ML17332A567: Difference between revisions

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{{#Wiki_filter:UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT MONTH: DECEMBER 1994 REV 1: UNIT NAME: DATE: COMPLETED BY: TELEPHONE:
{{#Wiki_filter:REV 1:           February 7,       -1995<<
PAGE February 7,-1995<<D.C.COOK UNIT" 2 Van 5, 1995 D.L.Bublick (616)465-5901 Page 1 of 1 DURATION NO.DATE TYPE HOURS METHOD OF SHUTTING LICENSEE DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION REASON REACTOR REPORT NO.CODE CODE TO PREVENT RECURRENCE X UN UUI ZO M DUI UO OO nw RW ON UIUI OO OM UOO UWV XII 0'39 940906 S 240 941211 F 50.7 H 255.2 B, C N/A 94-008 N/A IB N/A LS The unit was removed from servic on 940906 at 0318 hours EDT for the cycle 9 to 10 refueling/maintenance outage.All refueling and maintenance activities were completed and the main turbine generator was paralleled to the grid at 1514 hours on 941211.Total length of the outage was 2315.9 hours.During power escalation, with the reactor power at 19%RTP, an MSR high level trip signal was generated followed by a reactor trip at 1705 hours on 941211.The cause of the trip signal could not be conclusively determined.
UNIT  SHUTDOWNS AND POWER REDUCTIONS                                UNIT NAME:        D. C. COOK UNIT"2 DATE:            Van 5, 1995 REPORT MONTH: DECEMBER 1994                                      COMPLETED BY:    D. L. Bublick TELEPHONE:        (616) 465-5901 PAGE              Page 1 of 1 METHOD OF SHUTTING     LICENSEE DURATION            DOWN         EVENT       SYSTEM COMPONENT     CAUSE AND CORRECTIVE ACTION NO. DATE  TYPE      HOURS      REASON   REACTOR     REPORT NO. CODE   CODE           TO PREVENT RECURRENCE 940906   S       255.2       B, C                   N/A       N/A     N/A         The unit was removed from servic on 940906 at 0318 hours EDT for the cycle 9 to 10 refueling/maintenance     outage.
The unit was paralleled to the grid at 1949 hours on 941213.1 F: Forced S: Scheduled 2 Reason: A: Equipment Failure (Explain)B: Maintenance or Test C: Refueling D: Regulatory Restriction E: Operator Training and License Examination F: Administrative G: Operational Error (Explain)H: Other (Explain)3 Method: 1: Manual 2: Manual Scram 3: Automatic Scram 4: Other (Explain)Exhibit G-Instructions for preparation of data entry sheets for Licensee Event Report (LER)File (NUREG 1061)5 Exhibit I: Same Source}}
X UN                                                                                            All refueling and maintenance UUI ZO activities were completed and       the M                                                                                            main turbine generator was paralleled to the grid at 1514 0'39 DUI UO OO hours on 941211. Total length of the outage was 2315.9   hours.
nw RW 50.7                              94-008      IB    LS            During power escalation,     with the ON 240    941211    F                  H reactor power at   19% RTP, an MSR UIUI OO                                                                                            high level trip signal was OM                                                                                            generated followed by a reactor UOO UWV                                                                                              trip at 1705 hours on 941211.
XII                                                                                              The cause of the   trip signal could not be conclusively determined. The unit was paralleled to the grid at 1949 hours on 941213.
1               2                                    3                                                  5 F: Forced       Reason:                              Method:            Exhibit  G  Instructions      Exhibit I:    Same S: Scheduled     A: Equipment Failure (Explain)       1: Manual          for preparation of data                        Source B: Maintenance or Test               2: Manual Scram    entry sheets for Licensee C: Refueling                       3: Automatic Scram Event Report (LER) File D: Regulatory Restriction           4: Other (Explain) (NUREG  1061)
E: Operator Training and License Examination F: Administrative G: Operational Error (Explain)
H: Other (Explain)}}

Revision as of 12:40, 22 October 2019

Revised Unit Shutdowns & Power Reductions Rept for Dec 1994 for DCP Unit 2
ML17332A567
Person / Time
Site: Cook 
Issue date: 12/31/1994
From: Bublick D
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML17332A564 List:
References
NUDOCS 9502150093
Download: ML17332A567 (1)


Text

REV 1: February 7, -1995<<

UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME: D. C. COOK UNIT"2 DATE: Van 5, 1995 REPORT MONTH: DECEMBER 1994 COMPLETED BY: D. L. Bublick TELEPHONE: (616) 465-5901 PAGE Page 1 of 1 METHOD OF SHUTTING LICENSEE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE HOURS REASON REACTOR REPORT NO. CODE CODE TO PREVENT RECURRENCE 940906 S 255.2 B, C N/A N/A N/A The unit was removed from servic on 940906 at 0318 hours0.00368 days <br />0.0883 hours <br />5.257936e-4 weeks <br />1.20999e-4 months <br /> EDT for the cycle 9 to 10 refueling/maintenance outage.

X UN All refueling and maintenance UUI ZO activities were completed and the M main turbine generator was paralleled to the grid at 1514 0'39 DUI UO OO hours on 941211. Total length of the outage was 2315.9 hours.

nw RW 50.7 94-008 IB LS During power escalation, with the ON 240 941211 F H reactor power at 19% RTP, an MSR UIUI OO high level trip signal was OM generated followed by a reactor UOO UWV trip at 1705 hours0.0197 days <br />0.474 hours <br />0.00282 weeks <br />6.487525e-4 months <br /> on 941211.

XII The cause of the trip signal could not be conclusively determined. The unit was paralleled to the grid at 1949 hours0.0226 days <br />0.541 hours <br />0.00322 weeks <br />7.415945e-4 months <br /> on 941213.

1 2 3 5 F: Forced Reason: Method: Exhibit G Instructions Exhibit I: Same S: Scheduled A: Equipment Failure (Explain) 1: Manual for preparation of data Source B: Maintenance or Test 2: Manual Scram entry sheets for Licensee C: Refueling 3: Automatic Scram Event Report (LER) File D: Regulatory Restriction 4: Other (Explain) (NUREG 1061)

E: Operator Training and License Examination F: Administrative G: Operational Error (Explain)

H: Other (Explain)