ENS 46032: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by Mark Hawes)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 06/19/2010 06:36 CDT
| event date = 06/19/2010 06:36 CDT
| last update date = 06/19/2010
| last update date = 06/19/2010
| title = Manual Reactor Trip Due To Generator Lockout
| title = Manual Reactor Trip Due to Generator Lockout
| event text = At 0636 hours, control room personnel initiated a manual reactor trip of Unit 2 from MODE 2 at 0% power. Just prior to the initiation of the manual reactor trip, an automatic turbine trip had occurred as a result of the receipt of a generator lockout signal. Prior to the automatic turbine trip, an orderly power reduction to 44% power had been completed and the unit was being maintained in a stable condition in MODE 1. At the time of the turbine trip, two sets of condenser steam dump valves were isolated, in preparation for scheduled condenser waterbox tube cleaning. Following the manual reactor trip, all safety systems and equipment operated as expected. The cause of the turbine trip, including receipt of the generator lockout signal, is under investigation. The unit is stable in MODE 3 at normal RCS temperature and pressure.
| event text = At 0636 hours, control room personnel initiated a manual reactor trip of Unit 2 from MODE 2 at 0% power. Just prior to the initiation of the manual reactor trip, an automatic turbine trip had occurred as a result of the receipt of a generator lockout signal. Prior to the automatic turbine trip, an orderly power reduction to 44% power had been completed and the unit was being maintained in a stable condition in MODE 1. At the time of the turbine trip, two sets of condenser steam dump valves were isolated, in preparation for scheduled condenser waterbox tube cleaning. Following the manual reactor trip, all safety systems and equipment operated as expected. The cause of the turbine trip, including receipt of the generator lockout signal, is under investigation. The unit is stable in MODE 3 at normal RCS temperature and pressure.
This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) t and 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been notified.
This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) t and 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been notified.

Latest revision as of 22:09, 1 March 2018

ENS 46032 +/-
Where
Point Beach NextEra Energy icon.png
Wisconsin (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-0.18 h-0.0075 days <br />-0.00107 weeks <br />-2.46564e-4 months <br />)
Opened: Kile Hess
11:25 Jun 19, 2010
NRC Officer: Joe O'Hara
Last Updated: Jun 19, 2010
46032 - NRC Website
Loading map...