Information Notice 2010-21, Crack-Like Indication in the U-bend Region of a Thermally Treated Alloy 600 Steam Generator Tube: Difference between revisions

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{{#Wiki_filter:ML102210244 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF NUCLEAR REACTOR REGULATION WASHINGTON, DC 20555-0001 October 6, 2010  
{{#Wiki_filter:UNITED STATES
  NRC INFORMATION NOTICE 2010-21: CRACK-LIKE INDICATION IN THE U-BEND REGION OF A THERMALLY TREATED ALLOY 600 STEAM GENERATOR TUBE
 
NUCLEAR REGULATORY COMMISSION
 
OFFICE OF NUCLEAR REACTOR REGULATION
 
WASHINGTON, DC 20555-0001 October 6, 2010
NRC INFORMATION NOTICE 2010-21:               CRACK-LIKE INDICATION IN THE U-BEND
 
REGION OF A THERMALLY TREATED
 
ALLOY 600 STEAM GENERATOR TUBE


==ADDRESSEES==
==ADDRESSEES==
All holders of an operating license or construction permit for a nuclear power reactor issued under Title 10 of the Code of Federal Regulations, Part 50, "Domestic Licensing of Production and Utilization Facilities," except those who have permanently ceased operations and have certified that fuel has been permanently removed from the reactor vessel.
All holders of an operating license or construction permit for a nuclear power reactor issued
 
under Title 10 of the Code of Federal Regulations, Part 50, Domestic Licensing of Production
 
and Utilization Facilities, except those who have permanently ceased operations and have
 
certified that fuel has been permanently removed from the reactor vessel.


==PURPOSE==
==PURPOSE==
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform addressees of recent operating experience with the detection of a crack-like indication in the
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform


U-bend region of a thermally treated Alloy 600 steam generator tube. The NRC expects that recipients will review the information for applicability to their facilities and consider actions, as appropriate, to avoid similar problems. Suggestions contained in this IN are not NRC requirements; therefore, no specific action or written response is required.
addressees of recent operating experience with the detection of a crack-like indication in the
 
U-bend region of a thermally treated Alloy 600 steam generator tube. The NRC expects that
 
recipients will review the information for applicability to their facilities and consider actions, as
 
appropriate, to avoid similar problems. Suggestions contained in this IN are not NRC
 
requirements; therefore, no specific action or written response is required.


==DESCRIPTION OF CIRCUMSTANCES==
==DESCRIPTION OF CIRCUMSTANCES==
Vogtle Electric Generating Plant (Vogtle), Unit 1, has four Westinghouse Model F steam generators. Each steam generator has 5,626 tubes fabricated from thermally treated Alloy 600. The tubes have a nominal outside diameter of 0.688 inch and a nominal wall thickness of
Vogtle Electric Generating Plant (Vogtle), Unit 1, has four Westinghouse Model F steam
 
generators. Each steam generator has 5,626 tubes fabricated from thermally treated Alloy 600.
 
The tubes have a nominal outside diameter of 0.688 inch and a nominal wall thickness of
 
0.040 inch. Following the bending of the tubes, the U-bend region of the tubes installed in the
 
first 10 rows of the steam generator was thermally stress-relieved at approximately
 
1,320 degrees Fahrenheit (715 degrees Celsius) for 2 hours to relieve the residual stresses
 
induced by bending. The radius of a Row 1 U-bend is 2.20 inches. The tubes are arranged in a
 
square pattern, and the centers of the adjacent tubes are 0.98 inch apart.
 
When Vogtle, Unit 1 was shut down for the 2009 outage, the unit had operated for
 
approximately 19.8 effective full-power years. The hot leg temperature is approximately
 
618 degrees Fahrenheit (326 degrees Celsius).


0.040 inch.  Following the bending of the tubes, the U-bend region of the tubes installed in the first 10 rows of the steam generator was thermally stress-relieved at approximately 1,320 degrees Fahrenheit (715 degrees Celsius) for 2 hours to relieve the residual stresses induced by bending.  The radius of a Row 1 U-bend is 2.20 inches.  The tubes are arranged in a square pattern, and the centers of the adjacent tubes are 0.98 inch apart.
During the cycle before the 2009 refueling outage, no primary-to-secondary leakage was


When Vogtle, Unit 1 was shut down for the 2009 outage, the unit had operated for approximately 19.8 effective full-power years.  The hot leg temperature is approximately 618 degrees Fahrenheit (326 degrees Celsius).
observed at Vogtle, Unit 1; however, while the unit was being shut down, there were a few


During the cycle before the 2009 refueling outage, no primary-to-secondary leakage was observed at Vogtle, Unit 1; however, while the unit was being shut down, there were a few
radiation monitor alarms, indicating the presence of activity on the secondary side of the unit.


radiation monitor alarms, indicating the presence of activity on the secondary side of the unit.  The leak rate was too small to measure. With the static pressure from the water on the secondary side of the steam generator acting on the tubes, there was no visible evidence of leakage coming from any of the tubes. For this refueling outage, the licensee planned to use an eddy current rotating probe equipped with a +Point
The leak rate was too small to measure. With the static pressure from the water on the


TM coil to inspect the U-bend region of approximately 50 percent of the tubes in Rows 1 and 2 in each of the four steam generators.  During these rotating probe examinations, the licensee found an axially oriented crack-like indication approximately 3 inches above the uppermost hot-leg tube support plate (i.e., the seventh support plate) in the tube in Row 1, Column 20 (R1C20), in Steam Generator 3.  The crack-like indication was close to the apex of the tube on the extrados and was attributed to primary water stress-corrosion cracking.  The
secondary side of the steam generator acting on the tubes, there was no visible evidence of


voltage amplitude of the indication, as measured with the midrange +PointTM coil, operated at 300 kilohertz (kHz) was 3.09 volts.  The axial length of the indication was 0.54 inch, its maximum depth was 100 percent through-wall, and it exceeded 80 percent through-wall over 0.40 inch of its length.
leakage coming from any of the tubes.


As a result of detecting this indication, the rotating probe examinations in the U-bend region were expanded to include 100 percent of the Row 1 and 2 tubes in each of the four steam
For this refueling outage, the licensee planned to use an eddy current rotating probe equipped


generators and 20 percent of Row 3 tubes in Steam Generator 3. No other crack-like indications were found in the U-bend region during these examinations. The licensee plugged the tube in R1C20 in Steam Generator 3.
with a +PointTM coil to inspect the U-bend region of approximately 50 percent of the tubes in
 
Rows 1 and 2 in each of the four steam generators. During these rotating probe examinations, the licensee found an axially oriented crack-like indication approximately 3 inches above the
 
uppermost hot-leg tube support plate (i.e., the seventh support plate) in the tube in Row 1, Column 20 (R1C20), in Steam Generator 3. The crack-like indication was close to the apex of
 
the tube on the extrados and was attributed to primary water stress-corrosion cracking. The
 
voltage amplitude of the indication, as measured with the midrange +PointTM coil, operated at
 
300 kilohertz (kHz) was 3.09 volts. The axial length of the indication was 0.54 inch, its
 
maximum depth was 100 percent through-wall, and it exceeded 80 percent through-wall over
 
0.40 inch of its length.
 
As a result of detecting this indication, the rotating probe examinations in the U-bend region
 
were expanded to include 100 percent of the Row 1 and 2 tubes in each of the four steam
 
generators and 20 percent of Row 3 tubes in Steam Generator 3. No other crack-like
 
indications were found in the U-bend region during these examinations. The licensee plugged
 
the tube in R1C20 in Steam Generator 3.


The U-bend region of the tube in R1C20 in Steam Generator 3 was inspected in prior outages.
The U-bend region of the tube in R1C20 in Steam Generator 3 was inspected in prior outages.


The U-bend region was inspected with a bobbin coil in 1986 (baseline inspection), 1991, 1993, 1997, and 2000. A rotating probe examination of the U-bend region of this tube was also performed in 1997, 2003, and 2009. The practice of inspecting the U-bend region of tubes in low rows (e.g., Rows 1 and 2) with only a rotating probe (and not with a bobbin probe) is a fairly common practice today, given the difficulties in performing quality inspections of tight radius
The U-bend region was inspected with a bobbin coil in 1986 (baseline inspection), 1991, 1993,
1997, and 2000. A rotating probe examination of the U-bend region of this tube was also
 
performed in 1997, 2003, and 2009. The practice of inspecting the U-bend region of tubes in
 
low rows (e.g., Rows 1 and 2) with only a rotating probe (and not with a bobbin probe) is a fairly
 
common practice today, given the difficulties in performing quality inspections of tight radius


U-bends with a bobbin probe.
U-bends with a bobbin probe.


The prior inspections of this tube indicated the presence of a manufacturing indication, referred to as a Blairsville bump (because the bump was most likely introduced during bending of the tube at a facility in Blairsville, PA).  This bump is located at the start of the bent region of the
The prior inspections of this tube indicated the presence of a manufacturing indication, referred


tube (i.e., the start of the U-bend region).  During the review of the bobbin coil data obtained in 2000, one of the analysts reviewing the data (typically two analysts review all eddy current data) identified a nonquantifiable indication at the location where the crack-like indication was eventually discovered.  This indication was eventually dismissed by the resolution analyst (an analyst who oversees the review of the primary and secondary data analysts) because the 1997 rotating probe examination indicated that no flaws were present at this location, the bobbin coil data indicated that the signal had not changed since the 1986 inspection, and there was a general absence of any cracking in tubes fabricated from thermally treated Alloy 600 tubing at the time of the inspection.  During the review of the 2003 rotating probe data, an axial indication was reported by one of the analysts at the location where the crack-like indication was eventually discovered.  This indication was also dismissed by the resolution analyst because the indication from the rotating probe did not change appreciably from 1997 (1.75 volts as
to as a Blairsville bump (because the bump was most likely introduced during bending of the


measured from the 300-kHz channel) to 2003 (1.83 volts as measured from the 300-kHz channel).
tube at a facility in Blairsville, PA). This bump is located at the start of the bent region of the


The tube in R1C20 in Steam Generator 3 was pressure-tested in situ in 2009 to confirm its integrity. During the test, no leakage was observed under simulated normal operating conditions, approximately 0.002 gallons per minute was observed under simulated steamline break conditions, and approximately 0.09 gallons per minute was observed at three times the normal operating differential pressure.  The tube did not burst at three times the normal
tube (i.e., the start of the U-bend region). During the review of the bobbin coil data obtained in


operating differential pressure, demonstrating that it retained adequate structural integrity. The leak rate from this tube under accident conditions, when combined with all other sources of accident-induced leakage, was within acceptance limits, demonstrating that the steam generator had satisfied the accident-induced leakage performance criteria.
2000, one of the analysts reviewing the data (typically two analysts review all eddy current data)
identified a nonquantifiable indication at the location where the crack-like indication was
 
eventually discovered. This indication was eventually dismissed by the resolution analyst (an
 
analyst who oversees the review of the primary and secondary data analysts) because the 1997 rotating probe examination indicated that no flaws were present at this location, the bobbin coil
 
data indicated that the signal had not changed since the 1986 inspection, and there was a
 
general absence of any cracking in tubes fabricated from thermally treated Alloy 600 tubing at
 
the time of the inspection. During the review of the 2003 rotating probe data, an axial indication
 
was reported by one of the analysts at the location where the crack-like indication was
 
eventually discovered. This indication was also dismissed by the resolution analyst because the
 
indication from the rotating probe did not change appreciably from 1997 (1.75 volts as
 
measured from the 300-kHz channel) to 2003 (1.83 volts as measured from the 300-kHz
 
channel).
 
The tube in R1C20 in Steam Generator 3 was pressure-tested in situ in 2009 to confirm its
 
integrity. During the test, no leakage was observed under simulated normal operating conditions, approximately 0.002 gallons per minute was observed under simulated steamline
 
break conditions, and approximately 0.09 gallons per minute was observed at three times the
 
normal operating differential pressure. The tube did not burst at three times the normal
 
operating differential pressure, demonstrating that it retained adequate structural integrity. The
 
leak rate from this tube under accident conditions, when combined with all other sources of
 
accident-induced leakage, was within acceptance limits, demonstrating that the steam generator
 
had satisfied the accident-induced leakage performance criteria.


==BACKGROUND==
==BACKGROUND==
Previous related generic communications include the following:  
Previous related generic communications include the following:
*        NRC IN 2003-13, Steam Generator Tube Degradation at Diablo Canyon, dated


* NRC IN 2003-13, "Steam Generator Tube Degradation at Diablo Canyon," dated August 28, 2003 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML032410215)  
August 28, 2003 (Agencywide Documents Access and Management System (ADAMS)
        Accession No. ML032410215)
*        NRC IN 97-26, Degradation in Small-Radius U-Bend Regions of Steam Generator


* NRC IN 97-26, "Degradation in Small-Radius U-Bend Regions of Steam Generator Tubes," dated May 19, 1997 (ADAMS Accession No. ML031060007)  
Tubes, dated May 19, 1997 (ADAMS Accession No. ML031060007)


==DISCUSSION==
==DISCUSSION==
Cracking in the U-bend region of steam generator tubes has been observed for years. Many of these cracks have been located in the U-bends of tubes in Rows 1 and 2 as discussed in NRC IN 97-26; however, there have been some cracks in the U-bends of higher row tubes as
Cracking in the U-bend region of steam generator tubes has been observed for years. Many of


discussed in NRC IN 2003-13.  All of these cracks have been in tubes made with mill-annealed Alloy 600 tubing.  (Note:  Although NRC IN 97-26 indicates that an axial indication was discovered in the U-bend region of a thermally treated Alloy 600 tube at Braidwood Station, Unit 2, subsequent evaluation indicated that this indication was not a crack).
these cracks have been located in the U-bends of tubes in Rows 1 and 2 as discussed in NRC


The findings at Vogtle, Unit 1 are particularly noteworthy because this is the first confirmed instance of cracking in the U-bend region of a thermally treated Alloy 600 tube.  Although there was a manufacturing indication near the location where the crack developed, it is not known whether this condition is necessary to lead to the initiation of a crack in this region of the tubing.  In addition, although the crack at Vogtle, Unit 1 occurred in the U-bend region of a Row 1 tube, it is not clear that this phenomenon would be primarily limited to low-row (i.e., Rows 1 and 2) tubes as it primarily was for units with mill-annealed Alloy 600 steam generator tubing.  In the units with mill-annealed Alloy 600 tubing, the U-bends were typically not stress relieved after bending.  As a result, the residual stresses; and therefore, the susceptibility to cracking, would normally be expected to be highest in the lowest row tube (i.e., the one with the shortest bend
IN 97-26; however, there have been some cracks in the U-bends of higher row tubes as


radius), provided there were no significant changes in the bending processes from one tube row to another.  However, in the case of the units with thermally treated Alloy 600 tubing, the U-bends of the low-row tubes (i.e., Rows 1 through 8, 9, or 10, depending on the model) were stress relieved after bending.  Assuming the stresses were fully relieved as a result of this process, the resistance to cracking should generally be the same if all other factors (such as material microstructure) are the same. In 2003, the licensee concluded that there was no flaw at the location where the crack was eventually observed in 2009 in the tube in R1C20 in Steam Generator 3.  Its conclusion was based on observing only a minor change in the eddy current signal (bobbin and rotating probe)
discussed in NRC IN 2003-13. All of these cracks have been in tubes made with mill-annealed
between 1997, 2000, and 2003 and the general lack of cracking in units with thermally treated Alloy 600 tubing.  Following the discovery of the crack in 2009, the NRC staff reviewed the 2003 and 2009 rotating probe eddy current data for the tube in R1C20.  Although the NRC staff did not have all of the information available to the licensee, the NRC staff's review of the 2003 rotating probe data indicated the presence of a flaw-like signal.  These results highlight the


limitation of confirming flaw signals based on signals exhibiting change from one inspection to the next and the difficulties in detecting new or unexpected forms of degradation. Detecting primary water stress-corrosion cracking (i.e., cracking that initiates from the inside diameter of the tubing) may be enhanced by using smaller probes operated at high frequencies. Although the noise levels in the data obtained at higher and lower frequencies may be comparable, the signal level associated with a flaw on the inside diameter of the tube may be significantly greater at the higher frequencies. This will increase the signal-to-noise level for this type of flaw and
Alloy 600 tubing. (Note: Although NRC IN 97-26 indicates that an axial indication was
 
discovered in the U-bend region of a thermally treated Alloy 600 tube at Braidwood Station, Unit 2, subsequent evaluation indicated that this indication was not a crack).
 
The findings at Vogtle, Unit 1 are particularly noteworthy because this is the first confirmed
 
instance of cracking in the U-bend region of a thermally treated Alloy 600 tube. Although there
 
was a manufacturing indication near the location where the crack developed, it is not known
 
whether this condition is necessary to lead to the initiation of a crack in this region of the tubing.
 
In addition, although the crack at Vogtle, Unit 1 occurred in the U-bend region of a Row 1 tube, it is not clear that this phenomenon would be primarily limited to low-row (i.e., Rows 1 and 2)
tubes as it primarily was for units with mill-annealed Alloy 600 steam generator tubing. In the
 
units with mill-annealed Alloy 600 tubing, the U-bends were typically not stress relieved after
 
bending. As a result, the residual stresses; and therefore, the susceptibility to cracking, would
 
normally be expected to be highest in the lowest row tube (i.e., the one with the shortest bend
 
radius), provided there were no significant changes in the bending processes from one tube row
 
to another. However, in the case of the units with thermally treated Alloy 600 tubing, the
 
U-bends of the low-row tubes (i.e., Rows 1 through 8, 9, or 10, depending on the model) were
 
stress relieved after bending. Assuming the stresses were fully relieved as a result of this
 
process, the resistance to cracking should generally be the same if all other factors (such as
 
material microstructure) are the same. In 2003, the licensee concluded that there was no flaw at the location where the crack was
 
eventually observed in 2009 in the tube in R1C20 in Steam Generator 3. Its conclusion was
 
based on observing only a minor change in the eddy current signal (bobbin and rotating probe)
between 1997, 2000, and 2003 and the general lack of cracking in units with thermally treated
 
Alloy 600 tubing. Following the discovery of the crack in 2009, the NRC staff reviewed the 2003 and 2009 rotating probe eddy current data for the tube in R1C20. Although the NRC staff did
 
not have all of the information available to the licensee, the NRC staffs review of the 2003 rotating probe data indicated the presence of a flaw-like signal. These results highlight the
 
limitation of confirming flaw signals based on signals exhibiting change from one inspection to
 
the next and the difficulties in detecting new or unexpected forms of degradation. Detecting
 
primary water stress-corrosion cracking (i.e., cracking that initiates from the inside diameter of
 
the tubing) may be enhanced by using smaller probes operated at high frequencies. Although
 
the noise levels in the data obtained at higher and lower frequencies may be comparable, the
 
signal level associated with a flaw on the inside diameter of the tube may be significantly greater
 
at the higher frequencies. This will increase the signal-to-noise level for this type of flaw and


improve the likelihood that it would be detected.
improve the likelihood that it would be detected.


As discussed above, at least one of the eddy current data analysts during the 2000 and 2003 inspections identified a signal at the location where the crack was eventually observed in 2009. These signals were dismissed by a resolution analyst. To limit the potential for human error and
As discussed above, at least one of the eddy current data analysts during the 2000 and 2003 inspections identified a signal at the location where the crack was eventually observed in 2009.
 
These signals were dismissed by a resolution analyst. To limit the potential for human error and
 
to improve detection of flaws, some licensees require two independent resolution analysts to


to improve detection of flaws, some licensees require two independent resolution analysts to review the signals identified by the primary and secondary data analysts rather than assigning this review to a single resolution analyst. In addition, when dismissing indications based on a historical review of the data, two independent analysts reviewing the data may improve the detection of flaws or changing conditions.
review the signals identified by the primary and secondary data analysts rather than assigning
 
this review to a single resolution analyst. In addition, when dismissing indications based on a
 
historical review of the data, two independent analysts reviewing the data may improve the
 
detection of flaws or changing conditions.


==CONTACT==
==CONTACT==
This IN requires no specific action or written response. Please direct any questions about this matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor
This IN requires no specific action or written response. Please direct any questions about this
 
matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor


Regulation (NRR) project manager.
Regulation (NRR) project manager.
Line 92: Line 272:
/RA/ by TQuay for
/RA/ by TQuay for


Timothy J. McGinty, Director       Division of Policy and Rulemaking       Office of Nuclear Reactor Regulation
Timothy J. McGinty, Director
 
Division of Policy and Rulemaking
 
Office of Nuclear Reactor Regulation


===Technical Contact:===
===Technical Contact:===
Kenneth J. Karwoski, NRR 301-415-2752 E-mail:  kenneth.karwoski@nrc.gov


Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections. In 2003, the licensee concluded that there was no flaw at the location where the crack was eventually observed in 2009 in the tube in R1C20 in Steam Generator 3. Its conclusion was
===Kenneth J. Karwoski, NRR===
                        301-415-2752 E-mail: kenneth.karwoski@nrc.gov
 
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections. In 2003, the licensee concluded that there was no flaw at the location where the crack was
 
eventually observed in 2009 in the tube in R1C20 in Steam Generator 3. Its conclusion was
 
based on observing only a minor change in the eddy current signal (bobbin and rotating probe)
between 1997, 2000, and 2003 and the general lack of cracking in units with thermally treated
 
Alloy 600 tubing. Following the discovery of the crack in 2009, the NRC staff reviewed the 2003 and 2009 rotating probe eddy current data for the tube in R1C20. Although the NRC staff did


based on observing only a minor change in the eddy current signal (bobbin and rotating probe) between 1997, 2000, and 2003 and the general lack of cracking in units with thermally treated Alloy 600 tubing.  Following the discovery of the crack in 2009, the NRC staff reviewed the 2003 and 2009 rotating probe eddy current data for the tube in R1C20.  Although the NRC staff did not have all of the information available to the licensee, the NRC staff's review of the 2003 rotating probe data indicated the presence of a flaw-like signal. These results highlight the limitation of confirming flaw signals based on signals exhibiting change from one inspection to the next and the difficulties in detecting new or unexpected forms of degradation.  Detecting primary water stress-corrosion cracking (i.e., cracking that initiates from the inside diameter of the tubing) may be enhanced by using smaller probes operated at high frequencies.  Although the noise levels in the data obtained at higher and lower frequencies may be comparable, the signal level associated with a flaw on the inside diameter of the tube may be significantly greater
not have all of the information available to the licensee, the NRC staffs review of the 2003 rotating probe data indicated the presence of a flaw-like signal. These results highlight the


at the higher frequencies. This will increase the signal-to-noise level for this type of flaw and improve the likelihood that it would be detected.
limitation of confirming flaw signals based on signals exhibiting change from one inspection to
 
the next and the difficulties in detecting new or unexpected forms of degradation. Detecting
 
primary water stress-corrosion cracking (i.e., cracking that initiates from the inside diameter of
 
the tubing) may be enhanced by using smaller probes operated at high frequencies. Although
 
the noise levels in the data obtained at higher and lower frequencies may be comparable, the
 
signal level associated with a flaw on the inside diameter of the tube may be significantly greater
 
at the higher frequencies. This will increase the signal-to-noise level for this type of flaw and
 
improve the likelihood that it would be detected.


As discussed above, at least one of the eddy current data analysts during the 2000 and 2003 inspections identified a signal at the location where the crack was eventually observed in 2009.
As discussed above, at least one of the eddy current data analysts during the 2000 and 2003 inspections identified a signal at the location where the crack was eventually observed in 2009.


These signals were dismissed by a resolution analyst. To limit the potential for human error and to improve detection of flaws, some licensees require two independent resolution analysts to review the signals identified by the primary and secondary data analysts rather than assigning this review to a single resolution analyst. In addition, when dismissing indications based on a historical review of the data, two independent analysts reviewing the data may improve the
These signals were dismissed by a resolution analyst. To limit the potential for human error and
 
to improve detection of flaws, some licensees require two independent resolution analysts to
 
review the signals identified by the primary and secondary data analysts rather than assigning
 
this review to a single resolution analyst. In addition, when dismissing indications based on a
 
historical review of the data, two independent analysts reviewing the data may improve the


detection of flaws or changing conditions.
detection of flaws or changing conditions.


==CONTACT==
==CONTACT==
This IN requires no specific action or written response. Please direct any questions about this
This IN requires no specific action or written response. Please direct any questions about this
 
matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor
 
Regulation (NRR) project manager.
 
/RA/ by TQuay for
 
Timothy J. McGinty, Director


matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
Division of Policy and Rulemaking


/RA/ by TQuay for      Timothy J. McGinty, Director      Division of Policy and Rulemaking      Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


===Technical Contact:===
===Technical Contact:===
Kenneth J. Karwoski, NRR 301-415-2752 E-mail:  kenneth.karwoski@nrc.gov


Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.
===Kenneth J. Karwoski, NRR===
                        301-415-2752 E-mail: kenneth.karwoski@nrc.gov
 
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.
 
DISTIBUTION:
DLR/RARB                Allen Hiser
 
ADAMS Accession Number: ML102210244                                            TAC ME4181 OFFICE    NRR:DCI                  TECH EDITOR              D:DCI
 
NAME      KKarwoski (AJohnson for) KAzariah-Kribbs          MEvans


DISTIBUTION
DATE      09/29/10                08/16/10 e-mail          10/04/10
  OFFICE    PM:PGCB:DPR              LA:PGCB:DPR              BC:PGCB:DPR        D:DPR


: DLR/RARB Allen Hiser
NAME      ARussell                CHawes                  SRosenberg        TMcGinty


ADAMS Accession Number: ML102210244    TAC ME4181 OFFICE NRR:DCI TECH EDITOR D:DCI  NAME KKarwoski (AJohnson for) KAzariah-Kribbs MEvans  DATE 09/29/10 08/16/10 e-mail 10/04/10  OFFICE PM:PGCB:DPR LA:PGCB:DPR BC:PGCB:DPR D:DPR NAME ARussell CHawes SRosenberg TMcGinty DATE 10/04/10 10/4/10 10/5/10 10/6/10 OFFICIAL RECORD COPY}}
DATE     10/04/10                 10/4/10                 10/5/10           10/6/10
                                      OFFICIAL RECORD COPY}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 15:54, 13 November 2019

Crack-Like Indication in the U-bend Region of a Thermally Treated Alloy 600 Steam Generator Tube
ML102210244
Person / Time
Issue date: 10/06/2010
From: Mcginty T
Division of Policy and Rulemaking
To:
russell andrea
References
IN-10-021
Download: ML102210244 (5)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, DC 20555-0001 October 6, 2010

NRC INFORMATION NOTICE 2010-21: CRACK-LIKE INDICATION IN THE U-BEND

REGION OF A THERMALLY TREATED

ALLOY 600 STEAM GENERATOR TUBE

ADDRESSEES

All holders of an operating license or construction permit for a nuclear power reactor issued

under Title 10 of the Code of Federal Regulations, Part 50, Domestic Licensing of Production

and Utilization Facilities, except those who have permanently ceased operations and have

certified that fuel has been permanently removed from the reactor vessel.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform

addressees of recent operating experience with the detection of a crack-like indication in the

U-bend region of a thermally treated Alloy 600 steam generator tube. The NRC expects that

recipients will review the information for applicability to their facilities and consider actions, as

appropriate, to avoid similar problems. Suggestions contained in this IN are not NRC

requirements; therefore, no specific action or written response is required.

DESCRIPTION OF CIRCUMSTANCES

Vogtle Electric Generating Plant (Vogtle), Unit 1, has four Westinghouse Model F steam

generators. Each steam generator has 5,626 tubes fabricated from thermally treated Alloy 600.

The tubes have a nominal outside diameter of 0.688 inch and a nominal wall thickness of

0.040 inch. Following the bending of the tubes, the U-bend region of the tubes installed in the

first 10 rows of the steam generator was thermally stress-relieved at approximately

1,320 degrees Fahrenheit (715 degrees Celsius) for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to relieve the residual stresses

induced by bending. The radius of a Row 1 U-bend is 2.20 inches. The tubes are arranged in a

square pattern, and the centers of the adjacent tubes are 0.98 inch apart.

When Vogtle, Unit 1 was shut down for the 2009 outage, the unit had operated for

approximately 19.8 effective full-power years. The hot leg temperature is approximately

618 degrees Fahrenheit (326 degrees Celsius).

During the cycle before the 2009 refueling outage, no primary-to-secondary leakage was

observed at Vogtle, Unit 1; however, while the unit was being shut down, there were a few

radiation monitor alarms, indicating the presence of activity on the secondary side of the unit.

The leak rate was too small to measure. With the static pressure from the water on the

secondary side of the steam generator acting on the tubes, there was no visible evidence of

leakage coming from any of the tubes.

For this refueling outage, the licensee planned to use an eddy current rotating probe equipped

with a +PointTM coil to inspect the U-bend region of approximately 50 percent of the tubes in

Rows 1 and 2 in each of the four steam generators. During these rotating probe examinations, the licensee found an axially oriented crack-like indication approximately 3 inches above the

uppermost hot-leg tube support plate (i.e., the seventh support plate) in the tube in Row 1, Column 20 (R1C20), in Steam Generator 3. The crack-like indication was close to the apex of

the tube on the extrados and was attributed to primary water stress-corrosion cracking. The

voltage amplitude of the indication, as measured with the midrange +PointTM coil, operated at

300 kilohertz (kHz) was 3.09 volts. The axial length of the indication was 0.54 inch, its

maximum depth was 100 percent through-wall, and it exceeded 80 percent through-wall over

0.40 inch of its length.

As a result of detecting this indication, the rotating probe examinations in the U-bend region

were expanded to include 100 percent of the Row 1 and 2 tubes in each of the four steam

generators and 20 percent of Row 3 tubes in Steam Generator 3. No other crack-like

indications were found in the U-bend region during these examinations. The licensee plugged

the tube in R1C20 in Steam Generator 3.

The U-bend region of the tube in R1C20 in Steam Generator 3 was inspected in prior outages.

The U-bend region was inspected with a bobbin coil in 1986 (baseline inspection), 1991, 1993,

1997, and 2000. A rotating probe examination of the U-bend region of this tube was also

performed in 1997, 2003, and 2009. The practice of inspecting the U-bend region of tubes in

low rows (e.g., Rows 1 and 2) with only a rotating probe (and not with a bobbin probe) is a fairly

common practice today, given the difficulties in performing quality inspections of tight radius

U-bends with a bobbin probe.

The prior inspections of this tube indicated the presence of a manufacturing indication, referred

to as a Blairsville bump (because the bump was most likely introduced during bending of the

tube at a facility in Blairsville, PA). This bump is located at the start of the bent region of the

tube (i.e., the start of the U-bend region). During the review of the bobbin coil data obtained in

2000, one of the analysts reviewing the data (typically two analysts review all eddy current data)

identified a nonquantifiable indication at the location where the crack-like indication was

eventually discovered. This indication was eventually dismissed by the resolution analyst (an

analyst who oversees the review of the primary and secondary data analysts) because the 1997 rotating probe examination indicated that no flaws were present at this location, the bobbin coil

data indicated that the signal had not changed since the 1986 inspection, and there was a

general absence of any cracking in tubes fabricated from thermally treated Alloy 600 tubing at

the time of the inspection. During the review of the 2003 rotating probe data, an axial indication

was reported by one of the analysts at the location where the crack-like indication was

eventually discovered. This indication was also dismissed by the resolution analyst because the

indication from the rotating probe did not change appreciably from 1997 (1.75 volts as

measured from the 300-kHz channel) to 2003 (1.83 volts as measured from the 300-kHz

channel).

The tube in R1C20 in Steam Generator 3 was pressure-tested in situ in 2009 to confirm its

integrity. During the test, no leakage was observed under simulated normal operating conditions, approximately 0.002 gallons per minute was observed under simulated steamline

break conditions, and approximately 0.09 gallons per minute was observed at three times the

normal operating differential pressure. The tube did not burst at three times the normal

operating differential pressure, demonstrating that it retained adequate structural integrity. The

leak rate from this tube under accident conditions, when combined with all other sources of

accident-induced leakage, was within acceptance limits, demonstrating that the steam generator

had satisfied the accident-induced leakage performance criteria.

BACKGROUND

Previous related generic communications include the following:

August 28, 2003 (Agencywide Documents Access and Management System (ADAMS)

Accession No. ML032410215)

Tubes, dated May 19, 1997 (ADAMS Accession No. ML031060007)

DISCUSSION

Cracking in the U-bend region of steam generator tubes has been observed for years. Many of

these cracks have been located in the U-bends of tubes in Rows 1 and 2 as discussed in NRC

IN 97-26; however, there have been some cracks in the U-bends of higher row tubes as

discussed in NRC IN 2003-13. All of these cracks have been in tubes made with mill-annealed

Alloy 600 tubing. (Note: Although NRC IN 97-26 indicates that an axial indication was

discovered in the U-bend region of a thermally treated Alloy 600 tube at Braidwood Station, Unit 2, subsequent evaluation indicated that this indication was not a crack).

The findings at Vogtle, Unit 1 are particularly noteworthy because this is the first confirmed

instance of cracking in the U-bend region of a thermally treated Alloy 600 tube. Although there

was a manufacturing indication near the location where the crack developed, it is not known

whether this condition is necessary to lead to the initiation of a crack in this region of the tubing.

In addition, although the crack at Vogtle, Unit 1 occurred in the U-bend region of a Row 1 tube, it is not clear that this phenomenon would be primarily limited to low-row (i.e., Rows 1 and 2)

tubes as it primarily was for units with mill-annealed Alloy 600 steam generator tubing. In the

units with mill-annealed Alloy 600 tubing, the U-bends were typically not stress relieved after

bending. As a result, the residual stresses; and therefore, the susceptibility to cracking, would

normally be expected to be highest in the lowest row tube (i.e., the one with the shortest bend

radius), provided there were no significant changes in the bending processes from one tube row

to another. However, in the case of the units with thermally treated Alloy 600 tubing, the

U-bends of the low-row tubes (i.e., Rows 1 through 8, 9, or 10, depending on the model) were

stress relieved after bending. Assuming the stresses were fully relieved as a result of this

process, the resistance to cracking should generally be the same if all other factors (such as

material microstructure) are the same. In 2003, the licensee concluded that there was no flaw at the location where the crack was

eventually observed in 2009 in the tube in R1C20 in Steam Generator 3. Its conclusion was

based on observing only a minor change in the eddy current signal (bobbin and rotating probe)

between 1997, 2000, and 2003 and the general lack of cracking in units with thermally treated

Alloy 600 tubing. Following the discovery of the crack in 2009, the NRC staff reviewed the 2003 and 2009 rotating probe eddy current data for the tube in R1C20. Although the NRC staff did

not have all of the information available to the licensee, the NRC staffs review of the 2003 rotating probe data indicated the presence of a flaw-like signal. These results highlight the

limitation of confirming flaw signals based on signals exhibiting change from one inspection to

the next and the difficulties in detecting new or unexpected forms of degradation. Detecting

primary water stress-corrosion cracking (i.e., cracking that initiates from the inside diameter of

the tubing) may be enhanced by using smaller probes operated at high frequencies. Although

the noise levels in the data obtained at higher and lower frequencies may be comparable, the

signal level associated with a flaw on the inside diameter of the tube may be significantly greater

at the higher frequencies. This will increase the signal-to-noise level for this type of flaw and

improve the likelihood that it would be detected.

As discussed above, at least one of the eddy current data analysts during the 2000 and 2003 inspections identified a signal at the location where the crack was eventually observed in 2009.

These signals were dismissed by a resolution analyst. To limit the potential for human error and

to improve detection of flaws, some licensees require two independent resolution analysts to

review the signals identified by the primary and secondary data analysts rather than assigning

this review to a single resolution analyst. In addition, when dismissing indications based on a

historical review of the data, two independent analysts reviewing the data may improve the

detection of flaws or changing conditions.

CONTACT

This IN requires no specific action or written response. Please direct any questions about this

matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor

Regulation (NRR) project manager.

/RA/ by TQuay for

Timothy J. McGinty, Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contact:

Kenneth J. Karwoski, NRR

301-415-2752 E-mail: kenneth.karwoski@nrc.gov

Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections. In 2003, the licensee concluded that there was no flaw at the location where the crack was

eventually observed in 2009 in the tube in R1C20 in Steam Generator 3. Its conclusion was

based on observing only a minor change in the eddy current signal (bobbin and rotating probe)

between 1997, 2000, and 2003 and the general lack of cracking in units with thermally treated

Alloy 600 tubing. Following the discovery of the crack in 2009, the NRC staff reviewed the 2003 and 2009 rotating probe eddy current data for the tube in R1C20. Although the NRC staff did

not have all of the information available to the licensee, the NRC staffs review of the 2003 rotating probe data indicated the presence of a flaw-like signal. These results highlight the

limitation of confirming flaw signals based on signals exhibiting change from one inspection to

the next and the difficulties in detecting new or unexpected forms of degradation. Detecting

primary water stress-corrosion cracking (i.e., cracking that initiates from the inside diameter of

the tubing) may be enhanced by using smaller probes operated at high frequencies. Although

the noise levels in the data obtained at higher and lower frequencies may be comparable, the

signal level associated with a flaw on the inside diameter of the tube may be significantly greater

at the higher frequencies. This will increase the signal-to-noise level for this type of flaw and

improve the likelihood that it would be detected.

As discussed above, at least one of the eddy current data analysts during the 2000 and 2003 inspections identified a signal at the location where the crack was eventually observed in 2009.

These signals were dismissed by a resolution analyst. To limit the potential for human error and

to improve detection of flaws, some licensees require two independent resolution analysts to

review the signals identified by the primary and secondary data analysts rather than assigning

this review to a single resolution analyst. In addition, when dismissing indications based on a

historical review of the data, two independent analysts reviewing the data may improve the

detection of flaws or changing conditions.

CONTACT

This IN requires no specific action or written response. Please direct any questions about this

matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor

Regulation (NRR) project manager.

/RA/ by TQuay for

Timothy J. McGinty, Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contact:

Kenneth J. Karwoski, NRR

301-415-2752 E-mail: kenneth.karwoski@nrc.gov

Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.

DISTIBUTION:

DLR/RARB Allen Hiser

ADAMS Accession Number: ML102210244 TAC ME4181 OFFICE NRR:DCI TECH EDITOR D:DCI

NAME KKarwoski (AJohnson for) KAzariah-Kribbs MEvans

DATE 09/29/10 08/16/10 e-mail 10/04/10

OFFICE PM:PGCB:DPR LA:PGCB:DPR BC:PGCB:DPR D:DPR

NAME ARussell CHawes SRosenberg TMcGinty

DATE 10/04/10 10/4/10 10/5/10 10/6/10

OFFICIAL RECORD COPY