ML18067A709: Difference between revisions
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| issue date = 10/09/1997 | | issue date = 10/09/1997 | ||
| title = Forwards Response to Violations Noted in Insp Rept 50-255/97-08.Corrective Actions:Operating Procedures Have Been Revised to Better Define Safety State & Prohibit Operation at Steady State Power Level Greater than Limit | | title = Forwards Response to Violations Noted in Insp Rept 50-255/97-08.Corrective Actions:Operating Procedures Have Been Revised to Better Define Safety State & Prohibit Operation at Steady State Power Level Greater than Limit | ||
| author name = | | author name = Palmisano T | ||
| author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.), | | author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.), | ||
| addressee name = | | addressee name = | ||
Revision as of 18:01, 17 June 2019
| ML18067A709 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 10/09/1997 |
| From: | Thomas J. Palmisano CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| 50-255-97-08, 50-255-97-8, NUDOCS 9710150161 | |
| Download: ML18067A709 (6) | |
See also: IR 05000255/1997008
Text
- Consumers
Ener9i')>
October 9, 1997 U.S. Nuclear Regulatory
Commission
ATIN: Document Control Desk
Washington, DC 20555 DOCKET 50-255 -LICENSE DPR-20 -PALISADES
PLANT -=: '3: t5 ... '3J 2290 .-.: .... s: c -5..:
Tlloma* J. Palmluno Site Vice President
REPLY TO NOTICE OF VIOLATION
50-255/97008-01
-PLANT PROCEDURES
ALLOW STEADY STATE POWER LEVEL GREATER THAN LICENSE LIMIT NRC Inspection
Report No. 50-255/97008(DRP)
dated September
5, 1997, contained
for a Severity Level IV violation
concerning
the potential
to exceed the licensed full power limit. Attachment
1 contains our response to the violation.
The response to the violation
was required to be submitted
within 30 days from the date of the letter transmitting
the violation.
Discussion
with Bruce Burgess at Region Ill on September
23, 1997, confirmed
that the 30-day requested
response could be provided within 30 days of receipt of the letter, which was September
11, 1997. '-The inspection
cover letter also noted a continuing
weakness with post maintenance
testing and an example of weak ALARA planning.
These two weaknesses
are being addressed
and status of our efforts in this area will be submitted
in a separate letter. 9710150161 ADOCK PDR 1111111111111111111111111111111111111111
- 18 9 7 11 11 2 *
- * SUMMARY OF COMMITMENTS
This letter contains no new commitments
and no revisions
to existing commitments. Thomas J. Palmisano
Site Vice President
CC Administrator, Region Ill, USNRC Project Manager, NRR, USNRC NRC Resident Inspector
-Palisades
Attachment
2
ATTACHMENT
1 CONSUMERS
ENERGY COMPANY PALISADES
PLANT DOCKET 50-255 REPLY TO NOTICE OF VIOLATION
PLANT PROCEDURES
ALLOW STEADY STATE POWER LEVEL GREATER THAN LICENSE LIMIT 3 Pages
NRC VIOLATION
During an NRG inspection
conducted
on May 24 through July 7, 1997, one violation
of NRG requirements
was identified.
In accordance
with the "General Statement
of Policy and Procedure
for NRG Enforcement
Actions," NUREG 1600, the violation
is listed below: 10 CFR 50, Appendix B, Criterion
V, "Instructions, Procedures, and Drawings," requires, in part, that activities
affecting
quality shall be prescribed
by documented
instructions, procedures, or drawings, of a type appropriate
to the circumstances
and shall be accomplished
in accordance
with these instructions, procedures
and drawings.
Palisades
Plant Facility Operating
License, section 2.c.(1), states, in part, that "CPCo is authorized
to operate the facility at steady-state
reactor core power levels not in excess of 2530 megawatts
thermal (100 percent rated power) in accordance
with the conditions
specified
herein." Contrary to the above, on February 7, 1996, the operations
shift conducted
an activity affecting
quality, the delithiation
of the Reactor Coolant System, using General Operating
Procedure (GOP)-12, Revision 12, Section 5. 3. 1 a, a procedure
inappropriate
to the circumstances
in that it allowed plant operators
to operate the plant at 100.99 percent power (2555 megawatts
thermal}, a steady state power level greater than the license limit. ' This is a Severity Level IV violation (Supplement
I) CONSUMERS
ENERGY COMPANY RESPONSE Consumers Energy
agrees that the facts are as stated. General Operating
Procedure (GOP) -12 as written would have allowed plant operators
to operate the plant at a steady state power level greater than the license limit. Uncertainty
analyses combined with follow..:up
ultrasonic
flow measurements, however, reveal that neither the licensing
nor design bases were exceeded throughout
this event. ' BACKGROUND
On February 7, 1996, during a planned delithiation
of the reactor coolant system, a slight increase in the plant power level was observed.
The power level was controlled
and monitored
in compliance
with the existing procedures
and resulted in an indicated
1
plant power level slightly in excess of 100% of licensed power for nine consecutive
hours. Initial investigation
of the involved measurement
uncertainties
led to the event being reported as LER 96-006 on March 11, 1996, as a condition
possibly outside of the design basis and in violation
of a license condition
which requires that the plant not be operated in excess of 2530 Megawatts
thermal (100% rated power levels). Palisades'
procedures
had considered
this license condition
steady state limit to be met if reactor power averaged over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> was below 2530 megawatts.
Minor excursions
above 100 percent power were viewed as acceptable
as long as peak power did not exceed 101 percent and the 24-hour average power was less than 2530 megawatts.
The slow power rise during delithiation
was viewed as a transient
condition
not subject to the steady state limit specified
in the license. During a later review of power level records, questions
were raised about whether
averaging
was the appropriate
standard to assure license compliance, and whether measurement
uncertainties
were adequately
considered
in the procedure
limit on peak power. Subsequent
tests and analyses have shown that Palisades
did not exceed the 10 CFR 50.2 design basis and did not exceed 100% power during the period in question.
This conclusion
was reported to the NRC on August 2, 1996, as Supplement
1 to LER 96-006. EVENT ANALYSIS Two separate actions were taken during the investigation
of this event. These actions were: 1. The calorimetric
uncertainty
analysis was redone to more accurately
reflect the calorimetric
uncertainty.
This analysis was rigorously
reviewed by Consumers
Energy Company and an outside contractor
with significant
in uncertainty
analyses.
2. An ultrasonic
flow measurement (UFM) of the feedwater
flow was performed
on May 21-22, 1996 to assess the plant thermal performance.
The UFM provided a more accurate measurement
of feedwater
flow independent
of the installed
venturies.
The final results from the calorimetric
uncertainty
analysis showed the uncertainty
to be 1.01 %. Wl:ten this c:;alorimetric
uncertainty
of 1.01 % is added to the maximum power level recorded (100.41%), the resulting
value is within the Palisades
Design Basis value of 102%. It is, therefore, concluded
by this analysis that actual reactor power did not exceed the design basis value throughout
this event. 2
!' ,, i The results of the more accurate UFM revealed that actual power was 2.2% less than indicated
power based on the feedwater
venturies.
The conservative
bias associated
with the venturies
is due primarily
to a conservative
initial venturi calibration
and to venturi fouling. The UFM device is considered
to be more accurate than the venturies
due to rigorous testing by the vendor and the device's independence
from fouling. Using the ultrasonic
flow results, the maximum power level achieved during the event was determined
to be 98.2%. It has, therefore, been concluded
that Palisades'
actual reactor power did not exceed 100% licensed power throughout
the event. REASON FOR THE VIOLATION
- The root cause for the event was that the procedural
guidance for the operators
regarding
compliance
with licensed steady-state
reactor core power levels was not sufficiently
conservative.
CORRECTIVE
STEPS TAKEN AND RESULTS ACHIEVED The following
corrective
actions were accomplished:
Operating
procedures
have been revised to better define *isteady state" and prohibit operation
at a steady state power level greater than the license limit. The calorimetric
uncertainty
analysis was reviewed to verify that it reflected
known uncertainties.
The analysis revealed that Palisades
remained within the established
design basis at all times. A flow test using UFM was performed
on May 21-22, 1996. The results of the flow measurement
revealed that the installed
flow venturies
have a conservative
bias. This resulted in the indicated
reactor power reading higher than the actual power. The measurement
results indicated
that 100% power was not exceeded throughout
the event. CORRECTIVE
STEPS TAKEN TO AVOID FURTHER VIOLATIONS
No additional
actions are required.
DATE WHEN FULL COMPLIANCE
WILL BE ACHIEVED Full compliance
was achieved on March 11, 1996, when the appropriate
procedures
were revised. 3