ML18219B543

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D.C. Cook - Pursuant to the Requirements of the Appendix a Technical Specifications, Submit Report: RO 78-006/03L-0
ML18219B543
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 04/05/1978
From: Shaller D
American Electrtic Power System, Indiana Michigan Power Co, (Formerly Indiana & Michigan Power Co)
To: James Keppler
NRC/RGN-III
References
Download: ML18219B543 (8)


Text

REGULATORY DISTRIBUTION FOR INFORMATl'QN DISTRl'BUTION SYSTEM <RIDS)

INCOMING MATERIAL GRG:

SHALLER D V

'DOCDA IN Kc 'MI PWR DATE TE: 04/05/78 REC:

KEPPLER J G

RCVD: 04/10/78 NRC COPIES RECEIVED DGCTYPE:

LETTER NOTARIZED:

NO LTR 1

ENCL 1

SUBJECT:

8 CONCERNING FQRWARDING LICENSEE EVENT REPT

<RO 50-316/78-006/03L)

ON 03/12/7 DURING PHYSICS TESTING AFTER INITIALFUEL LOADING'RESSURIZER LEVEL)

CHANNEL II

< NLP-152)

INDICATIONS WAS 9/. HIGHER THAN THE OTHER TWO CHANNELS EXCEEDING TECH SPEC LIMIT IN TA PLANT NAME: COOK UNIT 2 REVIEWER INITIAL:

XJM DISTRIBUTOR INITIAL:~

assssst+st+ow+>+%+++>

DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS +w++wwww+wwwwwvww+

NOTES:

1.

SEND 3 COPIES OF ALL MATERIAL TO IS(E INCIDENT REPORTS (DISTRIBUTION CODE A002)

FOR ACTION:

INTERNAL:

EXTERNAL:

~W/4 ENCL G FILE++W/ENCL I

8c SCHROEDER/I PPOL ITO+4M/ENCL NOVAK/CHECK+4W/ENCL KNIGHT~l~W/ENCL HANAUER%+W/ENCI EISENHUT++W/ENCL SHA0~~4W/ENCL KREGER/J.

COLLINS+4W/ENCL K SEYFRI T/IE~~W/ENCL LPDR S

ST.

JOSEPH' I++W/ENCL TIC++W/ENCL NS IC++W/ENCL ACRS CAT B++W/16 ENCL NRC PDR~~W/ENCL MIPC++W/3 ENCL HOUSTON++W/ENCL GR IMES++W/ENCL BUTLER++W/ENCL TEDESCO++W/ENCL BAER~~W/ENCL VOLLMER/BUNCHi~~W/ENCL ROSA>+W/ENCL COPIES NOT SUB".fITTED PEP, REGULATORY CUIDE 10 ~ 1 DISTRIBUTION:

LTR 45 ENCL 45 SIZE:

1P+iP+1P CONTROL NBR 7810 0

THE END

+%%%%%%%%4%%+%%%%%%%%%3! 4%%%

(p F tc.5 col%

e0 PL mermen y t NDIANA& MICHIGANPOI/I/EH COMPANY

'DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 April 5, 1978 Mr. J.'G.

Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-74 Docket No. 50-316

Dear Mr. Keppler:

Pursuant to the requi rements of the Appendix A Tech~ical Specifications the following report is submitted:

RO 78-006/03L-0'.

Sincerely, D.V. Shaller Plant Manager

/bab cc:

J.E.

Dolan R.W. Jurgensen R.F.

Kroeger R. Kilburn R.J.

Vollen BPI K.R. Baker RO: III R C. Callen MPSC P.W. Steketee, Esq.

G. Charnoff, Esq.

R: Walsh, Esq.

G.

Olson J.M. Hennigan PNSRC J.F. Stietzel Dir., IE (30 copies)

Dir., MIPC (3 copies) gPR 10 t978

~ ~ 'a,.

. S. NUCLEAR REGULATORYCOMMISSION 1

LICENSEE EVENT REPORT (NLP-152)

INDICATION WAS 95 HIGHER THAN THE OTHER TWO CHANNELS.

THIS EXCEEDED THE NRC FORM 366 I7-77) ~~

n CONTROL BLOCK:

Q1

{PLEASE PRINT OR TYPE ALLREQUIRED INFORIVIATION) 1 6

[oats]

M I

D C

C ZQO 0

0 0

0 0

0 0

0 0Q4 1

1 I

1 Qs~Qs 8

9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T IX%

soo,"o;~LQs 0

5 0

0 0

3 1

6 Qs 0

3 1

2 7

8 Qso 4

0 5

7 8

Qs 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q1P

~oe DURING PHYSICS TESING AFTER INITIAL FUEL LOADING.

PRESSURIZER LEVEL, CHANNEL II,

~ps T.

S.

LIMIT IN TABLE 3.3-4.

THE APPLICABLE ACTION ITEM (TABLE 3.3-3 ACTION614) 6 WAS FULFILLEDa,PREVIOUS EVENTS OF A SIMILAR NATURE WERE REPORTED ON UNIT 1

DOCKET

~os No 050-0315 R 0.4 75-76,76-40,76-41, 77-41 and 78-10

~os 7

8 9

~OB 80 7

8 SYSTEM CAUSE CAUSE COMP.

VALVE.

CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~IA Qii X

Q12

~2Q13 I

N S

T R

U QPs

~TQ>>

~Z Q's 9

10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.

CODE TYPE NO.

Q>7 Rseos7

~78

~

~ap 6

~m

~03

~L

~

~0 21 22 23 24 26 27 28 29 30 31 32 ACTION FLITURE EFFECT SHUTDOWN ATTACHMENT NPRD.4 PRIME COMP.

COMPONENT TAKEN ACTION ON PLANT s METHOD HOURS Q22 SUBMITTED FORM SUB.

SUPPLIER MANUFACTURER

~BQs~28)

~ZQso

~Z 0

0 0

0 Y

Qso

~YQs4 L

Qse 8

0 8

0 Qss 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o 'NVESTIGATION REVEALED THAT THE ROOT VALVE.ON THE SENSING LINE OF THE TRANSMITTER (BARTON-MODEL A'764)

HAD A PACKING LEAK.

THIS PACKING LEAK RESULTED IN A LOSS OF WATER FROM THE REFERENCE LEG OF THE TRANSMITTER.

CONSEQUENTLY, AN: INCREASING LEVEL 4

REFERENCE LEG WAS REFILLED.

(

SEE ATTACHED SUPPLEMENT.)

7 8

9 FACILITY

~3P METHOD OF STATUS 56 POWER s

OTHER STATUS ~

DISCOVERY DISCOVERY DESCRIPTION Q32 s

8 Qes

~00 3

Qse NA

~BQw OPERATOR OBSERVATION 7

8 9

10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY~

LOCATION OF RELEASE Q CK z

Q" z

Q34 NA NA 7

8 9

10 44 PERSONNEI. EXPOSURES NUMBER TYPE DESCRIPTION Q39

~OO O

Qn Z

Qss NA 7

8 9

11 12

~ 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41

~e

~00 O

Qso NA 45 3

ON THIS CHANNEL RESULTED ~

THE PACKING ON THE AFFECTED VALVE WAS TIGHTENED AND THE, 80 80 80 80 7

8 7

8 o

7 8

9 11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE DESCRIPTION

~zQ42 9

10 PUBLICITY ISSUED DESCRIPTION~

~ZQ44 9

10 NAME OF PREPARER NA JackRisch1'0 68 69

,,616-465-59O1 sI 80 NRC USE ONLY 80 g 0

SUPPLEMENT TO LICENSE EVENT REPORT ¹ RO 78-006/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION I

THE AFFECTED CHANNEL WAS RETURNED TO OPERATION WITH LEVEL INDICATION WITHIN 1%

OF THE OTHER CHANNELS.

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