.

The licensees RCE included an extensive timeline of events, as well as an event and

causal factors (E&CF) chart as discussed in the previous section. Using a

multidisciplinary team, the licensee identified a single root cause as changing the plant

configuration (i.e., manual valves on the RN strainer backwash outlet were replaced with

air-operated valves) without a total understanding of the design and licensing bases. In

addition, the RCE identified four contributing causes (CC) stemming from inappropriate

actions identified on the E&CF chart.

CC1: Design study conducted in 1990 to evaluate the RN strainer design bases

(MGDS-224) missed the UFSAR requirement for manual backwash following a

LOCA.

CC2: Modifications made in 1993-1994 that downgraded the strainer backwash function

to non-safety related (MGMM-3794) were completed without a 10 CFR 50.59

evaluation as an editorial minor modification.

CC3: An assessment completed in 1993 (SITA-93-01) on the operational readiness and

functionality of the RN system found issues with the system design including the

need for safety related instrumentation for strainer backwash initiation, but the PIP

that was generated had no evaluation and no corrective actions.

CC4: The corrective actions from PIP M-02-2427 generated in 2002 for engineering to

evaluate the safety classification of the RN strainers based on past strainer fouling

events, did not correct the condition. The resulting modification that upgraded the

strainer to safety related requirements (MMGM-14403) did not consider the ability

to manually backwash the strainers following a loss of VI.

Enclosure

8

The RCE did not fully document the organizational and programmatic weaknesses that

led to the condition, nor the reasons that multiple opportunities were missed for earlier

discovery. For example, the reason(s) why there was not a clear understanding of the

design bases of the system or why the design change/50.59 process failed to identify the

USFAR requirement for manual backwash were not fully explored. This was identified

by the licensee during their 95001 readiness review (M-SAG-SA-10-11) and PIP M-10-

1208 was initiated to evaluate the reasons why the design bases were not fully

understood. It concluded that the licensee did not know the UFSAR was the Current

Licensing Basis (CLB) source at the time of the modification and that the Design and

Licensing ownership had moved from the General Office to the site in the 1992 to 1996

timeframe.

Contributing to the apparent lack of detailed documentation of the causes of the event

was that the licensee did not revise the RCE when new information was discovered (M-

08-3371 and M-09-2261) or when additional review of the RCE was conducted. The

inspector identified that Nuclear System Directive (NSD) 212, Cause Analysis, indicated

that in the event further information becomes available that potentially affects the results

of a root cause evaluation, the root cause should be reevaluated to determine if a

revision was required. The operability determination was revised and numerous

corrective actions were added or revised, however the evaluation portion of the PIP was

not changed. This resulted in cases where the critical thinking on why a corrective

action was added was not documented and made the linkage between the root and

contributing causes and the associated CAs to address the causes difficult. Additionally,

the original RCE did not identify that the failure to conduct testing to ensure that the

backwash system functioned as designed was a contributor to this event. This was

identified in the corrective actions for PIP M-08-3371, but the original RCE was never

updated.

However, the inspector determined that the organizational and programmatic

weaknesses that caused this event, even if not specifically documented in the RCE,

were ultimately addressed in the corrective actions for this PIP and in other related PIPs.

For example, the corrective actions addressed weaknesses in the design bases

documentation (e.g., DBD and UFSAR), in the design change process, in the 50.59

process and in the knowledge and skills of engineering personnel and 10 CFR 50.59

qualified evaluators and screeners. Based on the results of the inspection, the licensee

initiated PIP M-10-1516 to evaluate the quality of root cause evaluations, including

determining the reasons PIP M-07-4313 did not apply the why staircase sufficiently to

determine what process weaknesses needed to be corrected and the reasons the RCE

was not revised when additional information was uncovered.

c. IP 95001 requires that the inspection staff determine that the licensees RCE include a

consideration of prior occurrences of the problem and knowledge of prior operating

experience.

The licensees RCE included a review of both internal and external operating experience

(OE). A search of the McGuire PIP database was conducted for previous events

assigned cause codes of F1b (Unplanned entry into TS LCO) and J1e (Risks and

Consequences associated with change not adequately reviewed). No previous events

Enclosure

9

were identified. However, these specific cause codes were not assigned to the root or

contributing causes for this evaluation. This was identified by the licensee in their IP

95001 readiness review (M-SAG-SA-10-11) and a subsequent search using the

appropriate codes did not identify any prior occurrences. Based on the licensees

evaluation and conclusions, the inspector determined that the licensees RCE included a

consideration of prior occurrences of the problem and knowledge of prior OE.

d. IP 95001 requires that the inspection staff determine that the licensees RCE addresses

the extent of condition and the extent of cause of the issue.

To address the extent of condition issue, the licensees RCE contained a review of air-

operated valves (AOVs) that receive safety signals that may need to be repositioned

from their safety position following an accident. Based on recommendations from the

McGuire NSRB meeting on February 13, 2008, additional corrective actions were added

to expand the scope of the AOVs that were reviewed and to include instrumentation that

is required post-accident that relied on instrument air (VI). No additional valves were

found that required VI post-accident and some procedure changes were made to identify

alternate indications that could be used for instrumentation that would be unavailable

following a loss of VI. During the IP 95001 readiness review a deficiency was identified

with the extent of condition. The team found that the extent of condition corrective

actions (CAs) should address motive forces other than air (e.g., power-operated

components) and other systems containing safety related/non-safety related interfaces

should be sampled and evaluated to ensure no similar issues with other safety related

systems exist (PIP M-10-1210). At the time of the inspection, the extent of condition

review of safety/non-safety system interactions was still in progress.

To address the extent of cause the RCE reviewed other areas where engineering may

not have a clear understanding of design bases prior to changing plant configuration.

Specifically, a corrective action was created to review the design basis document (DBD)

for the entire RN system and the Design Basis Accident DBD to ensure they adequately

reflect the current licensing basis. In addition, engineering personnel and 10 CFR 50.59

qualified personnel were trained on this event and on the use of licensing basis

documents during the design change process. During the IP 95001 readiness review a

deficiency was identified with the extent of cause. The team found that the extent of

cause CAs should be expanded to include the 10 CFR 50.59 process (program

changes, effectiveness reviews and examples) and the Engineering

Change/Engineering Change Approval process (program changes, effectiveness

reviews and examples) to ensure current processes would prevent similar events (PIP

M-10-1211). This PIP determined that recent 10 CFR 50.59 process changes provide

confidence in the current processes such that a similar failure of the program, as

documented under PIP M-07-4313, would not occur. Likewise, the current modification

process related toward editorial changes process provides sufficient barriers to prevent

design and implementation of a non-editorial modification under the editorial process. In

addition, PIP M-10-1240 was initiated to perform detailed design bases impact reviews

for historical modifications, which were deemed to have potentially similar attributes to

the historical modification which improperly downgraded RN strainer safety

classification. At the time of the inspection, this review was still in progress.

Enclosure

10

As stated earlier, the original RCE did not identify that the failure to conduct testing to

ensure that the backwash system functioned as designed was a contributor to this event.

However, this was identified following the discovery that backwash to the RC system

was not possible and that backwash to the WZ sump could not be performed at high RN

flow rates (PIP M-08-3371). Subsequently an extent of cause was conducted that

sampled several other safety systems to ensure that all safety functions have been

adequately functionally tested and/or monitored (PIP M-08-4602).

The inspector concluded that the licensee has ultimately addressed the extent of

condition and the extent of cause of the issue. However, weakness of the original extent

of condition and extent of cause evaluations resulted in delays in conducting a thorough

review, some aspects of which were still in progress at the time of the inspection.

e. IP 95001 requires that the inspection staff determine that the licensees root cause

evaluation, extent of condition, and extent of cause appropriately considered the safety

culture components as described in IMC 0305.

As part of the RCE, the licensee did not specifically consider the safety culture

components of IMC 0305, but did reference some safety culture components in their

cause determination. Specifically, CC3 was assigned a cause code of previous industry

or in-house operating experience was not effectively used to prevent problems (safety

culture component of operating experience) and CC4 was assigned a cause code of

corrective actions from previously identified problems or previous event causes were

not adequate to prevent recurrence (safety culture component of problem identification

and resolution). The failure to consider safety culture components in the RCE was

recognized by the IP 95001 readiness review team (M-SAG-SA-10-11). A corrective

action was created in PIP M-07-4313 to conduct an assessment of the safety culture

components and a corrective action to PIP M-10-1205 was created for the Safety

Assurance/Performance Improvement (SA/PI) Manager to review the current processes

and McGuire site understanding of requirements for considering safety culture

components. The safety culture component evaluation that was conducted as a result of

the readiness review team recommendation concluded that there were no aspects of the

RCE that would indicate that the organizations or individuals involved exhibited behavior

indicative of a weakness in safety culture, even though the cause codes assigned to two

of the contributing causes directly relate to safety culture components. This further

demonstrated the lack of specific guidance on considering safety culture components

during root cause evaluations.

Based on the results of the inspection, the licensee initiated PIP M-10-1516 to evaluate

the quality of root cause evaluations, including addressing the lack of guidance on

considering safety culture components during root cause evaluations.

f. Findings

No findings of significance were identified.

Enclosure

11

02.03 Corrective Actions

a. IP 95001 requires that the inspection staff determine that: (1) the licensee specified

appropriate corrective actions for each root and/or contributing cause; or (2) an

evaluation that states no actions are necessary is adequate.

The root cause and contributing causes 1 and 2 were linked to corrective actions.

However contributing causes 3 and 4 were not linked to specific corrective actions. This

was identified in the IP 95001 readiness review and PIP M-10-1214 was initiated to

correct this oversight.

The inspector reviewed the corrective actions taken for PIP M-07-4313 and determined

that, although not well linked, adequate corrective actions have been or will be taken to

address the causes of this condition.

b. IP 95001 requires that the inspection staff determine that the licensee prioritized

corrective actions with consideration of risk significance and regulatory compliance.

The licensee took immediate corrective actions to compensate for the inability to

manually backwash the RN strainers following a loss of instrument air by modifying the

strainer backwash outlet valves to provide a manual means to open the valves without

relying on VI. These compensatory actions and associated operability determination

were later modified following the discovery that backwash flow path to the RC system

was unavailable and that a negative pressure was created in the strainer during high RN

flow rates (PIP M-08-3717). This led to procedure changes that provided guidance on

aligning strainer backwash flow, if needed, to the WZ sump only and to throttle RN flow

to the Component Cooling Water (KC) heat exchangers if strainer pressure was

inadequate for sump discharge. These compensatory actions and the associated

operability determination were modified again following the discovery of additional

macro-fouling sources (PIP M-09-2216). On November 6, 2009, the NRC requested the

licensee provide an explanation addressing what compensatory or other measures were

in place to assure the operability of the RN system in case strainer macro-fouling does

occur until full compliance is restored. In their response dated December 7, 2009, the

licensee stated that a dedicated operator was stationed to perform time-critical actions to

initiate backwash supply flow to the strainers on a loss of instrument air and listed

several modifications and procedural changes that have been made. The response only

addressed macro-fouling from soft debris that could be crushed in the strainer and

passed through the system and did not reference the procedure to align backwash outlet

flow to the WZ sump or the potential need to throttle RN flow to the KC heat exchangers

to achieve adequate strainer pressure for backwash operation. The licensee committed

to supplement their December 7, 2009 response by April 12, 2010, to more completely

describe their interim compensatory measures, including those that would mitigate all

design basis type macro-fouling mechanisms that could impact the RN system during

design basis events.

These events also impacted the corrective actions needed to restore the system to full

compliance. The licensee determined that the preferred approach to restore compliance

would be to implement a series of modifications including installation of safety related

Enclosure

12

strainer backwash discharge pumps to provide the motive force to direct backwash flow

to the RN return header. In a letter dated October 1, 2009, the licensee changed their

original commitment of submitting a license amendment to resolve the NOV, to

completing these modifications by December 2012. On November 6, 2009, the NRC

requested the licensee provide a discussion on why the proposed completion date

represented the first available opportunity to restore compliance. In their response dated

December 7, 2009, the licensee provided the justification for the proposed durations for

modification implementation. The inspector reviewed the reasons provided for the

projected completion dates for the modifications and found them to be reasonable given

the magnitude of the modifications.

The corrective action to prevent recurrence for the root cause was to revise the DBD for

the RN system. This action was appropriately prioritized and has been completed.

Based upon the appropriate prioritization of the DBD revision and the review of the

implementation schedule for the modifications needed to restore full compliance of the

system, the inspector determined that the corrective actions were prioritized with

consideration of the risk significance and regulatory compliance.

c. IP 95001 requires that the inspection staff determine that the licensee established a

schedule for implementing and completing the corrective actions.

The inspector determined that all of the corrective actions listed in the RCE have been

either scheduled or completed and that the schedule was consistent with the licensees

commitments made to resolve the violation as clarified in their December 7, 2009

response for additional information.

d. IP 95001 requires that the inspection staff determine that the licensee developed

quantitative and qualitative measures of success for determining the effectiveness of the

corrective actions to preclude repetition.

As documented in PIP M-07-4313, the licensee established measures for determining

the effectiveness of the corrective actions. These measures included the following:

  • Conduct an independent review of the RN DBD to ensure that it clearly provides

design and licensing bases of the RN Strainer and meets the actual design; and

  • Perform an effective review six to nine months following completion of the

modifications to RN strainer backwash system using the effectiveness review

template.

The licensees corrective action program only requires effectiveness reviews to be

conducted on corrective actions to prevent recurrence (CAPR) and does not provide

explicit guidance on how to conduct the reviews. The licensee uses a template posted

on their performance improvement website as guidance for these reviews. It consists of

a series of five questions: 1) Have the CAPR(s) been properly implemented; 2) Were

CAPR(s) implemented per the latest approved schedule; 3) Have the CAPR(s) been

challenged adequately; 4) Were the CAPR(s) successful in preventing recurrence; and

5) Have the CAPR(s) prevented the same or similar events?

Enclosure

13

The independent review of the revised DBD merely verifies that the action was

completed adequately and does not evaluate whether the revision prevented recurrence

of improper design changes. The effectiveness of the modifications to restore

compliance will be demonstrated during the post-modification testing. The action was

initiated to correct the condition, not to prevent recurrence for the causes of the event.

Since no other actions were designated as CAPRs, no additional reviews of

effectiveness to prevent recurrence are required by the CAP process. This was

recognized by the IP 95001 readiness review team (M-SAG-SA-10-11). A corrective

action on PIP M-10-1205 was created for the SA/PI Manager to review the current

processes and McGuire site understanding of requirements for evaluating CAPR

effectiveness.

e. IP 95001 requires that the inspection staff determine that the licensees planned or taken

corrective actions adequately address a Notice of Violation (NOV) that was the basis for

the supplemental inspection, if applicable.

The NRC issued the NOV to the licensee on October 27, 2008. The licensee provided

the NRC a written response to the NOV on November 25, 2008. The licensees

response described: 1) the reasons for the violation; 2) corrective steps which have

been taken and the results achieved; 3) corrective steps which will be taken to avoid

further violations; and 4) the date when full compliance will be achieved. However, the

licensee revised their commitments contained in the response to the NOV in a letter

dated October 1, 2009. The licensee had originally planned to submit a license

amendment to request that the NRC accept the non-conforming condition as is, however

following a detailed review the licensee determined a preferred approach would be to

implement plant changes to bring the system into full compliance. These changes will

be implemented in three phases. Phase 1 will add an assured air supply to the strainer

backwash inlet valves. Phase 2 will improve the piping layout from the strainer

backwash outlets to the WZ sump to reduce head loss when conducting backwash

operation to the sump. Phase 3 will install safety related strainer backwash discharge

pumps to provide the motive force to discharge backwash effluent to the RN return

header and will remove the air-operated strainer backwash outlet valves.

During this inspection, the inspector reviewed the preliminary designs for these

modifications and associated calculations. The inspector determined that when Phase 1

and 3 are completed the system will be restored to full compliance and that the

licensees planned and taken corrective actions addressed the NOV. However, the

inspector was unable to determine if the Phase 2 modification would be acceptable due

to incomplete design and associated calculations; and the potential reliance on throttling

RN flow to achieve the necessary strainer pressure for backwash operations to the WZ

sump. Since these corrective actions have not been completed, the implementation and

effectiveness of the licensees corrective actions will be reviewed during future

inspections.

f. Findings

No findings of significance were identified.

Enclosure

14

4OA6 Exit Meeting

On March 9, 2010, the inspector presented the results of the supplemental inspection to

Mr. Steven D. Capps and other members of licensee management and staff. The

inspector confirmed that no proprietary information was provided or examined during the

inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. Abbott, Regulatory Compliance Engineer

K. Ashe, Regulatory Compliance Manager

D. Brewer, Safety Assurance Manager

M. Broome, Electrical and I&C Engineer

S. Capps, Station Manager

K. Crane, Regulatory Compliance Engineer

C. Curry, Engineering Manager

R. Harris, Modifications Engineer

G. Holbrooks, Project Management

S. Heuertz, Performance Improvement Team

S. Karriker, Balance of Plant Engineering Supervisor

G. Kent, Duke Energy Regulatory Compliance Engineer

M. Leisure, Regulatory Compliance Engineer

W. Leggette, Nuclear Operations Support

J. Nolin, Mechanical and Civil Engineering Manager

R. Pacetti, Performance Improvement Team Manager

T. Pederson, RN System Engineer

R. Repko, Site Vice President

F. Twogood, Engineering Consultant

R. Weathers, RN System Engineer

M. Weiner, Nuclear Operations Support

NRC Personnel

J. Brady, Senior Resident Inspector - McGuire

J. Bartley, Chief, Reactor Projects Branch 1

ITEMS OPENED, CLOSED AND DISCUSSED

Closed

05000369,370/2008009-01 VIO Failure to Take Adequate Corrective Action

for Implementation of Safety-Related RN

Strainer Backwash (Section 4OA4)

LIST OF DOCUMENTS REVIEWED

Procedures

AP/1/A/5500/22, Loss of VI Abnormal Procedure, Rev. 28

AP/2/A/5500/22, Loss of VI Abnormal Procedure, Rev. 25

OP/1/A/6400/006, Nuclear Service Water System, Rev. 180

OP/2/A/6400/006, Nuclear Service Water System, Rev. 136

OP/1/A/6100/010 M, Annunciator Response for Panel 1 AD-12, Rev. 47

Attachment

2

OP/2/A/6100/010 M, Annunciator Response for Panel 2 AD-12, Rev. 31

RP/0/A/5700/006, Natural Disaster, Rev. 22

EDM-601, Engineering Change, Rev. 10

NSD 201, Reporting Requirements, Rev. 21

NSD 202, Reportability, Rev. 21

NSD 203, Operability/Functionality, Rev. 21

NSD 208, Problem Investigation Process (PIP), Rev. 31

NSD 209, 10CFR 50.59 Process, Rev. 14

NSD-212, Cause Analysis, Rev. 16

NSD-228, Applicability Determination, Rev. 5

NSD-301, Engineering Change Process, Rev. 34

PIPs

M-89-0290, Design Engineering Evaluate Safety Classification of RN Strainers

M-93-0297, Viability of RN Strainers

M-00-3122, RN strainer backwash valve modification MGMM8444 does not incorporate

adequate provisions for Operations to perform manual strainer backwash

M-02-2427, Re-evaluation of RN Strainer Filtration Function (Safety or Non-Safety Related)

M-07-4177, 1B and 2B RN strainer experienced numerous Hi D/P backwashes

M-07-4313, Inability to manually backwash RN strainers during post-accident conditions

M-07-5978, Evaluate Compliance with Design Basis for RN Strainer Backwash System Utilizing

Non-Safety Related Equipment

M-08-1574, McGuire NSRB Meeting Minutes from February 13, 2008

M-08-3371, RN Strainer Backwash Return Flow Direction is from RC (Lake) to the Strainer

Instead of from the Strainer to RC (Lake)

M-08-3668, Assess Functionality of Groundwater Level Monitoring System Based on RN

Strainer Backwash Flow to WZ Sump

M-08-4602, Engineering Management Discussion on Extent of Condition M-08-3371 Problem

Evaluation

M-08-4911, NRC Issuance of a Preliminary Greater then Green Finding

M-08-7507, NRC Issuance of Violation (VIO) 08-09-01

M-09-2216, 2A RN Strainer Fouled During High RN Flow Testing per TT Procedure

M-09-2341, During Loss of Instrument Air (VI) Events, RN A Train Pump Flow May Self-Limit

Based on Suction Pressure Limits When Aligned to the SNSWP

M-10-1145, engineering Review of SITA 93-01 Audit

M-10-1205, Assessment M-SAG-SA-10-11: NRC IP 95001 Supplemental Inspection Readiness

Review - RN System White Finding.

M-10-1208, Assessment M-SAG-SA-10-11 Deficiency #1 (M-07-4313 Root Cause Evaluation

lacks development)

M-10-1209, Assessment M-SAG-SA-10-11 Deficiency #2 (No evaluation was performed to

reconcile the difference between the M-07-4313 Root Cause and the NRC NOV EA-08-220)

M-10-1210, Assessment M-SAG-SA-10-11 Deficiency #3 (M-07-4313 Root Cause Extent of

Condition evaluation and corrective actions are fragmented and inadequate)

M-10-1211, Assessment M-SAG-SA-10-11 Deficiency #4 (M-07-4313 Extent of Cause

evaluation corrective actions are inadequate and not all-encompassing)

Attachment

3

M-10-1212, Assessment M-SAG-SA-10-11 Deficiency #5 (M-07-4313 Root Cause is not

adequately addressed by the CAPRs)

M-10-1214, Assessment M-SAG-SA-10-11 Deficiency #6 (There are no CAs for M-07-4313

Root Cause Evaluation Contributing Cause 3 (CC-3) or Contributing Cause 4 (CC-4))

M-10-1217, Assessment M-SAG-SA-10-11 Deficiency #7 (several situations noted in PIP M-07-

4313 wherein the individual performing the corrective action and the approver were the

same person)

M-10-1240, Perform Detailed Design Bases Impact Review for Historical Modifications Similar

to Modification to Downgrade RN Strainer Safety Classification

Miscellaneous

MCS-1465.00-00-0004, Design Basis Specification for Loss of VI, Rev. 1

MCS-1465.00-00-0005, Design Basis Specification for Design Events, Rev. 4

MCS-1574.RN-00-0001, Design Basis Specification for Nuclear Service Water (RN) System,

Rev. 28

MCS-1581.WZ-00-0001, Design Basis Specification for the WZ System, Rev. 9

MGDS-224, McGuire Design Study to Document the Design Basis for the RN Pump Strainer,

7/11/1990

M-SAG-SA-10-11, NRC IP 95001 Supplemental Inspection Readiness Review-RN System

White Finding

SITA-93-01, operational readiness and functionality of McGuires Nuclear Service Water (RN)

System

Licensee Event Report (LER) 05000369/2007-004-00, Procedure Deficiency identified for

Performing a Manual Backwash of Nuclear Service Water (RN) Strainers due to Reliance on

Non-Safety Instrument Air

UFSAR Section 9.2.2, Nuclear Service Water System and Ultimate Heat Sink

TS 3.7.7, Nuclear Service Water System (NSWS), Amendment Nos. 184/166, & Bases B3.7.7,

Rev. 0

A/R 00302781, 10CFR50.59 Screen for Modifications to Add Safety Related Air Supply to the

RN Strainer Backwash Inlet valves

A/R 00302920, 10CFR50.59 Screen for Modifications to Reroute the Backwash Effluent Line to

the Auxiliary Building Groundwater Sump (WZ)

A/R 00302925, 10CFR50.59 Screen for Modifications to Incorporate New Pressure Transmitters

and New Backwash Discharge Pumps

A/R 00302927, 10CFR50.59 Evaluation for Modifications to Incorporate New Pressure

Transmitters and New Backwash Discharge Pumps

A/R 00303967, 10CFR50.59 Screen for Modifications to Incorporate New Pressure

Transmitters and New Backwash Discharge Pumps

A/R 00303869, 10CFR50.59 Evaluation for Modifications to Incorporate New Pressure

Transmitters and New Backwash Discharge Pumps

A/R 00304335, 10CFR50.59 Screen for OP/1(2)/A/6400/006, Nuclear Service Water Revisions

202/158

A/R 00304336, 10CFR50.59 Screen for OP/1(2)/A/6400/006, Nuclear Service Water Revisions

203/159

OMP 12-1, Dedicated RN Strainer Backwash Operator is Required, Rev. 2 dated 5/6/2009

SOMP 01-13, Designated RN Back-Flush Operator for Loss of VI, Rev. 1 dated 6/22/2009

Attachment

4

Modifications

MGMM-3794, Editorial Minor Modification to Allow Downgrade of the function of the RN

Strainers, 8/12/1993

MGMM-8444, Install New ITT Diaphragm valves at Outlet of RN Strainers on Unit 2, 4/18/2001

MGMM-11224, Install New ITT Diaphragm valves at Outlet of RN Strainers on Unit 1, 9/7/2001

MGMM-14403, Reclassify RN Strainers as QA-1 due to Recent Macro-Fouling Events,

8/11/2003

MD101360, Temporary Modification to Install Ball Thrust Bearing on 1RN0022A and Mechanical

Gag on 1RN0023, 8/8/2007

MD101361, Temporary Modification to Install Ball Thrust Bearing on 1RN0026B and Mechanical

Gag on 1RN0027, 8/8/2007

MD201362, Temporary Modification to Install Ball Thrust Bearing on 2RN0022A and Mechanical

Gag on 2RN0023, 8/8/2007

MD201363, Temporary Modification to Install Ball Thrust Bearing on 2RN0026A and Mechanical

Gag on 2RN0027, 8/8/2007

MD102035, Permanently Install Ball Thrust Bearing on 1RN0022A/26B and Remove

Mechanical Gag on 1RN0023/27, 11/5/2008

MD202037, Permanently Install Ball Thrust Bearing on 1RN0022A/26B and Remove

Mechanical Gag on 1RN0023/27, 11/5/2008

MD501561 - LLI macrofouling barrier

MD101813 - RN Strainer 1A Backwash Instrumentation

MD101624 - RN Strainer 1B Backwash Instrumentation

MD201814 - RN Strainer 2A Backwash Instrumentation

MD201629 - RN Strainer 2B Backwash Instrumentation

EC 101543, Installation of an Assured Air Supply for 1-RN-21A

EC 101545, Installation of an Assured Air Supply for 1-RN-25B

EC 101544, Installation of an Assured Air Supply for 2-RN-21A

EC 101546, Installation of an Assured Air Supply for 2-RN-25B

EC 101547, Improved Piping Layout for Manual Strainer Backwash from 1A RN Strainer to WZ

Sump

EC 101549, Improved Piping Layout for Manual Strainer Backwash from 1B RN Strainer to WZ

Sump

EC 101548, Improved Piping Layout for Manual Strainer Backwash from 2A RN Strainer to WZ

Sump

EC 101550, Improved Piping Layout for Manual Strainer Backwash from 2B RN Strainer to WZ

Sump

EC 102477, Installation of RN Strainer Backwash Discharge Pump for 1A RN Strainer

EC 102478, Installation of RN Strainer Backwash Discharge Pump for 1B RN Strainer

EC 102479, Installation of RN Strainer Backwash Discharge Pump for 2A RN Strainer

EC 102482, Installation of RN Strainer Backwash Discharge Pump for 2B RN Strainer

ECR 2081, Provide Remote Throttling Capability to Unit 1 KC HX Supply Isolation Valves

ECR 2087, Provide Remote Throttling Capability to Unit 2 KC HX Supply Isolation Valves

Attachment

5

Calculations

MCC-1223.24-00-00P1, Mechanical/ Civil Design Inputs for Assured Air Supply for Strainer

Backwash Valves, Rev. 0

MCC-1223.24-00-00P2, Mechanical/ Civil Design Inputs for Piping Layoout for Manual Strainer

Backwash, Rev. 0

MCC-1223.24-00-00P3, Mechanical/ Civil Design Inputs for RN Strainer Backwash Discharge

Pumps, Rev. 0

MCC-1223.24-00-0096, RN System Flow Balance Acceptance Criteria Calculation, Rev. 4

MCC-1223.24-00-0100, FMEA of RN Strainer Modifications MD101813, MD101624,

MD201814, and MD201629, Rev. 1

MCC-1223.24-00-0102, RN Pump NPSH Calculation, Rev. 3

MCC-1223.24-00-0103, RN Strainer Macrofouling Source Calculation, Rev. 3

MCC-1223.24-00-0107, FMEA of RN Strainer Backwash Discharge Modifications, Rev. 3

MCC-1223.31-00-0010, Groundwater Drainage System Flow Analysis, Rev. 3

MCC-1331.16-00-0410, Electrical Discipline Design Inputs for EC 101543, EC 101544, EC 101545, EC 101546, Rev. 0

MCC-1331.16-00-0411, Electrical Discipline Design Inputs for EC 102477, EC 102478, EC 102479, EC 102482, Rev. 1

PIPs generated as a result of this inspection

PIP M-10-1429, NRC Inspector Questioned Basis and Conclusion of the Applicability

Determination for Procedure Change That Allowed Throttling of KC Flow

PIP M-10-1430, NRC Inspector Questioned Classification of Strainer Backwash as a Functional

Failure

PIP M-10-1448, NRC 95001 Supplemental Inspection Items to be Resolved

PIP M-10-1516, Evaluate the Quality of Root Cause Evaluations and Associated Process

Guidance Based on NRC 95001 Supplemental Inspection Results

Attachment