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| | issue date = 11/30/2008 | | | issue date = 11/30/2008 |
| | title = Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containm | | | title = Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containm |
| | author name = Conte R J, Richmond J E | | | author name = Conte R, Richmond J |
| | author affiliation = NRC/RGN-I | | | author affiliation = NRC/RGN-I |
| | addressee name = | | | addressee name = |
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Category:NRC Preliminary Notification of Event/Occurrence
MONTHYEARML12320A0202012-11-14014 November 2012 Update: PNO-I-12-007A Hurricane Sandy Update Causes Oyster Creek Alert and Shutdowns of Reactors at Nine Mile Point Unit 1, Indian Point Unit 3 and Salem Unit 1 PNO-I-12-007, Hurricane Sandy Causes Oyster Creek Alert and Shutdowns of Reactors at Nine Mile Point Unit 1, Indian Point Unit 3, and Salem Unit 12012-10-31031 October 2012 PNO-I-12-007 - Hurricane Sandy Causes Oyster Creek Alert and Shutdowns of Reactors at Nine Mile Point Unit 1, Indian Point Unit 3, and Salem Unit 1 PNO-I-12-005, Oyster Creek Reactor Shutdown and Unusual Event Due to a Loss of Offsite Power and Shutdown Greater than 72 Hours2012-07-31031 July 2012 PNO-I-12-005 - Oyster Creek Reactor Shutdown and Unusual Event Due to a Loss of Offsite Power and Shutdown Greater than 72 Hours ML1123601032011-08-23023 August 2011 PNO-II-11-005: North Anna, Emergency Declarations Due to Seismic Event PNO-I-09-005, A: Update: Oyster Creek Reactor Trip and Unusual Event Due to a Loss of Offsite Power and Shutdown Greater than 72 Hours2009-07-17017 July 2009 PNO-I-09-005A: Update: Oyster Creek Reactor Trip and Unusual Event Due to a Loss of Offsite Power and Shutdown Greater than 72 Hours ML0919604862009-07-15015 July 2009 PNO-I-09-005: Exelon Generation Co. Llc., Oyster Creek Reactor Trip and Unusual Event Due to a Loss of Offsite Power and Shutdown Greater than 72 Hours PNO-I-09-002, A: Oyster Creek, Update - Shutdown Greater than 72 Hours: Manual Reactor Scram Following Loss of Cooling to Main Transformer, Dated 05/04/20092009-05-0404 May 2009 PNO-I-09-002A: Oyster Creek, Update - Shutdown Greater than 72 Hours: Manual Reactor Scram Following Loss of Cooling to Main Transformer, Dated 05/04/2009 ML0911706642009-04-27027 April 2009 PNO-I-09-002 - Oyster Creek, Shutdown Greater than 72 Hours: Manual Reactor Scram Following Loss of Cooling to Main Transformer PNO-I-09-001, A: Exelon Generation Company, LLC, Update - Oyster Creek Unusual Event and Automatic Reactor Scram Due to Fire in M1A Main Transformer2009-02-0505 February 2009 PNO-I-09-001A: Exelon Generation Company, LLC, Update - Oyster Creek Unusual Event and Automatic Reactor Scram Due to Fire in M1A Main Transformer ML0903304152009-02-0202 February 2009 PNO-I-09-001: Unusual Event and Automatic Reactor Scram Due to a Fire in the M1A Main Transformer at Oyster Creek Station PNO-I-08-013, A - Update - Oyster Creek: Automatic Reactor Scram Due to Main Transformer Fault2008-12-0505 December 2008 PNO-I-08-013A - Update - Oyster Creek: Automatic Reactor Scram Due to Main Transformer Fault ML0833602712008-12-0101 December 2008 PNO-I-08-013: Shutdown Greater than 72 Hrs: Automatic Reactor Scram Due to Main Transformer Fault - Oyster Creek ML0914703712008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containm ML0914703692008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek Renewal Commitments Related to the Drywall Primary Containm ML0914703702008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywell Primary ML0914703722008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containm ML0914804412008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containm ML0914804422008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywall Primary ML0914804432008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywall Primary ML0914804442008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containm ML0914804452008-11-30030 November 2008 Draft Preliminary Notification of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Primary Containment Drywe ML0914804462008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Facility Amergen Energy Company, LLC, Oyster Creek, Subject - Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywell Primary ML0919605922008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX, Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywell Primary Containment ML0919605932008-11-30030 November 2008 Draft Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-XXX Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywell Primary Containment ML0911907252008-11-17017 November 2008 Preliminary Notification of Event of Unusual Occurrence, PNO-1-08-012; Subject Results of Implementation of Oyster Creek License Renewal Commitments Related to the Drywell Primary Containment, with Hand Written Notes ML0911906532008-11-17017 November 2008 E-mail from K. Heater of USNRC to Various, Regarding PNO-I-08-012: Oyster Creek - Results of Implementation of License Renewal Commitments ML0914606862008-11-14014 November 2008 E-mail from J. Richmond of USNRC to Various, Regarding Oc PNO - Nov 2008 Drywell Rev 3 ML0919004242008-11-0707 November 2008 E-mail from R. Conte of USNRC to J. Richmond, D. Tifft and D. Pelton of USNRC, Regarding Oyster Creek Preliminary Notification(Draft) and Communications Plan, Rev. 1 PNO-I-07-006, A - NRC Resident Inspector - Update - Reactor Scram on Low Reactor Vessel Water Level Due to a Trip of the 'C' Reactor Feed Pump2007-07-23023 July 2007 PNO-I-07-006A - NRC Resident Inspector - Update - Reactor Scram on Low Reactor Vessel Water Level Due to a Trip of the 'C' Reactor Feed Pump ML0719904282007-07-17017 July 2007 PNO-I-07-006: Reactor Scram on Low Reactor Vessel Water Level Due to a Trip of the C Reactor Feed Pump PNO-I-06-012, Oyster Creek, Evaluation of Containment Design Function2006-11-0909 November 2006 PNO-I-06-012: Oyster Creek, Evaluation of Containment Design Function PNO-I-05-022, Alert Declaration at Oyster Creek2005-08-0808 August 2005 PNO-I-05-022 - Alert Declaration at Oyster Creek ML0713401372003-05-22022 May 2003 Reactor Operating Events Event Notification Report, Event Number: 39876; Facility: Oyster Creek; Notification Date: 05/22/2003 PNO-I-03-016, Oyster Creek Bargaining Unit Strike at Oyster Creek (39876)2003-05-22022 May 2003 PNO-I-03-016: Oyster Creek Bargaining Unit Strike at Oyster Creek (#39876) PNO-I-02-020, Unusual Event Due to a Hydrogen Gas Ignition in the Off-Gas System (39348)2002-11-0707 November 2002 PNO-I-02-020: Unusual Event Due to a Hydrogen Gas Ignition in the Off-Gas System (#39348) 2012-07-31
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i.-4 Preliminary Notification G:\DRS\Engineering Branch 1\_LicRenewal\Oyster Creek\2008 Outage\Backup\OC PNO Nov-2008_Drywellrev-l.doc DCS No.: 05000219110XX08 Date: November XX, 2008 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PNO-1-08-XXX Facility Licensee Emergency Classification AmerGen Energy Company, LLC Notification of Unusual Event Oyster Creek Alert Forked River, New Jersey Site Area Emergency Docket: 50-219 General Emergency X Not Applicabl
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Subject:
RESULTS OF IMPLEMENTATION OF OYSTER CREEK LICENSE RENEWAL COMMITMENTS RELATED TO THE PRIMARY CONTAINMENT (DRYWELL)The NRC staff conducted an on-site inspection of ArnerGen's actions related to license renewal commitments to be implemented during the 2008 refueling outage at the Oyster Creek Nuclear Generating Station (OCNGS). In particular, the NRC review a multi-week inspection of AmerGen's three aging management associated with the primary containment (drywell):
Containment Metallic Liner Inservice Inspection; Structures Monitoring Program; and Protective Coating Monitoring and Maintenance Program. In accordance with the NRC's agreement with the State of New Jersey, State Engineer s)Pberved portions of the NRC's staff review. Based on the resultsof the NRC's inspection activities to date, the NRC staff concluded there were no safety si'nificant conditions with respect to the primary containment that would prohibit plant startup.<In the mid-1 980s, GPU Niclear (p'revi'ous licensee) identified corrosion of the drywell containment steel shell, in the sand bed egion. Initial licensee actions were not effective in arresting corrosion.
In 1992, all sand was removed from the sand bed region and the accessible exterior sufaces of the dry-welshell were cleaned and coated with epoxy. Ultrasonic test (UT) measurementsrof the dayweli shell taken in 1992 and 1996 indicated the corrosion had been effectively arrested.
This inforna:tion was confirmed in 2006, during a refueling outage.On October 24, 2008, OCNGS shut down for a refueling and maintenance outage. Scheduled outage work implenmentation of various license renewal aging management programs.During the 2008 refueling the NRC's drywell shell inspection focused on: 1. Results of drywell shell UT thickness measurements.
- 2. Direct observation of drywell shell conditions both inside the drywell, including the floor trenches, and outside the drywell, in the sand bed regions.3. Condition and integrity of the drywell shell epoxy coating, including AmerGen's activities to evaluate and repair four small coating blisters found in Bay-1 1.4. Condition and integrity of the drywell shell moisture barrier seal between the shell and the sand bed floor, including AmerGen's activities to evaluate and repair identified cracks in moisture barrier seals in multiple sand bed bays, including a seal crack in Bay-3 which also exhibited small rust stains.5. AmerGen's activities to monitor, evaluate, mitigate water leakage from the reactor refueling r ;Preliminary Notification cavity onto the external surface of the drywell shell and into the sand bed regions.On a sampling basis, the NRC staff had the following observations of Amergen's implementation of license renewal commitments, during the 2008 refueling outage: 1. All drywell shell UT thickness measurements satisfied AmerGen's acceptance criteria and current licensing basis design requirements.
- 2. There were no identified significant conditions affecting the drywell shell structural integrity.
As described below, there were several problems identified during AmerGen's implementation of license renewal commitments.
- 3. The as-found condition of the external drywell shell epoxy coating, in the sand bed regions, was acceptable, except for four small coating blisters found in Bay-1 1. The blisters were repaired.
AmerGen reported that some blistering was expected, nd would be identified during routine visual examinations.
The NRC staff will1review AmerQIn s cause evaluation when it is complete.4. The as-found condition of the external drywellshell, moisture barrier seal between the shell and the sand bed floor, was acceptable, exxcqdfor multiple surface cracks, Which did not appear to completely penetrate the seal. The~idlntified seal cracks were repair>&d.
During one crack repair, in Bay-3, some drywell shell surface corrosion was identified and repaired.5. AmerGen's activities to monitor and mitigate water lea~kagefrom the reactor refueling cavity onto the external surface of the drywellt/shell and intothe sand bed regions was, in general, acceptable, with a few noted a .described below.On the fourteenth day of outage, water leakage froI the reactorrefueling cavity into the cavity drain trough, as monitored in theetrough's drain line icreased-from less than 1 gallon per minute (gpm) to approximately 5.to 7 gpm. ll-over freom the cavity drain trough appeared to occur, which resulted n some wat entry into the sand bed region. AmerGen enhanced it's leakage monitoring, renopened all'sand bed bays, and performed visual inspections to water enty. Water pud dles were identified in several sand bed bays.After the cavity was drained and e.aleakage.stoppl, NRC and AmerGen performed direct inspections of the sand bedbys, no adaversgemonditions were identified.
To determine whether any .eshei may have occurred, as a result of this leakage, AmerGen stated additional UM.ti"knessr asurements would be performed in the next refueling outage, in 20, AmerGe, identified and fixgd problemr found in sand bed Bay-3 and Bay-i 1, during license renewal ag]panagement program implementation.
The drywell shell epoxy coating and the moisture barniýeseals, both ie sand bed region, are barrier systems used to protect the drywell shell frofm crrosion.
The problems identified with these barriers had a minimal impact on the drywell shel11' d theprojected shell corrosion rate remained very small.Based on a review of the technical information, the NRC staff determined AmerGen had an adequate basis to restart OCNGS.The State of New Jersey has been notified and no further updates are planned.This PN is being issued for information only and will not be updated.ADAMS Accession Number: ML .....................
CONTACT: Richard J. Conte John Richmond Preliminary Notification
(@nrc.gov (610) 337-5183 (610) 337-5220* ,\: