ML18219B543: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:REGULATORY DISTRIBUTION FOR INFORMATl'QN DISTRl'BUTION SYSTEM<RIDS)INCOMING MATERIAL GRG: SHALLER D V'DOCDA IN Kc'MI PWR DATE TE: 04/05/78 REC: KEPPLER J G RCVD: 04/10/78 NRC COPIES RECEIVED DGCTYPE: LETTER NOTARIZED:
{{#Wiki_filter:REGULATORY INFORMATl'QN DISTRl'BUTION SYSTEM <RIDS)
NO LTR 1 ENCL 1
DISTRIBUTION FOR INCOMING MATERIAL REC:    KEPPLER J    G                  GRG: SHALLER D V                   'DOCDATE: 04/05/78 NRC                                    IN Kc 'MI PWR                     DATE RCVD: 04/10/78 DGCTYPE:     LETTER     NOTARIZED: NO                                         COPIES RECEIVED


==SUBJECT:==
==SUBJECT:==
8 CONCERNING FQRW ARDING LICENSEE EVENT REPT<RO 50-316/78-006/03L)
LTR 1      ENCL 1 FQRW ARDING LICENSEE EVENT REPT <RO 50-316/78-006/03L) ON 03/12/7 8 CONCERNING DURING PHYSICS TESTING AFTER INITIAL FUEL LOADING'RESSURIZER LEVEL) CHANNEL I I < NLP-152) INDICATIONS WAS 9/. HIGHER THAN THE OTHER TWO CHANNELS EXCEEDING TECH SPEC LIMIT IN TA PLANT NAME: COOK UNIT 2                                         REVIEWER   INITIAL: X JM DISTRIBUTOR     INITIAL:   ~
ON 03/12/7 DURING PHYSICS TESTING AFTER INITIAL FUEL LOADING'RESSURIZER LEVEL)CHANNEL I I<NLP-152)INDICATIONS WAS 9/.HIGHER THAN THE OTHER TWO CHANNELS EXCEEDING TECH SPEC LIMIT IN TA PLANT NAME: COOK-UNIT 2 REVIEWER INITIAL: X JM DISTRIBUTOR INITIAL:~assssst+st+ow+>+%+++>
assssst+st+ow+>+%+++>   DISTRIBUTION OF THIS MATERIAL IS       AS FOLLOWS +w++wwww+wwwwwvww+
DISTRIBUTION OF THIS MATERIAL IS A S FOLLOWS+w++wwww+wwwwwvww+
NOTES:
NOTES: 1.SEND 3 COPIES OF ALL MATERIAL TO IS(E INCI DENT REPORTS (DISTRIBUTION CODE A002)FOR ACTION: INTERNAL: EXTERNAL:~W/4 ENCL G FILE++W/ENCL I 8c SCHROEDER/I PPOL I TO+4 M/ENCL NOVAK/CHECK+4W/ENCL KNIGHT~l~W/ENCL HANAUER%+W/ENCI E I SENHUT++W/ENCL SHA0~~4W/ENCL KREGER/J.COLL INS+4W/ENCL K SEYFRI T/IE~~W/ENCL LPDR S ST.JOSEPH'I++W/ENCL TI C++W/ENCL NS I C++W/ENCL ACRS CAT B++W/16 ENCL NRC PDR~~W/ENCL MIPC++W/3 ENCL HOUSTON++W/ENCL GR IMES++W/ENCL BUTLER++W/ENCL TEDESCO++W/ENCL BAER~~W/ENCL VOLLMER/BUNCHi~~W/ENCL ROSA>+W/ENCL COPIES NOT SUB".fITTED PEP, REGULATORY CUI DE 10~1 DISTRIBUTION:
: 1. SEND 3 COPIES OF ALL MATERIAL TO IS(E INCIDENT    REPORTS (DISTRIBUTION   CODE     A002)
LTR 45 ENCL 45 SIZE: 1P+iP+1P CONTROL NBR 7810 0 THE END+%%%%%%%%4%%+%%%%%%%%%3!
FOR ACTION:                             ~W/4 ENCL INTERNAL:              G   FILE++W/ENCL                  NRC PDR~~W/ENCL I   8c                               MIPC++W/3 ENCL SCHROEDER/I PPOL I TO+4 M/ENCL        HOUSTON++W/ENCL NOVAK/CHECK+4W/ENCL                  GR IMES++W/ENCL KNIGHT~l ~W/ENCL                      BUTLER++W/ENCL HANAUER%+W/ENCI                       TEDESCO++W/ENCL E I SENHUT++W/ENCL                    BAER~~W/ENCL SHA0~~4W/ENCL                        VOLLMER/BUNCHi~~W/ENCL KREGER/J. COLL INS+4W/ENCL            ROSA>+W/ENCL K SEYFRI T/IE~~W/ENCL EXTERNAL:          LPDR S ST. JOSEPH'     I ++W/ENCL TI C++W/ENCL NS I C++W/ENCL ACRS CAT B++W/16 ENCL                   COPIES NOT SUB".fITTED PEP, REGULATORY CUI DE 10 ~ 1 DISTRIBUTION:         LTR 45       ENCL 45                         CONTROL NBR      7810    0 SIZE: 1P+iP+1P THE END +%%%%%%%%4%%+%%%%%%%%%3! 4%%%
4%%%  


(p F tc.5 col%e0 PL mermen y t NDIANA&MICHIGAN POI/I/EH COMPANY'DONALD C.COOK NUCLEAR PLANT P.O.Box 458, Bridgman, Michigan 49106 April 5, 1978 Mr.J.'G.Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-74 Docket No.50-316  
(p F tc.5 col%
e0 PL mermen y t   NDIANA & MICHIGANPOI/I/EH COMPANY
                  'DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 April 5,     1978 Mr. J.'G. Keppler, Regional       Director Office of Inspection       and Enforcement United States     Nuclear Regulatory Commission Region   III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-74 Docket No. 50-316


==Dear Mr.Keppler:==
==Dear Mr. Keppler:==
Pursuant to the requi rements of the Appendix A Tech~ical Specifications the following report is submitted:
RO 78-006/03L-0'.
Sincerely, D.V.Shaller Plant Manager/bab cc: J.E.Dolan R.W.Jurgensen R.F.Kroeger R.Kilburn R.J.Vollen BPI K.R.Baker RO: III R C.Callen MPSC P.W.Steketee, Esq.G.Charnoff, Esq.R: Walsh, Esq.G.Olson J.M.Hennigan PNSRC J.F.Stietzel Dir., IE (30 copies)Dir., MIPC (3 copies)gPR 10 t978
~~'a,.
.S.NUCLEAR REGULATORY COMMISSION 1 LICENSEE EVENT REPORT (NLP-152)INDICATION WAS 95 HIGHER THAN THE OTHER TWO CHANNELS.THIS EXCEEDED THE NRC FORM 366 I7-77)~~n CONTROL BLOCK: Q1{PLEASE PRINT OR TYPE ALL REQUIRED INFORIVIATION) 1 6[oats]M I D C C ZQO 0 0 0 0 0 0 0 0 0Q4 1 1 I 1 Qs~Qs 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T IX%soo,"o;~LQs 0 5 0 0 0 3 1 6 Qs 0 3 1 2 7 8 Qso 4 0 5 7 8 Qs 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q1P~oe DURING PHYSICS TESING AFTER INITIAL FUEL LOADING.PRESSURIZER LEVEL, CHANNEL II,~ps T.S.LIMIT IN TABLE 3.3-4.THE APPLICABLE ACTION ITEM (TABLE 3.3-3 ACTION614) 6 WAS FULFILLEDa,PREVIOUS EVENTS OF A SIMILAR NATURE WERE REPORTED ON UNIT 1 DOCKET~os No 050-0315 R 0.4 75-76,76-40,76-41, 77-41 and 78-10~os 7 8 9~OB 80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE.CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~IA Qii X Q12~2Q13 I N S T R U QPs~TQ>>~Z Q's 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.CODE TYPE NO.Q>7 Rseos7~78~~ap 6~m~03~L~~0 21 22 23 24 26 27 28 29 30 31 32 ACTION FLITURE EFFECT SHUTDOWN ATTACHMENT NPRD.4 PRIME COMP.COMPONENT TAKEN ACTION ON PLANT s METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
~BQs~28)~ZQso~Z 0 0 0 0 Y Qso~YQs4 L Qse 8 0 8 0 Qss 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o'NVESTIGATION REVEALED THAT THE ROOT VALVE.ON THE SENSING LINE OF THE TRANSMITTER (BARTON-MODEL A'764)HAD A PACKING LEAK.THIS PACKING LEAK RESULTED IN A LOSS OF WATER FROM THE REFERENCE LEG OF THE TRANSMITTER.
CONSEQUENTLY, AN: INCREASING LEVEL 4 REFERENCE LEG WAS REFILLED.(SEE ATTACHED SUPPLEMENT.)
7 8 9 FACILITY~3P METHOD OF STATUS 56 POWER s OTHER STATUS~-DISCOVERY DISCOVERY DESCRIPTION Q32 s 8 Qes~00 3 Qse NA'~BQw OPERATOR OBSERVATION 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY~LOCATION OF RELEASE Q CK z Q" z Q34 NA NA 7 8 9 10 44 PERSONNEI.
EXPOSURES NUMBER TYPE DESCRIPTION Q39~OO O Qn Z Qss NA 7 8 9 11 12~13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41
~e~00 O Qso NA 45 3 ON THIS CHANNEL RESULTED~THE PACKING ON THE AFFECTED VALVE WAS TIGHTENED AND THE, 80 80 80 80 7 8 7 8 o 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION
~zQ42 9 10 PUBLICITY ISSUED DESCRIPTION
~~ZQ44 9 10 NAME OF PREPARER NA Jack Risch1'0 68 69 ,,616-465-59O1 s I 80 NRC USE ONLY 80 g 0


SUPPLEMENT TO LICENSE EVENT REPORT&#xb9;RO 78-006/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION I THE AFFECTED CHANNEL WAS RETURNED TO OPERATION WITH LEVEL INDICATION WITHIN 1%OF THE OTHER CHANNELS.  
Pursuant to the requi rements of the Appendix    A Tech~ical Specifications the following report is submitted:
'f 0" I I'1 l e}}
RO  78-006/03L-0'.
Sincerely, D.V. Shaller Plant Manager
        /bab cc:  J.E. Dolan R.W. Jurgensen R.F. Kroeger R. Kilburn R.J. Vollen BPI K.R. Baker RO: III R C. Callen MPSC P.W. Steketee, Esq.
G. Charnoff, Esq.
R: Walsh, Esq.
G. Olson                                          gPR 10 t978 J.M. Hennigan PNSRC J.F. Stietzel Dir.,    IE (30 copies)
Dir.,    MIPC  (3 copies)
 
~ ~ 'a,.
NRC FORM 366 I7-77) ~~
LICENSEE EVENT REPORT 1    . S. NUCLEAR REGULATORY COMMISSION n
CONTROL BLOCK:                                                  Q1                      {PLEASE PRINT OR TYPE ALL REQUIRED INFORIVIATION) 1                                    6
[oats]8        9 M    I    D LICENSEE CODE C    C      ZQO14      15 0    0    0    0        0 LICENSE NUMBER 0    0    0      0Q4 25      26 1      1 LICENSE TYPE I      1 30 Qs~Qs57 CAT 58 CON'T IX%                  soo,"o;~LQs                  0      5      0    0    0    3    1        6 Qs        0    3    1    2    7      8    Qso            4    0      5  7    8    Qs 60          61              DOCKET NUMBER                    68    69        EVENT DATE              74        75        REPORT DATE              80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                    Q1P
~oe                DURING PHYSICS TESING AFTER                              INITIAL FUEL                LOADING.            PRESSURIZER LEVEL, CHANNEL                                II, (NLP-152) INDICATION                          WAS    95 HIGHER THAN THE OTHER                            TWO CHANNELS.                      THIS EXCEEDED THE
  ~ps              T. S. LIMIT IN TABLE 3.3-4.                                THE APPLICABLE ACTION ITEM (TABLE                                          3.3-3      ACTION614) 6          WAS    FULFILLEDa,PREVIOUS EVENTS OF A SIMILAR NATURE WERE REPORTED                                                                        ON  UNIT        1  DOCKET
  ~os              No    050-0315                R    0.4 75-76,76-40,76-41, 77-41 and 78-10
  ~os                                                                                                                                                                                                  80 7        8 9 SYSTEM                CAUSE          CAUSE                                                                COMP.            VALVE.
CODE                CODE        SUBCODE                        COMPONENT CODE                        SUBCODE            SUBCODE
  ~OB 7        8                        9
                                      ~IA        10 Qii 11 X  Q12    ~2Q13 12                  13 I    N      S    T      R    U 18 QPs        ~TQ>>
19
                                                                                                                                                                      ~Z 20 Q's SEQUENTIAL                                OCCURRENCE              REPORT                          REVISION Q>7 LERIRO Rseos7 ACTION FLITURE EVENT YEAR
                                      ~78 21        22 EFFECT
                                                                ~
23 SHUTDOWN
                                                                              ~ap 24 REPORT NO.
6 26
                                                                                                            ~m 27
                                                                                                                            ~03 28 ATTACHMENT CODE 29 NPRD.4 TYPE
                                                                                                                                                      ~L 30 PRIME COMP.
                                                                                                                                                                        ~
31
                                                                                                                                                                                      ~0 NO.
32 COMPONENT TAKEN ACTION                  ON PLANT      s      METHOD                      HOURS Q22          SUBMITTED          FORM SUB.            SUPPLIER              MANUFACTURER
                ~BQs~28) 33          34
                                                ~ZQso 35
                                                                    ~Z 36              37 0        0    0      0 40 Y
41 Qso        ~YQs4 42 L
43 Qse        8 44 0    8  0 47 Qss CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o    'NVESTIGATION                    REVEALED THAT THE ROOT VALVE .ON THE SENSING LINE OF THE TRANSMITTER (BARTON-MODEL A'764) HAD A PACKING LEAK.                                              THIS PACKING LEAK RESULTED IN A LOSS                                            OF WATER FROM THE REFERENCE                              LEG OF THE TRANSMITTER.                            CONSEQUENTLY, AN: INCREASING LEVEL 3        ON    THIS CHANNEL RESULTED                        ~  THE PACKING ON THE AFFECTED VALVE WAS TIGHTENED AND THE, 4          REFERENCE            LEG WAS          REFILLED. ( SEE ATTACHED SUPPLEMENT.)
8    9                                                                                                                                                                                    80
                                                                                      ~
7 FACILITY                                                                ~3P          METHOD OF STATUS              56 POWER              s        OTHER STATUS            '
                                                                                                -    DISCOVERY                                  DISCOVERY DESCRIPTION Q32 s          8  Qes    ~00            3    Qse                    NA                          ~BQw                OPERATOR OBSERVATION 7        8    9              10              12        13                                44        45          46                                                                              80 CK ACTIVITY z    Q" CONTENT RELEASED OF RELEASE z    Q34 AMOUNT OF ACTIVITY NA
                                                                                    ~                                      NA LOCATION OF RELEASE              Q 7        8    9              10                                                            44              45                                                                                    80 PERSONNEI. EXPOSURES NUMBER              TYPE          DESCRIPTION Q39
                ~OO          O Qn          Z Qss                        NA 7        8    9                11      12        ~  13                                                                                                                                          80 PERSONNEL INJURIES NUMBER              DESCRIPTIONQ41
~e ~00 7        8    9 O Qso 11      12 NA LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION                      Q43 Risch1'0
              ~zQ42 7        8    9          10                                                                                                                                                                        80 o
ISSUED
              ~ZQ44 PUBLICITY DESCRIPTION        ~                            NA NRC USE ONLY 7        8    9          10                                                                                                                                  68  69                              80 g
                                                                                                                                                              ,,616-465-59O1                              0 NAME OF PREPARER                                    Jack s
I
 
SUPPLEMENT TO LICENSE EVENT REPORT &#xb9; RO 78-006/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION I
THE AFFECTED CHANNEL WAS RETURNED TO OPERATION WITH LEVEL INDICATION WITHIN 1% OF THE OTHER CHANNELS.
 
          'f 0" I
l I
    '1 e}}

Revision as of 18:56, 20 October 2019

D.C. Cook - Pursuant to the Requirements of the Appendix a Technical Specifications, Submit Report: RO 78-006/03L-0
ML18219B543
Person / Time
Site: Cook  
Issue date: 04/05/1978
From: Shaller D
American Electrtic Power System, Indiana Michigan Power Co, (Formerly Indiana & Michigan Power Co)
To: James Keppler
NRC/RGN-III
References
Download: ML18219B543 (8)


Text

REGULATORY INFORMATl'QN DISTRl'BUTION SYSTEM <RIDS)

DISTRIBUTION FOR INCOMING MATERIAL REC: KEPPLER J G GRG: SHALLER D V 'DOCDATE: 04/05/78 NRC IN Kc 'MI PWR DATE RCVD: 04/10/78 DGCTYPE: LETTER NOTARIZED: NO COPIES RECEIVED

SUBJECT:

LTR 1 ENCL 1 FQRW ARDING LICENSEE EVENT REPT <RO 50-316/78-006/03L) ON 03/12/7 8 CONCERNING DURING PHYSICS TESTING AFTER INITIAL FUEL LOADING'RESSURIZER LEVEL) CHANNEL I I < NLP-152) INDICATIONS WAS 9/. HIGHER THAN THE OTHER TWO CHANNELS EXCEEDING TECH SPEC LIMIT IN TA PLANT NAME: COOK UNIT 2 REVIEWER INITIAL: X JM DISTRIBUTOR INITIAL: ~

assssst+st+ow+>+%+++> DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS +w++wwww+wwwwwvww+

NOTES:

1. SEND 3 COPIES OF ALL MATERIAL TO IS(E INCIDENT REPORTS (DISTRIBUTION CODE A002)

FOR ACTION: ~W/4 ENCL INTERNAL: G FILE++W/ENCL NRC PDR~~W/ENCL I 8c MIPC++W/3 ENCL SCHROEDER/I PPOL I TO+4 M/ENCL HOUSTON++W/ENCL NOVAK/CHECK+4W/ENCL GR IMES++W/ENCL KNIGHT~l ~W/ENCL BUTLER++W/ENCL HANAUER%+W/ENCI TEDESCO++W/ENCL E I SENHUT++W/ENCL BAER~~W/ENCL SHA0~~4W/ENCL VOLLMER/BUNCHi~~W/ENCL KREGER/J. COLL INS+4W/ENCL ROSA>+W/ENCL K SEYFRI T/IE~~W/ENCL EXTERNAL: LPDR S ST. JOSEPH' I ++W/ENCL TI C++W/ENCL NS I C++W/ENCL ACRS CAT B++W/16 ENCL COPIES NOT SUB".fITTED PEP, REGULATORY CUI DE 10 ~ 1 DISTRIBUTION: LTR 45 ENCL 45 CONTROL NBR 7810 0 SIZE: 1P+iP+1P THE END +%%%%%%%%4%%+%%%%%%%%%3! 4%%%

(p F tc.5 col%

e0 PL mermen y t NDIANA & MICHIGANPOI/I/EH COMPANY

'DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 April 5, 1978 Mr. J.'G. Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-74 Docket No. 50-316

Dear Mr. Keppler:

Pursuant to the requi rements of the Appendix A Tech~ical Specifications the following report is submitted:

RO 78-006/03L-0'.

Sincerely, D.V. Shaller Plant Manager

/bab cc: J.E. Dolan R.W. Jurgensen R.F. Kroeger R. Kilburn R.J. Vollen BPI K.R. Baker RO: III R C. Callen MPSC P.W. Steketee, Esq.

G. Charnoff, Esq.

R: Walsh, Esq.

G. Olson gPR 10 t978 J.M. Hennigan PNSRC J.F. Stietzel Dir., IE (30 copies)

Dir., MIPC (3 copies)

~ ~ 'a,.

NRC FORM 366 I7-77) ~~

LICENSEE EVENT REPORT 1 . S. NUCLEAR REGULATORY COMMISSION n

CONTROL BLOCK: Q1 {PLEASE PRINT OR TYPE ALL REQUIRED INFORIVIATION) 1 6

[oats]8 9 M I D LICENSEE CODE C C ZQO14 15 0 0 0 0 0 LICENSE NUMBER 0 0 0 0Q4 25 26 1 1 LICENSE TYPE I 1 30 Qs~Qs57 CAT 58 CON'T IX% soo,"o;~LQs 0 5 0 0 0 3 1 6 Qs 0 3 1 2 7 8 Qso 4 0 5 7 8 Qs 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q1P

~oe DURING PHYSICS TESING AFTER INITIAL FUEL LOADING. PRESSURIZER LEVEL, CHANNEL II, (NLP-152) INDICATION WAS 95 HIGHER THAN THE OTHER TWO CHANNELS. THIS EXCEEDED THE

~ps T. S. LIMIT IN TABLE 3.3-4. THE APPLICABLE ACTION ITEM (TABLE 3.3-3 ACTION614) 6 WAS FULFILLEDa,PREVIOUS EVENTS OF A SIMILAR NATURE WERE REPORTED ON UNIT 1 DOCKET

~os No 050-0315 R 0.4 75-76,76-40,76-41, 77-41 and 78-10

~os 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE.

CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OB 7 8 9

~IA 10 Qii 11 X Q12 ~2Q13 12 13 I N S T R U 18 QPs ~TQ>>

19

~Z 20 Q's SEQUENTIAL OCCURRENCE REPORT REVISION Q>7 LERIRO Rseos7 ACTION FLITURE EVENT YEAR

~78 21 22 EFFECT

~

23 SHUTDOWN

~ap 24 REPORT NO.

6 26

~m 27

~03 28 ATTACHMENT CODE 29 NPRD.4 TYPE

~L 30 PRIME COMP.

~

31

~0 NO.

32 COMPONENT TAKEN ACTION ON PLANT s METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~BQs~28) 33 34

~ZQso 35

~Z 36 37 0 0 0 0 40 Y

41 Qso ~YQs4 42 L

43 Qse 8 44 0 8 0 47 Qss CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o 'NVESTIGATION REVEALED THAT THE ROOT VALVE .ON THE SENSING LINE OF THE TRANSMITTER (BARTON-MODEL A'764) HAD A PACKING LEAK. THIS PACKING LEAK RESULTED IN A LOSS OF WATER FROM THE REFERENCE LEG OF THE TRANSMITTER. CONSEQUENTLY, AN: INCREASING LEVEL 3 ON THIS CHANNEL RESULTED ~ THE PACKING ON THE AFFECTED VALVE WAS TIGHTENED AND THE, 4 REFERENCE LEG WAS REFILLED. ( SEE ATTACHED SUPPLEMENT.)

8 9 80

~

7 FACILITY ~3P METHOD OF STATUS 56 POWER s OTHER STATUS '

- DISCOVERY DISCOVERY DESCRIPTION Q32 s 8 Qes ~00 3 Qse NA ~BQw OPERATOR OBSERVATION 7 8 9 10 12 13 44 45 46 80 CK ACTIVITY z Q" CONTENT RELEASED OF RELEASE z Q34 AMOUNT OF ACTIVITY NA

~ NA LOCATION OF RELEASE Q 7 8 9 10 44 45 80 PERSONNEI. EXPOSURES NUMBER TYPE DESCRIPTION Q39

~OO O Qn Z Qss NA 7 8 9 11 12 ~ 13 80 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41

~e ~00 7 8 9 O Qso 11 12 NA LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 Risch1'0

~zQ42 7 8 9 10 80 o

ISSUED

~ZQ44 PUBLICITY DESCRIPTION ~ NA NRC USE ONLY 7 8 9 10 68 69 80 g

,,616-465-59O1 0 NAME OF PREPARER Jack s

I

SUPPLEMENT TO LICENSE EVENT REPORT ¹ RO 78-006/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION I

THE AFFECTED CHANNEL WAS RETURNED TO OPERATION WITH LEVEL INDICATION WITHIN 1% OF THE OTHER CHANNELS.

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