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See also: [[followed by::IR 05000528/2006012]]
See also: [[see also::IR 05000528/2006012]]


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Revision as of 07:36, 13 July 2019

APS Response to NRC Inspection Reports 05000528-06-012, 05000529-06-012 and 05000530-06-012, Corrected Copy
ML070180148
Person / Time
Site: Palo Verde  
Issue date: 01/09/2007
From: Mauldin D
Arizona Public Service Co
To:
Document Control Desk, NRC Region 4
References
102-05626-CDM/SAB/JAP/CJS IR-06-012
Download: ML070180148 (12)


See also: IR 05000528/2006012

Text

CORRECTED

COPY L A M A subsidiary

of Pinnacle West Capital Corporation

David Mauldin Vice President

Mail Station 7605 Palo Verde Nuclear Nuclear Engineering

Tel: 623-393-5553

PO Box 52034 Generating

Station and Support Fax: 623-393-6077

Phoenix, Arizona 85072-2034

102-05626-CDM/SAB/JAP/CJS

January 09, 2007 U.S. Nuclear Regulatory

Commission

ATTN: Document Control Desk Washington, DC 20555 Dear Sir: Subject: Palo Verde Nuclear Generating

Station (PVNGS)Units 1, 2 and 3 Docket Nos. STN 50-528, 50-529, and 50-530 APS Response to NRC Inspection

Report 0500052812006012;

0500052912006012;

05000530/2006012

In NRC Special Inspection

Report 2006012, dated December 6, 2006, the NRC documented

their examination

of activities

associated

with the PVNGS Unit 3, Train A, emergency

diesel generator (EDG) failures that occurred on July 25 and September

22, 2006. On both occasions

the EDG failed to produce an output voltage during testing.The report discusses

two findings.The two findings were (1) a lack of adequate instructions

for corrective

maintenance

of the K-1 relay and (2) the failure to identify and correct the cause of erratic K-1 relay operation

prior to installation

of the spare relay on July 26, 2006. These two findings resulted in the Unit 3, Train A, EDG being inoperable

from September

4 until September 22, 2006. APS has reviewed the NRC Inspection

Report and has no substantive

disagreement

with the facts, as documented

in the report.In accordance

with the Inspection

Manual Chapter 0609, the NRC is currently evaluating

the safety significance

of the findings.

At a January 16, 2007 Regulatory

Conference

in Arlington, Texas, APS will provide the NRC its perspective

on the facts and analytical

assumptions

relevant to determining

the safety significance

of the findings.The purpose of this letter is to provide the results of APS' evaluation

of the EDG K-1 relay failures in advance of the Regulatory

Conference

to facilitate

a focused discussion

at the conference

on the safety significance

of the EDG K-1 relay failures.

APS is providing

our position on the findings as well as the causes and corrective

actions which have been or will be taken.A member of the STARS (Strategic

Teaming and Resource Sharing) Alliance J gI0 J Callaway 0 Comanche Peak 0 Diablo Canyon * Palo Verde 0 South Texas Project & Wolf Creek

U.S. Nuclear Regulatory

Commission

ATTN: Document Control Desk APS Response to NRC Inspection

Report 05000528/2006012;

05000529/2006012;

05000530/2006012

Page 2 NRC letter dated December 22, 2006, which communicated

the results of the Regulatory

Conference

on the Spray Pond operability

issue, re-iterated

the NRC's concern about the continuing

occurrence

of problem identification, root cause analysis and technical

rigor issues. APS recognizes

that this is another such example and is committed

to improving

its performance

in these areas.APS realizes the troubleshooting

and problem solving process lacked the technical

rigor necessary

to ensure deficiencies

were properly identified

and resolved the first time. In this case, the failure to consider all possible causes of the July K-1 relay failure resulted in a subsequent

failure in September.

Immediate

actions have been taken to assure the EDGs remain within their design basis. Additional

actions to address the programmatic

weaknesses

have been identified.

We continue to implement, reinforce, monitor and adjust our performance

improvement

plan to provide greater confidence

that similar events will not recur.The Enclosure

to this letter contains a summary of APS' preliminary

root cause of failure evaluation

for the K-1 relay and also includes a response to the two apparent violations.

Finally, APS intends to supplement

Licensee Event Report (LER) 2006-006 to reflect the results of the K-1 relay failure investigation.

The actions described

in the Enclosure

represent

corrective

actions and are not regulatory

commitments.

There are no regulatory

commitments

in this letter. If you have any questions, please contact James A. Proctor at (623) 393-5730.Sincerely, JMLISAB/JAP/CJS/gt

Enclosure:

Summary of APS Investigation

into Unit 3, Train A, Emergency

Diesel Generator (EDG) K-1 Relay Failures and Corrective

Actions cc: B. S. Mallett NRC Region IV Regional Administrator

M. B. Fields NRC NRR Project Manager M. T. Markley NRC NRR Project Manager G. G. Warnick NRC Senior Resident Inspector

for PVNGS

ENCLOSURE Summary of APS Investigation

into Unit 3, Train A Emergency

Diesel Generator (EDG) K-1 Relay Failures And Corrective

Actions 1 -Introduction

The following

describes

the sequence of events and establishes

the context for the K-1 relay failure on September

22, 2006. This discussion

is not intended to justify the recurrence

of the failure, but to establish

that APS personnel

acted in good faith, though in retrospect, with less than adequate rigor, to identify the apparent cause of failure in July 2006. The EDG was tested repeatedly

to confirm that the apparent cause had been addressed

before it was returned to service in July 2006.The root cause analysis of the September

22, 2006 failure of the replacement

K-1 relay was determined

to be inadequate

auxiliary

dc contact 'compression.'

The symptoms of failure in July, however, could be explained

by contact oxidation, and the contact'compression'

issue did not reveal itself during repeated testing prior to returning

the relay to service in July 2006. This is explained

in more detail in the following

sections.At the time of the original K-1 relay failure on July 25, 2006, there had not been a failure of an EDG to produce any output voltage following

a start in the emergency

mode in over 3,000 starts since 1990, when a database was initiated

to track EDG start history.A written troubleshooting

plan was developed

on July 25, 2006 by personnel

with over 40 years combined EDG experience.

When it was identified

that the K-1 relay was the cause of the EDG to not produce output voltage, the 'original'

K-1 relay was removed and segregated

for failure analysis.

The maintenance

practice had been to replace the K-1 relay unit, due to its hybrid design, and not to perform maintenance

on the K-1 relay.APS had already planned to replace all of the EDG automatic

voltage regulators, including

replacement

of the K-1 relays, with a different

design during the next refueling outage for each unit beginning

with Unit 1 in the spring of 2007. The planned replacements

were for a variety of reasons, including

the inability

to obtain replacement

parts, since the component

parts of the K-1 relay are no longer being manufactured

and there were limited spares available.

When the first replacement

K-1 relay was obtained from the warehouse (one of two remaining

spares) it exhibited

symptoms of auxiliary

dc contact oxidation, which was not unexpected

due to the relay being stored for about 20 years. Initial attempts to remove this oxidation

by non-intrusive

methods were not entirely successful, and the last replacement

spare in the warehouse

was judged to not be suitable for use, due to a warped relay cover and apparent auxiliary

dc contact oxidation.

It was only after these efforts that APS personnel

had no recourse but to disassemble

the auxiliary

dc contact assembly on the first replacement

relay to perform more extensive

contact cleaning.1

Before disassembly

of the replacement

dc auxiliary

contact assembly, a dc auxiliary contact assembly from a training relay was disassembled

with the craft to ensure adequate knowledge

of the device. Maintenance

and Engineering

personnel

practiced repeated disassemblies

and reassemblies

of the auxiliary

dc contact assembly for approximately

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to ensure proficiency.

There was no attempt to change the configuration

of the relay, just an effort to clean the contacts, following

disassembly.

Following

the corrective

maintenance

on the replacement

relay, approximately

10 manual actuation

tests and 3 electrical

functional

tests verified that the replacement

relay was performing

properly.

A successful

maintenance

run of the Unit 3, Train A, EDG was performed

and the EDG passed a Technical

Specification

surveillance

test, before being declared operable.

During these retests, there was no indication

of erratic dc auxiliary

contact assembly operation.

The Unit 3, Train A, EDG was subsequently

successfully

tested on August 7 and 24, 2006 and finally on September

4, 2006. Our root cause efforts have led us to the conclusion

that the relay failed to properly reset after the September

4, 2006 test. This failure led to the September

22, 2006 failure of the Unit 3, Train A, EDG.In retrospect, APS acknowledges, as described

in the inspection

report "the licensee's

problem analysis efforts were narrowly focused, which led them to conclude that the cause of the erratic dc auxiliary

switch operation

was oxidized contacts." (Page 7 of IR enclosure)

The failure mechanism

of inadequate

contact 'compression'

of September 22, 2006 did not reveal itself during repeated maintenance

and post-installation

tests following

cleaning of the contacts in July 2006. Subsequent

testing demonstrated

that inadequate

contact 'compression'

was the cause of the September

22, 2006 failure.The latent failure mechanism

did ultimately

reveal itself as part of the routine testing protocols

implemented

as part of normal plant operations.

It should be noted that subsequent

root cause of failure testing of the replacement

K-1 relay determined

that the mean number of operations

before failure was 58 cycles, with a minimum of 0 and a maximum of 323 cycles.2 -Summary of Emergency

Diesel Generator

K-1 Relay Root Cause of Failure (RCF) Testing and Evaluation

The testing developed

to determine

the root cause of failure of the September

22, 2006 event was performed

in the following

five phases: 1. Verified the integrity

of circuits external to the K-1 relay to conclusively

determine that the K-1 relay is the appropriate

focus of this root cause investigation.

2. Performed

a physical and dimensional

comparison

of the K-1 relay as well as other training, failed or spare K-1 relays.2

3. Determined

if temperature

can affect the K-1 relay dc auxiliary

contact assembly performance

such that it can cause dimensional

tolerances

to grow and open closed contacts.4. Electrically

cycled the K-1 relay to determine

if the September

22, 2006 event could be repeated.5. Performed

an internal inspection

of the September

22, 2006 dc auxiliary

contact assembly.The root cause of failure testing of the K-1 relay produced the following

substantive

conclusions: " The K-1 relay failure to reset was repeatable.

  • A troubleshooting

event, where a technician

made contact with a terminal (wire number 69) on the dc auxiliary

contact assembly which caused the K-1 relay to reset on September

22, 2006, was repeatable.

The K-1 testing revealed that when the K-1 relay failed to reset, it was then possible to manipulate

wire number 69 which caused the dc auxiliary

normally open contact to open and close. It was noted during an internal inspection

of the dc auxiliary

contact assembly that the lower terminal on this device was loose due to an anomaly in the molded enclosure.

Straightening

the K-1 relay metal actuator arm rectified

the loose terminal by applying positive pressure to the stationary

and movable contacts of the dc auxiliary

contact assembly.* Dimensional

comparison

showed that the root cause of failure of the September 22, 2006 event was due to the accumulation

of tolerances

associated

with the various components

that make-up the K-1 relay (inadequate

auxiliary

dc contact'compression')." With the K-1 relay in the latched state, and the position of the dc auxiliary

contact assembly normally open contact marginally

closed, an increase of temperature

did not provide the needed external stimulus to cause a change of state with this contact." During the cycle testing, there were no failures noted when the K-1 relay's dc auxiliary

contact assembly's

normally open contact closed and then subsequently

opened. It was observed that during a failure, the normally open contact simply did not make-up when the K-1 relay was latched.* The decision made by engineering, after the September

22, 2006 failure, to 'field straighten'

the metal actuator was correct. This compensates

for any tolerance stack-up issues. This configuration

was evaluated

both dimensionally

and by cycling a K-1 relay.3

In summary, the root cause of failure analysis concluded

that the Unit 3, Train A, EDG was inoperable

from September

4 to September

22, 2006 as the K-1 relay dc auxiliary contact assembly contacts did not close properly following

the September

4th shutdown of the EDG. The auxiliary

dc contacts were stable (i.e., would not change state due to physical contact) if they properly reset, but were unstable (i.e., easily changed state with physical contact) if they failed to properly reset.3 -Response to Apparent Violations

This section sets forth APS' position on the two apparent violations

and summarizes

corrective

actions taken or planned that are directly related to the apparent violations.

Apparent Violation

of 10 CFR 50, Appendix B, Criterion

V, "Instructions, Procedures, and Drawings" Restatement

of Apparent Violation 10 CFR Part 50, Appendix B, Criterion

V, "Instructions, Procedures, and Drawings," states, in part, that activities

affecting

quality shall be prescribed

by documented

instructions, procedures, or drawings of a type appropriate

to the circumstances

and shall be accomplished

in accordance

with these instructions, procedures, or drawings.Contrary to this, the licensee failed to develop appropriate

instructions

or procedures

for corrective

maintenance

activities

on the Unit 3 Train A EDG K-1 relay. This failure resulted in the Unit 3 Train A EDG being inoperable

between September

4 and 22, 2006. This item has been entered into the licensee's

corrective

action program as Condition

Report/Disposition

Request (CRDR) 2926830. Pending determination

of safety significance, this finding is identified

as an apparent violation (AV)5000530/2006012-01, "Failure to Establish

Appropriate

Instructions." Apparent Violation

of 10 CFR 50, Appendix B, Criterion

XVI, "Corrective

Actions" Restatement

of Apparent Violation 10 CFR Part 50, Appendix B, Criterion

XVI, "Corrective

Action," states, in part, that measures shall be established

to assure that conditions

adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective

material and equipment, and nonconformances

are promptly identified

and corrected

and for significant

conditions

adverse to quality, measures shall assure that the cause of the condition

is determined

and corrective

action taken to preclude repetition.

Contrary to this, the licensee failed to identify and correct the cause of the erratic EDG K-1 relay operation

prior to installation

of the relay on July 26, 2006. This failure resulted in the Unit 3 Train A EDG being inoperable

between September

4 and 22, 2006. This item has been entered into the licensee's

corrective

action program as CRDR 2926830. Pending determination

of safety significance, this finding is identified

as AV 05000530/2006012-02, "Failure to Identify and Correct a Condition

Adverse to Quality." 4

Admission APS admits these apparent violations.

Cause Personnel

attempted

to address the most likely cause of the failure first, and to determine

if this first cause, when corrected, addressed

the problem. This approach tries to ensure that actual causes are not masked by performing

multiple actions and then not knowing which action was the reason for solving the apparent problem. This narrow approach, however, did not consider all potential

failure possibilities

and was not successful

in identifying

the latent flaw in the set-up of the K-1 replacement

relay.When contact cleaning appeared to correct the performance

problem, as evidenced

by repeated manual, electrical

and in-service

tests, it was thought that the cause had been addressed.

APS acknowledges

the problem analysis efforts were narrowly focused, which led to an incorrect

conclusion

that the cause of the erratic relay operation

was solely due to oxidized contacts.

During the investigation

following

the September

22, 2006 failure, it was determined

that an opportunity

to identify the cause of failure was missed early in the July 25 investigation.

There was a lack of communication

between organizations (i.e., technicians

and engineers)

during the troubleshooting

and relay installation

process, which may have led to a realization

that more than contact oxidation

was involved.APS recognized

that this failure to correctly

identify the cause of the July 25, 2006 Unit 3, Train A, EDG K-1 relay failure had potential

organizational

and programmatic

elements and initiated

a specific investigation (CRDR 2950124) to identify any such issues. The analysis methodology

and preliminary

results of this investigation

are provided to demonstrate

that APS recognizes

that this specific equipment

failure is an opportunity

to reassess the adequacy of the problem analysis, troubleshooting

and cause evaluation

processes

being implemented

at Palo Verde.Instead of simply extrapolating

the organizational

and programmatic (O&P) root causes from this single event, the investigation

team took a broader look at all the barriers to minimize error in problem solving and root cause analysis at PVNGS in general. An independent

consultant

with failure mode analysis and O&P experience

was used in the assessment, working in conjunction

with PVNGS personnel.

The team identified

the possible failure modes that result in inconsistent

use of the problem solving methodology

to solve equipment

failures and evaluated

their effects.The team evaluated

the effectiveness

of barriers and determined

their contribution

to ineffective

cause analysis.

Finally, the team applied stream analysis to determine cause-effect

relationships

among the organization

and programmatic

failure modes.5

In summary, the team has preliminarily

identified

4 organizational

and programmatic

'root' causes and 6 'contributing'

causes. The root causes were: 1. Inconsistent

equipment

root cause of failure program management, resulting

in varying degrees of document quality.2. No formal problem solving and troubleshooting

process in place to establish evaluation

consistency.

3. Inconsistent

management

reinforcement

of the equipment

root cause of failure application

methodology

resulting

in inconsistent

evaluation

quality.4. Inconsistent

application

of a problem solving methodology, as evidenced

by varying degrees of rigor in root cause of failure determinations.

The contributing

causes were: 1. Inconsistent

consideration

of all failure modes (lack of formal troubleshooting

and problem solving process).2. No continuing

training on equipment

failure analysis methodology.

3. Operating

experience

was not typically

reviewed prior to opening components

for analysis (lack of formal problem solving and troubleshooting

process).4. Program to program interface

between corrective

maintenance

and the equipment

root cause of failure programs has allowed the equipment

root cause of failure process to be bypassed in some cases.5. Inconsistent

priority has been given to the equipment

failure analyses, resulting in less than acceptable

documentation.

6. Inappropriate

accountability

for meeting both timeliness

and quality expectations

on equipment

failure determinations.

Corrective

Actions Taken and Results Achieved Equipment

Actions Corrective

actions involved mechanical

adjustments

to the relay actuating

arm to provide adequate auxiliary

contact compression.

Additional

corrective

actions included inspecting, cleaning, and making mechanical

adjustments, as necessary, to all other affected EDG K-1 relays consistent

with detailed methodology

that determined

the proper amount of contact 'compression.'

These actions corrected

the direct cause of the September

22, 2006 Unit 3, Train A, EDG failure.Orqanizational

and Programmatic

Actions Completed

and on-going corrective

actions for the root and contributing

causes of the organizational

and programmatic

issues include elements of the Performance

Improvement

Plan and review of ERCFA reports by the Engineering

Product Review Board (EPRB).6

The Operations

decision making process (ODP-16) and the Engineering

human performance

tools (EDG-01 and 02) are considered

sufficient

interim action until the more extensive

planned actions are fully implemented.

Corrective

Actions to Be Taken Equipment

Actions APS plans to replace all of the EDG automatic

voltage regulators, including

replacement

of the K-1 relays, with a different

design during the next refueling

outage for each unit.This is the longer-term

equipment

corrective

action to prevent recurrence.

Related longer-term

corrective

actions resulting

from the root cause of failure analysis that address precluding

event recurrence

include:* Perform a review of the proposed modification

that will change the control and power components

of the diesel generator

excitation

systems. This review will include: o Method of de-excitation (e.g., type of relay to be used for field shorting, other types of field shorting devices used in the industry, reset circuit logic, circuit redundancy, etc.)o Evaluate the need for an annunciator

and alarm circuit on the field shorting relay.o Completeness

of vendor documentation (e.g., complete set of control documentation

from the prime and sub-component

suppliers, etc.)o PM's for the various newly installed

components (e.g., PM's on K-1 relay including

verification

of sufficient

contact 'compression.').(Due date: May 1, 2007)* Incorporate

the findings from the failure analysis into the current K-1 documentation (e.g., technical

manuals, operating

procedures, etc.) (Due date: August 31, 2007)" Evaluate the need for the field shorting components

of the diesel generator excitation

system. (Due date: August 31, 2007)* Evaluate installing

a jumper across the dc auxiliary

contact assembly normally open contact to eliminate

the potential

of the contact failing to close and making the EDG inoperable. (Due date: August 31, 2007)" Assess if there are other similar safety-related

circuits in the units where alarms need to be installed

to monitor the operability

of the circuit. (Due date: August 31,2007)* The final root cause analysis will assess the extent of cause and the extent of condition.

7

Organizational

and Programmatic

Actions Corrective

actions to be taken for each root and contributing

cause for the organizational

and programmatic

issues are as follows: The Plant Health Committee

will review the organizational

and programmatic

root cause evaluation. (Due date: February 28, 2007)Root Cause 1 -Inconsistent

equipment

root cause of failure analysis (ERCFA) program management, resulting

in varying degrees of ERCFA document quality.Corrective

Actions Establish

a single ERCFA program owner. (Due date: February 1, 2007)Establish

performance

indicators

for the ERCFA program. (Due date: April 1, 2007)Perform an ERCFA program self assessment. (Due date: March 1, 2007)Include the ERCFA program in procedure

73DP-OAP05, Engineering

Programs Management

and Health Reporting. (Due date: March 31, 2007)Establish

an ERCFA program improvement

plan. (Due date: April 1, 2007)Root Cause 2 -Lack of a formal problem solving and trouble shooting process to establish

ERCFA consistency.

Corrective

Actions Develop a troubleshooting

and problem solving process to be used by Operations, Maintenance

and Engineering.

Include as part of this process guidance and directions

on when and how to develop specific work or troubleshooting

instructions

in the absence of component

design instructions

or information. (Due date: February 1, 2007)Revise the ERCFA program to include the new problem solving process. (Due date: March 1, 2007)Provide training on the new process to selected Operations, Maintenance

and Engineering

personnel. (Due date: May 1, 2007)Root Cause 3 -Inconsistent

management

reinforcement

of ERCFA application

methodology, which resulted in inconsistent

quality of root cause of failure determinations.

Corrective

Actions Establish

a quality checklist

for EPRB and Corrective

Action Review Board review of ERCFA evaluations. (Due date: February 10, 2007)8

Ensure samples of ERCFA evaluations

are included in the next EPRB meeting (Due date: February 10, 2007)The existing Leadership

Performance

Improvement

Plan has established

common goals and the expectation

that the highest standards

of performance

and personal accountability

be pursued.Root Cause 4 -Inconsistent

application

of a systematic

problem solving methodology, resulting

in varying degrees of rigor in root cause of failure determinations

and quality of documented

evaluations.

Corrective

Actions Provide training to selected Operations, Maintenance

and Engineering

personnel on the new troubleshooting

and problem solving process. (Due date: May 1, 2007)Contributing

Cause 1 -Inconsistent

consideration

of all failure modes.Corrective

Actions Provide training to ERCFA qualified

engineers

that will include the need to consider all failure modes as part of initial troubleshooting

and root cause activities. (Due date: May 1, 2007)Contributing

Cause 2 -No continuing

training on equipment

failure analysis methodology.

Corrective

Actions Provide training to ERCFA-qualified

engineers

on changes to the ERCFA program. (Due date: May 1, 2007)Establish

periodic ERCFA industry events training. (Due date: March 31, 2007)Contributing

Cause 3 -Operating

experience

was not typically

reviewed prior to opening components

for analysis.Corrective

Actions Provide training to ERCFA qualified

engineers

that will include reviewing

any applicable

Operating

Experience

as part of the initial troubleshooting

and root cause activities. (Due date: May 1, 2007)Contributing

Cause 4 -Program to Program interface

between Corrective

Maintenance

and ERCFA programs allows the ERCFA process to be bypassed in some cases.9

Corrective

Actions Perform a self assessment

of ERCFA program, including

corrective

maintenance

interface, to identify appropriate

corrective

actions. (Due date: March 1, 2007)Contributing

Cause 5 -Inconsistent

priority has been given to the equipment

failure analyses, resulting

in less than acceptable

documentation.

Corrective

Actions Provide training to ERCFA qualified

engineers

that will include a discussion

of establishing

appropriate

priority to ensure a quality analysis. (Due date: May 1, 2007)The existing Leadership

Performance

Improvement

Plan has established

common goals and the expectation

that the highest standards

of performance

and personal accountability

be pursued.Contributing

Cause 6 -Inappropriate

accountability

for meeting both timeliness

and quality expectations

on ERCFA determinations.

Corrective

Actions Establish

a single ERCFA program owner. (Due date: February 1, 2007)Provide training to ERCFA qualified

engineers

that will include a discussion

of accountability

and expectations

for both quality and timeliness. (Due date: May 1, 2007)The existing Leadership

Performance

Improvement

Plan has established

common goals and the expectation

that the highest standards

of performance

and personal accountability

be pursued.An effectiveness

review will be established

to ensure the equipment

failure analysis program improvements

are achieving

the desired results. Performance

indicators

established

as part of the above corrective

actions will be used to monitor performance.

4 -Conclusion

APS realizes the troubleshooting

and problem solving process lacked the technical

rigor necessary

to ensure deficiencies

were properly identified

and resolved the first time. In this case, the failure to consider all possible causes of the July K-1 relay failure resulted in a subsequent

failure in September.

Immediate

actions have been taken to assure the EDGs remain within their design basis. Additional

actions to address the programmatic

weaknesses

have been identified

to provide greater assurance

that similar events will not occur.10