ENS 40604: Difference between revisions
Jump to navigation
Jump to search
StriderTol (talk | contribs) (Created page by program invented by Mark Hawes) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
Line 16: | Line 16: | ||
| event date = 03/22/2004 19:31 CST | | event date = 03/22/2004 19:31 CST | ||
| last update date = 03/22/2004 | | last update date = 03/22/2004 | ||
| title = Reactor Scram | | title = Reactor Scram from 93% Power Due to Generator Trip | ||
| event text = The plant had a reactor SCRAM, cause is under investigation with initial indications of a Main Generator over voltage alarm and Generator lockout #2 were indicated on the Generator first hit panel. All plant systems responded as expected to the generator trip and Reactor SCRAM. All rods fully inserted and no ECCS actuations or relief valves lifted. The plant is stable in Mode 3 with the recovery plan being implemented. | | event text = The plant had a reactor SCRAM, cause is under investigation with initial indications of a Main Generator over voltage alarm and Generator lockout #2 were indicated on the Generator first hit panel. All plant systems responded as expected to the generator trip and Reactor SCRAM. All rods fully inserted and no ECCS actuations or relief valves lifted. The plant is stable in Mode 3 with the recovery plan being implemented. | ||
The NRC Resident Inspector was notified. | The NRC Resident Inspector was notified. |
Latest revision as of 21:23, 1 March 2018
Where | |
---|---|
Clinton Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-2.52 h-0.105 days <br />-0.015 weeks <br />-0.00345 months <br />) | |
Opened: | Edward Beck 23:00 Mar 22, 2004 |
NRC Officer: | Chauncey Gould |
Last Updated: | Mar 22, 2004 |
40604 - NRC Website
| |