ENS 49454: Difference between revisions

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| event date = 10/19/2013 03:31 EDT
| event date = 10/19/2013 03:31 EDT
| last update date = 10/19/2013
| last update date = 10/19/2013
| title = Group 1 Isolation Due To High Reactor Water Level
| title = Group 1 Isolation Due to High Reactor Water Level
| event text = On Saturday, October 19, 2013 at 0331 hours, with the reactor critical at approximately 1% core thermal power and the mode switch in start-up, a high reactor water level condition resulted in a main turbine trip and a valid Group 1 isolation signal. As a result, the Main Steam Isolation Valves (MSIVs) closed.
| event text = On Saturday, October 19, 2013 at 0331 hours, with the reactor critical at approximately 1% core thermal power and the mode switch in start-up, a high reactor water level condition resulted in a main turbine trip and a valid Group 1 isolation signal. As a result, the Main Steam Isolation Valves (MSIVs) closed.
The plant was in start-up from a forced outage. The initial plant conditions were reactor pressure at approximately 280 psig with a corresponding reactor coolant temperature for that pressure. Currently reactor pressure and water level are being maintained with the MSIVs closed in normal bands. The reactor is being cooled down in preparation for operation in shutdown cooling. Off-site power is supplying station power from the Start-up Transformer (normal power supply for shutdown operations). All plant systems responded as designed.
The plant was in start-up from a forced outage. The initial plant conditions were reactor pressure at approximately 280 psig with a corresponding reactor coolant temperature for that pressure. Currently reactor pressure and water level are being maintained with the MSIVs closed in normal bands. The reactor is being cooled down in preparation for operation in shutdown cooling. Off-site power is supplying station power from the Start-up Transformer (normal power supply for shutdown operations). All plant systems responded as designed.

Latest revision as of 21:52, 1 March 2018

ENS 49454 +/-
Where
Pilgrim
Massachusetts (NRC Region 1)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
LER: 05000293/LER-2013-010
Time - Person (Reporting Time:+2.43 h0.101 days <br />0.0145 weeks <br />0.00333 months <br />)
Opened: Ken Goodall
09:57 Oct 19, 2013
NRC Officer: Charles Teal
Last Updated: Oct 19, 2013
49454 - NRC Website
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