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{{#Wiki_filter:NUCLEAR OPERATING CORPORATIONSteven R. KoenigManager Regulatory AffairsMarch 4, 2015RA 15-0013U. S. Nuclear Regulatory CommissionATTN: Document Control DeskWashington, DC 20555
{{#Wiki_filter:NUCLEAR OPERATING CORPORATION Steven R. KoenigManager Regulatory AffairsMarch 4, 2015RA 15-0013U. S. Nuclear Regulatory Commission ATTN: Document Control DeskWashington, DC 20555


==Subject:==
==Subject:==
Docket No. 50-482:Evaluation ReportWolf Creek Generating Station Biennial 50.59Gentlemen:This letter transmits the Biennial 50.59 Evaluation Report for Wolf Creek Generating Station(WCGS), which is being submitted pursuant to 10 CFR 50.59(d)(2). The attachment providesthe WCGS Biennial 50.59 Evaluation Report including a summary of the evaluation results.This report covers the period from January 1, 2013, to December 31,2014, and contains asummary of 50.59 evaluations implemented during this period that were approved by theWCGS onsite review committee.This letter contains no commitments. If you have any questions concerning this matter, pleasecontact me at (620) 364-4041.SRK/rltAttachmentcc: M. L. Dapas (NRC), w/aC. F. Lyon (NRC), w/aN. F. O'Keefe (NRC), w/aSenior Resident Inspector (NRC), w/a41V-1%0CLP.O. Box 411 / Burlington, KS 66839 / Phone: (620) 364-8831An Equal Opportunity Employer M/F/HCNET Attachment RA 15-0013Page 1 of 11WOLF CREEK NUCLEAR OPERATING CORPORATIONWolf Creek Generating StationDocket No.: 50-482Facility Operating License No.: NPF-42BIENNIAL 50.59 EVALUATION REPORTReport No.: 24Reporting Period: January 1, 2013 through December 31, 2014 Attachment RA 15-0013Page 2 of 11SUMMARYThis report provides a brief description of changes, test, and experiments implemented at WolfCreek Generating Station (WCGS) and evaluated pursuant to 10 CFR 50.59(c)(1). This reportincludes summaries of the associated 50.59 evaluations that were reviewed and found to beacceptable by the Plant Safety Review Committee (PSRC) for the period beginning January 1,2013 and ending December 31, 2014. This report is submitted in accordance with therequirements of 10 CFR 50.59(d)(2).On the basis of these evaluation of changes:" There is less than a minimal increase in the frequency of occurrence of an accidentpreviously evaluated in the Updated Final Safety Analysis Report (USAR)." There is less than a minimal increase in the likelihood of occurrence of a malfunctionof a structure, system, or component (SSC) important to safety previously evaluatedin the USAR." There is less than a minimal increase in the consequences of an accident previouslyevaluated in the USAR." There is less than a minimal increase in the consequences of a malfunction of anSSC important to safety previously evaluated in the USAR." There is no possibility for an accident of a different type than any previouslyevaluated in the USAR being created.* There is no possibility for a malfunction of a SSC important to safety with a differentresult than any previously evaluated in the USAR being created." There is no result in a design basis limit for a fission product barrier as described inthe USAR being exceeded or altered." There is no result in a departure from a method of evaluation described in the USARused in establishing the design bases or in the safety analyses.Therefore, all items contained within this report have been determined not to require a licenseamendment.
Docket No. 50-482:Evaluation ReportWolf Creek Generating Station Biennial 50.59Gentlemen:
Attachment RA 15-0013Page 3 of 11Evaluation Number: 59 2012-0002 Revision: 0Title: Turbine Control System (TCS) UpgradeActivity
This letter transmits the Biennial 50.59 Evaluation Report for Wolf Creek Generating Station(WCGS), which is being submitted pursuant to 10 CFR 50.59(d)(2).
The attachment providesthe WCGS Biennial 50.59 Evaluation Report including a summary of the evaluation results.This report covers the period from January 1, 2013, to December 31,2014, and contains asummary of 50.59 evaluations implemented during this period that were approved by theWCGS onsite review committee.
This letter contains no commitments.
If you have any questions concerning this matter, pleasecontact me at (620) 364-4041.
SRK/rltAttachment cc: M. L. Dapas (NRC), w/aC. F. Lyon (NRC), w/aN. F. O'Keefe (NRC), w/aSenior Resident Inspector (NRC), w/a41V-1%0CLP.O. Box 411 / Burlington, KS 66839 / Phone: (620) 364-8831An Equal Opportunity Employer M/F/HCNET Attachment RA 15-0013Page 1 of 11WOLF CREEK NUCLEAR OPERATING CORPORATION Wolf Creek Generating StationDocket No.: 50-482Facility Operating License No.: NPF-42BIENNIAL 50.59 EVALUATION REPORTReport No.: 24Reporting Period: January 1, 2013 through December 31, 2014 Attachment RA 15-0013Page 2 of 11SUMMARYThis report provides a brief description of changes, test, and experiments implemented at WolfCreek Generating Station (WCGS) and evaluated pursuant to 10 CFR 50.59(c)(1).
This reportincludes summaries of the associated 50.59 evaluations that were reviewed and found to beacceptable by the Plant Safety Review Committee (PSRC) for the period beginning January 1,2013 and ending December 31, 2014. This report is submitted in accordance with therequirements of 10 CFR 50.59(d)(2).
On the basis of these evaluation of changes:" There is less than a minimal increase in the frequency of occurrence of an accidentpreviously evaluated in the Updated Final Safety Analysis Report (USAR)." There is less than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component (SSC) important to safety previously evaluated in the USAR." There is less than a minimal increase in the consequences of an accident previously evaluated in the USAR." There is less than a minimal increase in the consequences of a malfunction of anSSC important to safety previously evaluated in the USAR." There is no possibility for an accident of a different type than any previously evaluated in the USAR being created.* There is no possibility for a malfunction of a SSC important to safety with a different result than any previously evaluated in the USAR being created." There is no result in a design basis limit for a fission product barrier as described inthe USAR being exceeded or altered." There is no result in a departure from a method of evaluation described in the USARused in establishing the design bases or in the safety analyses.
Therefore, all items contained within this report have been determined not to require a licenseamendment.
Attachment RA 15-0013Page 3 of 11Evaluation Number: 59 2012-0002 Revision:
0Title: Turbine Control System (TCS) UpgradeActivity  


== Description:==
==
The WCGS Turbine Control System (TCS) was upgraded by replacement of the existingGeneral Electric Mark II Electro-Hydraulic Control (EHC) system and Emergency Trip System(ETS), with a Distributed Control System (DCS) supplied by Westinghouse. The replacementsystem is based upon the Ovation platform supplied by Emerson Process Management (EPM).The main turbine control system is designed to prevent turbine overspeed in the event of asudden loss of load using multiple levels of component redundancy and diversity. Failure of anysingle component will not result in a turbine rotor speed exceeding the design overspeed of 120percent of rated speed, or 2160 RPM. The function and performance of the TCS, as describedin the USAR, is not being changed, with the exception being the replacement of the existingmechanical-hydraulic overspeed trip based upon the centrifugal principle with an alternate morereliable design.50.59 Evaluation:The TCS is non-safety related and the modification does not change the function orperformance requirements for the system as described in the USAR. The TCS upgrade doesnot increase any plant operating parameters that would result in increased challenges toimportant safety components or the frequency of any accident described in the USAR. No newinterface requirements with important to safety components that function to limit theconsequences of an accident are established by this upgrade.The WCGS specific TCS upgrade Software Hazards Analysis (SHA) evaluated the TCSupgrade related system-level hazards to ensure that the results would be bounded by theresults of malfunctions or accidents previously considered in the USAR.The evaluation determined that the results of potential TCS upgrade failures are enveloped bythe current USAR Chapter 15 analyses.An SHA review of the WCGS USAR Chapter 15 events was performed to identify any newsystem-level hazards with regard to the digital TCS upgrade. No new system-level hazards orfailure modes were identified as a result of this review.An SHA evaluation of sub-system level software failures, including software common causefailures and cyber security events/cyber-attacks, to determine their impact on the identifiedsystem-level hazards, concluded that potential sub-system level software failures would notlead to different types of accidents or impact plant USAR analyses.A turbine trip evaluation determined the total system failure probability of both the existing TCSand the upgraded TCS to be essentially identical, 1.142E-6 and 1.08E-6 respectively.
Description:==
Attachment RA 15-0013Page 4 of 11Evaluation Number: 59 2012-0003 Revision: 0Title: Replace current Number 1 Seal inserts in the four Wolf Creek Model 93A-1 ReactorCoolant Pumps (RCP's) with a modified design called the Shield Shutdown Seal(SDS)Activity


== Description:==
The WCGS Turbine Control System (TCS) was upgraded by replacement of the existingGeneral Electric Mark II Electro-Hydraulic Control (EHC) system and Emergency Trip System(ETS), with a Distributed Control System (DCS) supplied by Westinghouse.
The Number 1 Seal inserts in the four Wolf Creek Model 93A-1 Reactor Coolant Pumps (RCPs)were replaced with a modified design called the Shield Shutdown Seal (SDS). The affectedSystems, Structures, Components (SSC's) are the Number 1 Seal inserts in RCPs PBB01A, B,C, and D. The activity includes the preparation of design and configuration change documents,procurement, and actual installation of the SDS in Refuel 19.The SDS integrated new features into the existing Number 1 Seal insert and is locateddownstream of the current film-riding face seal. A shoulder is machined into the inner diameterat the top flange and bore machined into the groove diameter above the shoulder. SDS sealingrings and a thermal actuator are then placed into the shoulder and bore respectively.This activity was performed to reduce the impact of loss of all RCP seal cooling which is mostlikely to occur during loss of all on-site and off-site AC power (Station Blackout (SBO)). Thisimproves margin to a severe core damage event. SBO is the dominant core damage event forWCGS.50.59 Evaluation:The SDS is designed to only deploy on a stationary RCP shaft and only after all seal coolinghas been lost and the seal temperature rises to a prescribed temperature. The SDS willactuate when a wax material within the actuator assembly melts. Actuators are factory-testedto verify repeatable operation within their design temperature range (250 degrees F to 300degrees F). With WCGS at 100 percent power, the number 1 seal temperatures indicate 130degrees F.The frequency of SDS inadvertent actuation is 1.2 E-06 events per pump-year of operation or4.8 E-06 per year for a four-loop plant. This is a very low probability of occurrence; thus it isconcluded that inadvertent actuation of an SDS during normal plant operation has negligiblecontribution to the overall frequency of a forced shutdown of the plant from all causes which isabout 1 E-01 per year including forced outages due to RCP issues which is about 6 E-02 peryear. Thus, the frequency of this previously evaluated event is not increased due to SDSinstallation.The evaluation concluded that no new accident is created or any existing analyzed accident ismade worse, including the consequences. There are no new, unanalyzed failures introducedbecause of this change in design of the number 1 RCP seal insert.
The replacement system is based upon the Ovation platform supplied by Emerson Process Management (EPM).The main turbine control system is designed to prevent turbine overspeed in the event of asudden loss of load using multiple levels of component redundancy and diversity.
Attachment RA 15-0013Page 5 of 11Evaluation Number: 59 2012-0004 Revision: 0Title: Steam Generator Feed Pump Protection and Control System UpgradeActivity
Failure of anysingle component will not result in a turbine rotor speed exceeding the design overspeed of 120percent of rated speed, or 2160 RPM. The function and performance of the TCS, as described in the USAR, is not being changed, with the exception being the replacement of the existingmechanical-hydraulic overspeed trip based upon the centrifugal principle with an alternate morereliable design.50.59 Evaluation:
The TCS is non-safety related and the modification does not change the function orperformance requirements for the system as described in the USAR. The TCS upgrade doesnot increase any plant operating parameters that would result in increased challenges toimportant safety components or the frequency of any accident described in the USAR. No newinterface requirements with important to safety components that function to limit theconsequences of an accident are established by this upgrade.The WCGS specific TCS upgrade Software Hazards Analysis (SHA) evaluated the TCSupgrade related system-level hazards to ensure that the results would be bounded by theresults of malfunctions or accidents previously considered in the USAR.The evaluation determined that the results of potential TCS upgrade failures are enveloped bythe current USAR Chapter 15 analyses.
An SHA review of the WCGS USAR Chapter 15 events was performed to identify any newsystem-level hazards with regard to the digital TCS upgrade.
No new system-level hazards orfailure modes were identified as a result of this review.An SHA evaluation of sub-system level software
: failures, including software common causefailures and cyber security events/cyber-attacks, to determine their impact on the identified system-level
: hazards, concluded that potential sub-system level software failures would notlead to different types of accidents or impact plant USAR analyses.
A turbine trip evaluation determined the total system failure probability of both the existing TCSand the upgraded TCS to be essentially identical, 1.142E-6 and 1.08E-6 respectively.
Attachment RA 15-0013Page 4 of 11Evaluation Number: 59 2012-0003 Revision:
0Title: Replace current Number 1 Seal inserts in the four Wolf Creek Model 93A-1 ReactorCoolant Pumps (RCP's) with a modified design called the Shield Shutdown Seal(SDS)Activity


== Description:==
==
The existing WCGS Steam Generator Feed Pump (SGFP) protection and control of theGeneral Electric MDT-20 system and electro-hydraulic controls was upgraded with a DistributedControl System (DCS) supplied by Westinghouse. The digital replacement system is basedupon the Ovation platform supplied by Emerson Process Management (EPM). The normalfunction of the SGFP protection and control system is to generate position signals for the HighPressure and Low Pressure control valves, the SGFP recirculation valves, and the condensatepump recirculation valves. Changing the position of the steam valves provides the method ofcontrolling the SGFP turbine speed. Using the system, the SGFP turbines are capable ofoperation from a shutdown state to full load.The function and performance of the SGFP protection and control system as described in theUSAR, is not being changed, with the exception being the elimination of the existing electricaloverspeed trip valves, associated test solenoid valves, and the mechanical overspeed tripelimination. The SGFP protection and control system upgrade eliminates existing Single PointVulnerabilities.50.59 Evaluation:The SGFP protection and control system is non-safety related and the modification does notchange the function or performance requirements for the system. The SGFP protection andcontrol system upgrade does not change any plant operating parameters that would result inincreased challenges to important safety components or the frequency of any accidentdescribed in the USAR. Furthermore, no new interface requirements with important to safetycomponents that function to limit the consequences of an accident are established by thisupgrade.The removal of the mechanical overspeed trip mechanism and the electrical overspeed tripvalves has no impact on accident mitigation or the consequences of an accident.The function of tripping the SGFPs is not part of the primary success path for accidentmitigation and does not impact any USAR transient or accident analyses.The WCGS specific SGFP protection and control system upgrade Software Hazards Analysis(SHA) evaluated the SGFP protection and control system upgrade related system-level hazardsand concluded that the results would be bounded by the results of malfunctions or accidentspreviously considered in the USAR.The evaluation determined that the results of potential SGFP protection and control systemupgrade failures are enveloped by the current USAR Chapter 15 analyses and no new system-level hazards or failure modes were identified as a result of this review.An SHA evaluation of sub-system level software failures, including software common causefailures and cyber security events/cyber-attacks, to determine their impact on the identifiedsystem-level hazards, concluded that potential sub-system level software failures are boundedby or do not impact the USAR accident analyses previously considered.
Description:==
Attachment RA 15-0013Page 6 of 11Evaluation Number: 59 2013-0001 Revision: 0Title: Turbine-Driven Auxiliary Feedwater Pump Controls ReplacementActivity


== Description:==
The Number 1 Seal inserts in the four Wolf Creek Model 93A-1 Reactor Coolant Pumps (RCPs)were replaced with a modified design called the Shield Shutdown Seal (SDS). The affectedSystems, Structures, Components (SSC's) are the Number 1 Seal inserts in RCPs PBB01A, B,C, and D. The activity includes the preparation of design and configuration change documents, procurement, and actual installation of the SDS in Refuel 19.The SDS integrated new features into the existing Number 1 Seal insert and is locateddownstream of the current film-riding face seal. A shoulder is machined into the inner diameterat the top flange and bore machined into the groove diameter above the shoulder.
The analog governor controls for the Turbine Driven Auxiliary Feedwater Pump (TDAFWP) areobsolete. This change replaced the equipment with a new digital platform for the turbinegovernor controls and replaced the Trip and Throttle (T&T) Valve (FC HV 0312) starter controls.This change consists of the following:Replacement of the local control panel with new Original Equipment Manufacturer suppliedcontrols based on a digital platform for governor controls and new motor starter for the DCmotor operator for the T&T Valve.The Operator Manual/Auto stations on the Main Control Board and the Auxiliary ShutdownPanel (RP1 18B) will be replaced with new simplified stations compatible with the new controls.The electrohydraulic actuator for the governor valve will be replaced with a new electricactuator.The governor valve linkage arm and bracket will be eliminated with a new actuator bracket,aligning the actuator to a direct linear arrangement with the governor valve stem.Replacement of the Foxboro Spec 200 control loops that supported the old Manual/Autostations and speed setpoint and provided control signal isolation for Control Room Fire SafeShutdown with a simple isolation device for the 24VDC circuit in the Main Control Board.50.59 Evaluation:The impact on the Auxiliary Feedwater System and the accidents listed in the USAR Chapter 15were reviewed. The change to the plant and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.There is no adverse impact to the provisions to prevent the accumulation of condensate in theturbine steam supply lines and no lessening of the system's ability to operate with steam inletpressures ranging from 92 to 1,290 psia, as defined in the original specification M-021 andverified in the original turbine qualification testing contained in M-021-00087.The design continues to meet the requirements defined for the exhaust line to remain functionalafter a Safe Shutdown Earthquake and or to perform its intended function following a postulatedhazard, such as internal missile or pipe break.
SDS sealingrings and a thermal actuator are then placed into the shoulder and bore respectively.
Attachment RA 15-0013Page 7 of 11Evaluation Number: 59 2013-0002 Revision: 0Title: HKE25 Conveyer Car Operation with Removal of the Hold Down LatchActivity
This activity was performed to reduce the impact of loss of all RCP seal cooling which is mostlikely to occur during loss of all on-site and off-site AC power (Station Blackout (SBO)). Thisimproves margin to a severe core damage event. SBO is the dominant core damage event forWCGS.50.59 Evaluation:
The SDS is designed to only deploy on a stationary RCP shaft and only after all seal coolinghas been lost and the seal temperature rises to a prescribed temperature.
The SDS willactuate when a wax material within the actuator assembly melts. Actuators are factory-tested to verify repeatable operation within their design temperature range (250 degrees F to 300degrees F). With WCGS at 100 percent power, the number 1 seal temperatures indicate 130degrees F.The frequency of SDS inadvertent actuation is 1.2 E-06 events per pump-year of operation or4.8 E-06 per year for a four-loop plant. This is a very low probability of occurrence; thus it isconcluded that inadvertent actuation of an SDS during normal plant operation has negligible contribution to the overall frequency of a forced shutdown of the plant from all causes which isabout 1 E-01 per year including forced outages due to RCP issues which is about 6 E-02 peryear. Thus, the frequency of this previously evaluated event is not increased due to SDSinstallation.
The evaluation concluded that no new accident is created or any existing analyzed accident ismade worse, including the consequences.
There are no new, unanalyzed failures introduced because of this change in design of the number 1 RCP seal insert.
Attachment RA 15-0013Page 5 of 11Evaluation Number: 59 2012-0004 Revision:
0Title: Steam Generator Feed Pump Protection and Control System UpgradeActivity


== Description:==
==
The hold down latch on the fuel handling conveyer car was removed as the hold down latchwas not engaging all the time on the reactor end of the system. The fuel bundle needs to beplaced in the horizontal position to allow for transport of the fuel bundle to the spent fuel pool(SFP). The hold down latch is a mechanical latch device on the transfer car that is opened bythe car moving into position in the horizontal position. The conveyer car was moving intoposition but the latch was not latching when loaded with a bundle and ready to return to the fuelbuilding from the upender pit in the reactor building. This change removed the hold down latchand allowed positioning the fuel bundle from the vertical to the horizontal position for transportto the SFP.50.59 Evaluation:The removal of the hold down latch from the conveyer car, with the compensating action ofvisual verification of the car in the proper position for upending, remains a reliable means forhandling the fuel assemblies. The conveyer car shall be utilized in the manual mode when thehold down latch is removed. Two redundant interlocks allow a lifting arm operation only whenthe transfer car is at the respective end of its travel on the reactor side as well as on the fuelbuilding side, one of these interlocks is the position switch, the other is the hold down latch thatthis modification is removing. The position switch is the primary device with the hold down latchbeing the backup. Removal of the hold down latch will remove the redundancy but this featurewill be compensated for by visual examination and verification that the car is at its properposition for upending the fuel by utilizing the positions arrows.The removal of the hold down latch and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.
Description:==
Attachment RA 15-0013Page 8 of 11Evaluation Number: 59 2013-0002 Revision: ITitle: HKE25 Conveyer Car Operation with Removal of the Hold Down LatchActivity


== Description:==
The existing WCGS Steam Generator Feed Pump (SGFP) protection and control of theGeneral Electric MDT-20 system and electro-hydraulic controls was upgraded with a Distributed Control System (DCS) supplied by Westinghouse.
The hold down latch on the -fuel handling conveyer car was removed as the hold down latchwas not engaging all the time on the reactor end of the system. The fuel bundle needs to beplaced in the horizontal position to allow for transport of the fuel bundle to either the spent fuelpool (SFP) or the refueling pool. The hold down latch is a mechanical latch device on thetransfer car that is opened by the car moving into position horizontally. The conveyer car wasmoving into position but the latch was not actuating, preventing the fuel bundle from pivotingfrom the horizontal to the vertical position. Removing the hold down latch allowed for upendingthe fuel bundle for transporting it to the SFP or refueling pool. Revision 0 only allowed fuelmovement to the SFP, while revision 1 also allows fuel movement to the refueling pool.50.59 Evaluation:The removal of the hold down latch from the conveyer car, with the compensating action ofvisual verification of the car in the proper position for upending, provides a reliable means forhandling the fuel assemblies. The conveyer car shall be utilized in the manual mode when thehold down latch is removed. Two redundant interlocks allow a lifting arm operation only whenthe transfer car is at the respective end of its travel on the reactor side as well as on the fuelbuilding side, one of these interlocks is the position switch, and the other is the hold down latchthat this modification is removing. The position switch is the primary device with the hold downlatch being the backup. Removal of the hold down latch will remove the redundancy but thisfeature will be compensated for by visual examination and verification that the car is at itsproper position for upending the fuel by utilizing the positions arrows.The removal of the hold down latch and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.
The digital replacement system is basedupon the Ovation platform supplied by Emerson Process Management (EPM). The normalfunction of the SGFP protection and control system is to generate position signals for the HighPressure and Low Pressure control valves, the SGFP recirculation valves, and the condensate pump recirculation valves. Changing the position of the steam valves provides the method ofcontrolling the SGFP turbine speed. Using the system, the SGFP turbines are capable ofoperation from a shutdown state to full load.The function and performance of the SGFP protection and control system as described in theUSAR, is not being changed, with the exception being the elimination of the existing electrical overspeed trip valves, associated test solenoid valves, and the mechanical overspeed tripelimination.
Attachment RA 15-0013Page 9 of 11Evaluation Number: 59 2013-0003 Revision: 0Title: Probable Maximum Precipitation (PMP) Flood CalculationsActivity
The SGFP protection and control system upgrade eliminates existing Single PointVulnerabilities.
50.59 Evaluation:
The SGFP protection and control system is non-safety related and the modification does notchange the function or performance requirements for the system. The SGFP protection andcontrol system upgrade does not change any plant operating parameters that would result inincreased challenges to important safety components or the frequency of any accidentdescribed in the USAR. Furthermore, no new interface requirements with important to safetycomponents that function to limit the consequences of an accident are established by thisupgrade.The removal of the mechanical overspeed trip mechanism and the electrical overspeed tripvalves has no impact on accident mitigation or the consequences of an accident.
The function of tripping the SGFPs is not part of the primary success path for accidentmitigation and does not impact any USAR transient or accident analyses.
The WCGS specific SGFP protection and control system upgrade Software Hazards Analysis(SHA) evaluated the SGFP protection and control system upgrade related system-level hazardsand concluded that the results would be bounded by the results of malfunctions or accidents previously considered in the USAR.The evaluation determined that the results of potential SGFP protection and control systemupgrade failures are enveloped by the current USAR Chapter 15 analyses and no new system-level hazards or failure modes were identified as a result of this review.An SHA evaluation of sub-system level software
: failures, including software common causefailures and cyber security events/cyber-attacks, to determine their impact on the identified system-level
: hazards, concluded that potential sub-system level software failures are boundedby or do not impact the USAR accident analyses previously considered.
Attachment RA 15-0013Page 6 of 11Evaluation Number: 59 2013-0001 Revision:
0Title: Turbine-Driven Auxiliary Feedwater Pump Controls Replacement Activity


== Description:==
==
WCGS Flood Calculation XX-C-023 is the Analysis of Record for determining the maximumflood elevation at WCGS. This calculation was updated and replaced by 3 new floodcalculations as listed below: The new flood calculations were developed using the guidanceprovided in NUREG/CR -7046 so it is compatible with WCGS's Fukushima response toperform a flooding hazard re-evaluation for the site.Calculation 69461-C-001: determines the Probable Maximum Precipitation (PMP) usingprocedures outlined in Hydrometeorological Report No. 52 for WCGS.Calculation 69461-C-002: determines the peak discharge associated with the PMP that wascalculated in Calculation No. 69461-C-001 using procedures outlined in HydrometeorologicalReport No. 52 for the WCGS. This calculation uses the data developed within the CalculationNo. 69461-C-001 as input to the computer program Hydrologic Engineering Center -Hydrologic Modeling System (HEC-HMS) version 3.5.Calculation 69461-C-003: estimates water surface elevations at WCGS for the PMP event. Thepeak discharges determined from Calculation No. 69461-C-002 are used as input into theUSACE Hydrologic Engineering Center River Analysis System (HEC-RAS) software todetermine the water surface elevations throughout the site.50.59 Evaluation:NUREG/CR-7046 requires that the water surface elevation near a safety-related buildingproduced by the PMP be less than the floor elevation. While the calculated water surfaceelevations varied across the site, modeling results indicated that all safety-related buildinglocation flood stages are less than the floor elevation using the methodology and guidanceprovided in NUREG/CR -7046.The new calculations use methods that have been approved by the NRC for the intendedapplication (NUREG/CR-7046). Additionally, they do not change how WCGS uses the floodinformation to operate or control SSCs to prevent flood events from adversely affecting SafetyRelated Seismic Category 1 Structures. The results from the new flood calculations are similarto the existing calculation of record (XX-C-023) except these provide more site-specificinformation. Compared with the existing flood calculation the new calculations slightly reducemargin at the north end of the powerblock and improve margin to the south, and are consideredconservative or essentially the same and continue to meet the acceptance criteria.
Description:==
Attachment RA 15-0013Page 10 of 11Evaluation Number: 59 2014-0001 Revision: 0Title: Thermocouple/Core Cooling Monitor UpgradeActivity


== Description:==
The analog governor controls for the Turbine Driven Auxiliary Feedwater Pump (TDAFWP) areobsolete.
The Thermocouple/Core Cooling Monitor (TCCM) combines the functions of monitoring forexcessive core exit thermocouple temperatures and monitoring both core exit thermocoupletemperatures and hot and cold leg temperatures for saturation margin. The TCCM System hasexperienced obsolescence and reliability issues that have caused system components andmodules to be degraded or fail.The WCGS TCCM upgrade involved replacement of the existing microprocessor-based systemsupplied by Westinghouse. The replacement system is based upon the Advanced LogicSystem (ALS) supplied by Westinghouse. The ALS platform was installed at WCGS as areplacement of Main Steam and Feedwater Isolation System (MSFIS) equipment.An ALS Service Unit (ASU) is allocated for each train of the TCCM and resides entirely withinthe TCCM cabinet. The ASU consists of a PC Node Box and a Flat Panel Display. ASUdisplays core temperatures, pressures, channel calibration, system status and enables theperformance of system test and calibration activities. The implementation of the ASU is basedon the Common Qualified (Common Q) Platform defined in Westinghouse WCAP-16097-P-A,"Common Qualified Platform Topical Report."50.59 Evaluation:NUREG-0737, "Clarification of TMI Action Plan Requirements," specifies the functionalrequirements for the TCCM. WCGS USAR Chapter 18, section 18.2.13 describes how theTCCM complies with NUREG-0737 requirements. The function and performance of the TCCMas described in the USAR, is not being changed.WCGS USAR Chapter 7, Table 7A-3, addresses TCCM compliance with Regulatory Guide 1.97requirements for post-accident monitoring indication. No changes are required for RegulatoryGuide 1.97 compliance as described in the Table 7A-3 data sheets as a result of the TCCMupgrade because exactly the same functions in the original TCCM are replicated in thereplacement TCCM.Each train of the ALS platform-based TCCM includes an ASU. The ASU consists of a PC NodeBox and a Flat Panel Display. The implementation of the ASU is based on the Common QPlatform described in WCAP-16097-P-A, "Common Qualified Platform Topical Report." TheCommon Q platform is a set of commercial-grade hardware and previously developed softwarecomponents dedicated and qualified for use in nuclear power plants. The NRC has reviewedand approved the Common Q system for installation in safety related applications. WCAP-16097-P-A includes the NRC SER for the Common Q platform.The built-in diversity features provided by the ALS platform significantly reduces the potentialfor common cause failures in TCCM functions as compared to the existing microprocessorbased TCCM.
This change replaced the equipment with a new digital platform for the turbinegovernor controls and replaced the Trip and Throttle (T&T) Valve (FC HV 0312) starter controls.
Attachment RA 15-0013Page 11 of 11Evaluation Number: 59 2014-0002 Revision: 0Title: ESW Below Ground Plant Tie-In Approval and Component AbandonmentActivity
This change consists of the following:
Replacement of the local control panel with new Original Equipment Manufacturer suppliedcontrols based on a digital platform for governor controls and new motor starter for the DCmotor operator for the T&T Valve.The Operator Manual/Auto stations on the Main Control Board and the Auxiliary ShutdownPanel (RP1 18B) will be replaced with new simplified stations compatible with the new controls.
The electrohydraulic actuator for the governor valve will be replaced with a new electricactuator.
The governor valve linkage arm and bracket will be eliminated with a new actuator bracket,aligning the actuator to a direct linear arrangement with the governor valve stem.Replacement of the Foxboro Spec 200 control loops that supported the old Manual/Auto stations and speed setpoint and provided control signal isolation for Control Room Fire SafeShutdown with a simple isolation device for the 24VDC circuit in the Main Control Board.50.59 Evaluation:
The impact on the Auxiliary Feedwater System and the accidents listed in the USAR Chapter 15were reviewed.
The change to the plant and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.
There is no adverse impact to the provisions to prevent the accumulation of condensate in theturbine steam supply lines and no lessening of the system's ability to operate with steam inletpressures ranging from 92 to 1,290 psia, as defined in the original specification M-021 andverified in the original turbine qualification testing contained in M-021-00087.
The design continues to meet the requirements defined for the exhaust line to remain functional after a Safe Shutdown Earthquake and or to perform its intended function following a postulated hazard, such as internal missile or pipe break.
Attachment RA 15-0013Page 7 of 11Evaluation Number: 59 2013-0002 Revision:
0Title: HKE25 Conveyer Car Operation with Removal of the Hold Down LatchActivity


== Description:==
==
The Essential Service Water (ESW) system has experienced localized degradation in buriedpiping in the form of tuberculation, pitting, and through-wall leakage. WCGS replaced andredesigned the below ground ESW piping.The buried ESW Train "A" and "B" supply and return piping including the warming lines andaccess vaults were replaced and rerouted. The supply and return piping was routed to the newcirculating water crossing and required seismic support to alleviate potential concern associatedwith a circulating water line break washing out bedding below the new ESW. The return pipingwas rerouted to a new discharge point located in the ultimate heat sink (UHS). The changeabandoned the original discharge structure. The warming lines were rerouted from the returnpiping through penetrations into the ESW pumphouse forebays. New access vaults wereinstalled periodically along the new ESW system piping route.This ESW system change involved revising the current tornado-generated missile protectionand freeze protection configuration and seismic support configuration for portions of the ESWbelow ground piping and components.50.59 Evaluation:The change to the ESW missile and freeze protection .configuration, seismic supportconfiguration, and new discharge structure will continue to provide protection against the effectsof natural phenomena, such as earthquakes, tornadoes, hurricanes, floods, and externalmissiles. The changes do not reduce the capabilities of the ESW system in performance of thefunctions described in the USAR and the system and equipment will continue to meet all of theirexisting safety design bases. The failure modes and effects analysis for the ESW system is notaffected by the change.The USAR was reviewed to identify the accidents/transients previously evaluated that arepotentially affected by the change to ESW piping and the seismic support configuration. Theyare the steam generator tube rupture (SGTR) and the Loss-of-coolant accident (LOCA)resulting from a spectrum of postulated piping breaks within the reactor coolant pressureboundary. The Station Blackout (SBO) analysis was also reviewed.The new ESW missile and freeze protection configuration, seismic support configuration, andnew discharge structure provides all the capabilities and functions present in the existingconfiguration and will not create any additional failure modes. After implementation, the ESWsystem continues to be capable of supplying the minimum flow rates required to remove heatfrom the containment and necessary safety-related components from a postulated design basisaccident (DBA) and dissipate it to the ultimate heat sink, including the SBO coping time of fourhours. The ESW system will continue to be capable of removing heat from plant componentsnecessary to achieve and maintain post-fire or post-accident safe shutdown.The ESW system will continue to be available for the mitigation of the effects associated withthe limiting DBAs and transients previously evaluated in the USAR. Therefore, all assumptionsutilized within USAR-described dose analyses remain valid and bounding.}}
Description:==
 
The hold down latch on the fuel handling conveyer car was removed as the hold down latchwas not engaging all the time on the reactor end of the system. The fuel bundle needs to beplaced in the horizontal position to allow for transport of the fuel bundle to the spent fuel pool(SFP). The hold down latch is a mechanical latch device on the transfer car that is opened bythe car moving into position in the horizontal position.
The conveyer car was moving intoposition but the latch was not latching when loaded with a bundle and ready to return to the fuelbuilding from the upender pit in the reactor building.
This change removed the hold down latchand allowed positioning the fuel bundle from the vertical to the horizontal position for transport to the SFP.50.59 Evaluation:
The removal of the hold down latch from the conveyer car, with the compensating action ofvisual verification of the car in the proper position for upending, remains a reliable means forhandling the fuel assemblies.
The conveyer car shall be utilized in the manual mode when thehold down latch is removed.
Two redundant interlocks allow a lifting arm operation only whenthe transfer car is at the respective end of its travel on the reactor side as well as on the fuelbuilding side, one of these interlocks is the position switch, the other is the hold down latch thatthis modification is removing.
The position switch is the primary device with the hold down latchbeing the backup. Removal of the hold down latch will remove the redundancy but this featurewill be compensated for by visual examination and verification that the car is at its properposition for upending the fuel by utilizing the positions arrows.The removal of the hold down latch and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.
Attachment RA 15-0013Page 8 of 11Evaluation Number: 59 2013-0002 Revision:
ITitle: HKE25 Conveyer Car Operation with Removal of the Hold Down LatchActivity
 
==
Description:==
 
The hold down latch on the -fuel handling conveyer car was removed as the hold down latchwas not engaging all the time on the reactor end of the system. The fuel bundle needs to beplaced in the horizontal position to allow for transport of the fuel bundle to either the spent fuelpool (SFP) or the refueling pool. The hold down latch is a mechanical latch device on thetransfer car that is opened by the car moving into position horizontally.
The conveyer car wasmoving into position but the latch was not actuating, preventing the fuel bundle from pivotingfrom the horizontal to the vertical position.
Removing the hold down latch allowed for upendingthe fuel bundle for transporting it to the SFP or refueling pool. Revision 0 only allowed fuelmovement to the SFP, while revision 1 also allows fuel movement to the refueling pool.50.59 Evaluation:
The removal of the hold down latch from the conveyer car, with the compensating action ofvisual verification of the car in the proper position for upending, provides a reliable means forhandling the fuel assemblies.
The conveyer car shall be utilized in the manual mode when thehold down latch is removed.
Two redundant interlocks allow a lifting arm operation only whenthe transfer car is at the respective end of its travel on the reactor side as well as on the fuelbuilding side, one of these interlocks is the position switch, and the other is the hold down latchthat this modification is removing.
The position switch is the primary device with the hold downlatch being the backup. Removal of the hold down latch will remove the redundancy but thisfeature will be compensated for by visual examination and verification that the car is at itsproper position for upending the fuel by utilizing the positions arrows.The removal of the hold down latch and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.
Attachment RA 15-0013Page 9 of 11Evaluation Number: 59 2013-0003 Revision:
0Title: Probable Maximum Precipitation (PMP) Flood Calculations Activity
 
==
Description:==
 
WCGS Flood Calculation XX-C-023 is the Analysis of Record for determining the maximumflood elevation at WCGS. This calculation was updated and replaced by 3 new floodcalculations as listed below: The new flood calculations were developed using the guidanceprovided in NUREG/CR
-7046 so it is compatible with WCGS's Fukushima response toperform a flooding hazard re-evaluation for the site.Calculation 69461-C-001:
determines the Probable Maximum Precipitation (PMP) usingprocedures outlined in Hydrometeorological Report No. 52 for WCGS.Calculation 69461-C-002:
determines the peak discharge associated with the PMP that wascalculated in Calculation No. 69461-C-001 using procedures outlined in Hydrometeorological Report No. 52 for the WCGS. This calculation uses the data developed within the Calculation No. 69461-C-001 as input to the computer program Hydrologic Engineering Center -Hydrologic Modeling System (HEC-HMS) version 3.5.Calculation 69461-C-003:
estimates water surface elevations at WCGS for the PMP event. Thepeak discharges determined from Calculation No. 69461-C-002 are used as input into theUSACE Hydrologic Engineering Center River Analysis System (HEC-RAS) software todetermine the water surface elevations throughout the site.50.59 Evaluation:
NUREG/CR-7046 requires that the water surface elevation near a safety-related buildingproduced by the PMP be less than the floor elevation.
While the calculated water surfaceelevations varied across the site, modeling results indicated that all safety-related buildinglocation flood stages are less than the floor elevation using the methodology and guidanceprovided in NUREG/CR
-7046.The new calculations use methods that have been approved by the NRC for the intendedapplication (NUREG/CR-7046).
Additionally, they do not change how WCGS uses the floodinformation to operate or control SSCs to prevent flood events from adversely affecting SafetyRelated Seismic Category 1 Structures.
The results from the new flood calculations are similarto the existing calculation of record (XX-C-023) except these provide more site-specific information.
Compared with the existing flood calculation the new calculations slightly reducemargin at the north end of the powerblock and improve margin to the south, and are considered conservative or essentially the same and continue to meet the acceptance criteria.
Attachment RA 15-0013Page 10 of 11Evaluation Number: 59 2014-0001 Revision:
0Title: Thermocouple/Core Cooling Monitor UpgradeActivity
 
==
Description:==
 
The Thermocouple/Core Cooling Monitor (TCCM) combines the functions of monitoring forexcessive core exit thermocouple temperatures and monitoring both core exit thermocouple temperatures and hot and cold leg temperatures for saturation margin. The TCCM System hasexperienced obsolescence and reliability issues that have caused system components andmodules to be degraded or fail.The WCGS TCCM upgrade involved replacement of the existing microprocessor-based systemsupplied by Westinghouse.
The replacement system is based upon the Advanced LogicSystem (ALS) supplied by Westinghouse.
The ALS platform was installed at WCGS as areplacement of Main Steam and Feedwater Isolation System (MSFIS) equipment.
An ALS Service Unit (ASU) is allocated for each train of the TCCM and resides entirely withinthe TCCM cabinet.
The ASU consists of a PC Node Box and a Flat Panel Display.
ASUdisplays core temperatures, pressures, channel calibration, system status and enables theperformance of system test and calibration activities.
The implementation of the ASU is basedon the Common Qualified (Common Q) Platform defined in Westinghouse WCAP-16097-P-A, "Common Qualified Platform Topical Report."50.59 Evaluation:
NUREG-0737, "Clarification of TMI Action Plan Requirements,"
specifies the functional requirements for the TCCM. WCGS USAR Chapter 18, section 18.2.13 describes how theTCCM complies with NUREG-0737 requirements.
The function and performance of the TCCMas described in the USAR, is not being changed.WCGS USAR Chapter 7, Table 7A-3, addresses TCCM compliance with Regulatory Guide 1.97requirements for post-accident monitoring indication.
No changes are required for Regulatory Guide 1.97 compliance as described in the Table 7A-3 data sheets as a result of the TCCMupgrade because exactly the same functions in the original TCCM are replicated in thereplacement TCCM.Each train of the ALS platform-based TCCM includes an ASU. The ASU consists of a PC NodeBox and a Flat Panel Display.
The implementation of the ASU is based on the Common QPlatform described in WCAP-16097-P-A, "Common Qualified Platform Topical Report."
TheCommon Q platform is a set of commercial-grade hardware and previously developed softwarecomponents dedicated and qualified for use in nuclear power plants. The NRC has reviewedand approved the Common Q system for installation in safety related applications.
WCAP-16097-P-A includes the NRC SER for the Common Q platform.
The built-in diversity features provided by the ALS platform significantly reduces the potential for common cause failures in TCCM functions as compared to the existing microprocessor based TCCM.
Attachment RA 15-0013Page 11 of 11Evaluation Number: 59 2014-0002 Revision:
0Title: ESW Below Ground Plant Tie-In Approval and Component Abandonment Activity
 
==
Description:==
 
The Essential Service Water (ESW) system has experienced localized degradation in buriedpiping in the form of tuberculation,  
: pitting, and through-wall leakage.
WCGS replaced andredesigned the below ground ESW piping.The buried ESW Train "A" and "B" supply and return piping including the warming lines andaccess vaults were replaced and rerouted.
The supply and return piping was routed to the newcirculating water crossing and required seismic support to alleviate potential concern associated with a circulating water line break washing out bedding below the new ESW. The return pipingwas rerouted to a new discharge point located in the ultimate heat sink (UHS). The changeabandoned the original discharge structure.
The warming lines were rerouted from the returnpiping through penetrations into the ESW pumphouse forebays.
New access vaults wereinstalled periodically along the new ESW system piping route.This ESW system change involved revising the current tornado-generated missile protection and freeze protection configuration and seismic support configuration for portions of the ESWbelow ground piping and components.
50.59 Evaluation:
The change to the ESW missile and freeze protection  
.configuration, seismic supportconfiguration, and new discharge structure will continue to provide protection against the effectsof natural phenomena, such as earthquakes, tornadoes, hurricanes, floods, and externalmissiles.
The changes do not reduce the capabilities of the ESW system in performance of thefunctions described in the USAR and the system and equipment will continue to meet all of theirexisting safety design bases. The failure modes and effects analysis for the ESW system is notaffected by the change.The USAR was reviewed to identify the accidents/transients previously evaluated that arepotentially affected by the change to ESW piping and the seismic support configuration.
Theyare the steam generator tube rupture (SGTR) and the Loss-of-coolant accident (LOCA)resulting from a spectrum of postulated piping breaks within the reactor coolant pressureboundary.
The Station Blackout (SBO) analysis was also reviewed.
The new ESW missile and freeze protection configuration, seismic support configuration, andnew discharge structure provides all the capabilities and functions present in the existingconfiguration and will not create any additional failure modes. After implementation, the ESWsystem continues to be capable of supplying the minimum flow rates required to remove heatfrom the containment and necessary safety-related components from a postulated design basisaccident (DBA) and dissipate it to the ultimate heat sink, including the SBO coping time of fourhours. The ESW system will continue to be capable of removing heat from plant components necessary to achieve and maintain post-fire or post-accident safe shutdown.
The ESW system will continue to be available for the mitigation of the effects associated withthe limiting DBAs and transients previously evaluated in the USAR. Therefore, all assumptions utilized within USAR-described dose analyses remain valid and bounding.}}

Revision as of 03:03, 1 July 2018

Wolf Creek Generating Station - Biennial 50.59 Evaluation Report
ML15075A028
Person / Time
Site: Wolf Creek 
Issue date: 03/04/2015
From: Koenig S R
Wolf Creek
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
RA 15-0013
Download: ML15075A028 (12)


Text

NUCLEAR OPERATING CORPORATION Steven R. KoenigManager Regulatory AffairsMarch 4, 2015RA 15-0013U. S. Nuclear Regulatory Commission ATTN: Document Control DeskWashington, DC 20555

Subject:

Docket No. 50-482:Evaluation ReportWolf Creek Generating Station Biennial 50.59Gentlemen:

This letter transmits the Biennial 50.59 Evaluation Report for Wolf Creek Generating Station(WCGS), which is being submitted pursuant to 10 CFR 50.59(d)(2).

The attachment providesthe WCGS Biennial 50.59 Evaluation Report including a summary of the evaluation results.This report covers the period from January 1, 2013, to December 31,2014, and contains asummary of 50.59 evaluations implemented during this period that were approved by theWCGS onsite review committee.

This letter contains no commitments.

If you have any questions concerning this matter, pleasecontact me at (620) 364-4041.

SRK/rltAttachment cc: M. L. Dapas (NRC), w/aC. F. Lyon (NRC), w/aN. F. O'Keefe (NRC), w/aSenior Resident Inspector (NRC), w/a41V-1%0CLP.O. Box 411 / Burlington, KS 66839 / Phone: (620) 364-8831An Equal Opportunity Employer M/F/HCNET Attachment RA 15-0013Page 1 of 11WOLF CREEK NUCLEAR OPERATING CORPORATION Wolf Creek Generating StationDocket No.: 50-482Facility Operating License No.: NPF-42BIENNIAL 50.59 EVALUATION REPORTReport No.: 24Reporting Period: January 1, 2013 through December 31, 2014 Attachment RA 15-0013Page 2 of 11SUMMARYThis report provides a brief description of changes, test, and experiments implemented at WolfCreek Generating Station (WCGS) and evaluated pursuant to 10 CFR 50.59(c)(1).

This reportincludes summaries of the associated 50.59 evaluations that were reviewed and found to beacceptable by the Plant Safety Review Committee (PSRC) for the period beginning January 1,2013 and ending December 31, 2014. This report is submitted in accordance with therequirements of 10 CFR 50.59(d)(2).

On the basis of these evaluation of changes:" There is less than a minimal increase in the frequency of occurrence of an accidentpreviously evaluated in the Updated Final Safety Analysis Report (USAR)." There is less than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component (SSC) important to safety previously evaluated in the USAR." There is less than a minimal increase in the consequences of an accident previously evaluated in the USAR." There is less than a minimal increase in the consequences of a malfunction of anSSC important to safety previously evaluated in the USAR." There is no possibility for an accident of a different type than any previously evaluated in the USAR being created.* There is no possibility for a malfunction of a SSC important to safety with a different result than any previously evaluated in the USAR being created." There is no result in a design basis limit for a fission product barrier as described inthe USAR being exceeded or altered." There is no result in a departure from a method of evaluation described in the USARused in establishing the design bases or in the safety analyses.

Therefore, all items contained within this report have been determined not to require a licenseamendment.

Attachment RA 15-0013Page 3 of 11Evaluation Number: 59 2012-0002 Revision:

0Title: Turbine Control System (TCS) UpgradeActivity

==

Description:==

The WCGS Turbine Control System (TCS) was upgraded by replacement of the existingGeneral Electric Mark II Electro-Hydraulic Control (EHC) system and Emergency Trip System(ETS), with a Distributed Control System (DCS) supplied by Westinghouse.

The replacement system is based upon the Ovation platform supplied by Emerson Process Management (EPM).The main turbine control system is designed to prevent turbine overspeed in the event of asudden loss of load using multiple levels of component redundancy and diversity.

Failure of anysingle component will not result in a turbine rotor speed exceeding the design overspeed of 120percent of rated speed, or 2160 RPM. The function and performance of the TCS, as described in the USAR, is not being changed, with the exception being the replacement of the existingmechanical-hydraulic overspeed trip based upon the centrifugal principle with an alternate morereliable design.50.59 Evaluation:

The TCS is non-safety related and the modification does not change the function orperformance requirements for the system as described in the USAR. The TCS upgrade doesnot increase any plant operating parameters that would result in increased challenges toimportant safety components or the frequency of any accident described in the USAR. No newinterface requirements with important to safety components that function to limit theconsequences of an accident are established by this upgrade.The WCGS specific TCS upgrade Software Hazards Analysis (SHA) evaluated the TCSupgrade related system-level hazards to ensure that the results would be bounded by theresults of malfunctions or accidents previously considered in the USAR.The evaluation determined that the results of potential TCS upgrade failures are enveloped bythe current USAR Chapter 15 analyses.

An SHA review of the WCGS USAR Chapter 15 events was performed to identify any newsystem-level hazards with regard to the digital TCS upgrade.

No new system-level hazards orfailure modes were identified as a result of this review.An SHA evaluation of sub-system level software

failures, including software common causefailures and cyber security events/cyber-attacks, to determine their impact on the identified system-level
hazards, concluded that potential sub-system level software failures would notlead to different types of accidents or impact plant USAR analyses.

A turbine trip evaluation determined the total system failure probability of both the existing TCSand the upgraded TCS to be essentially identical, 1.142E-6 and 1.08E-6 respectively.

Attachment RA 15-0013Page 4 of 11Evaluation Number: 59 2012-0003 Revision:

0Title: Replace current Number 1 Seal inserts in the four Wolf Creek Model 93A-1 ReactorCoolant Pumps (RCP's) with a modified design called the Shield Shutdown Seal(SDS)Activity

==

Description:==

The Number 1 Seal inserts in the four Wolf Creek Model 93A-1 Reactor Coolant Pumps (RCPs)were replaced with a modified design called the Shield Shutdown Seal (SDS). The affectedSystems, Structures, Components (SSC's) are the Number 1 Seal inserts in RCPs PBB01A, B,C, and D. The activity includes the preparation of design and configuration change documents, procurement, and actual installation of the SDS in Refuel 19.The SDS integrated new features into the existing Number 1 Seal insert and is locateddownstream of the current film-riding face seal. A shoulder is machined into the inner diameterat the top flange and bore machined into the groove diameter above the shoulder.

SDS sealingrings and a thermal actuator are then placed into the shoulder and bore respectively.

This activity was performed to reduce the impact of loss of all RCP seal cooling which is mostlikely to occur during loss of all on-site and off-site AC power (Station Blackout (SBO)). Thisimproves margin to a severe core damage event. SBO is the dominant core damage event forWCGS.50.59 Evaluation:

The SDS is designed to only deploy on a stationary RCP shaft and only after all seal coolinghas been lost and the seal temperature rises to a prescribed temperature.

The SDS willactuate when a wax material within the actuator assembly melts. Actuators are factory-tested to verify repeatable operation within their design temperature range (250 degrees F to 300degrees F). With WCGS at 100 percent power, the number 1 seal temperatures indicate 130degrees F.The frequency of SDS inadvertent actuation is 1.2 E-06 events per pump-year of operation or4.8 E-06 per year for a four-loop plant. This is a very low probability of occurrence; thus it isconcluded that inadvertent actuation of an SDS during normal plant operation has negligible contribution to the overall frequency of a forced shutdown of the plant from all causes which isabout 1 E-01 per year including forced outages due to RCP issues which is about 6 E-02 peryear. Thus, the frequency of this previously evaluated event is not increased due to SDSinstallation.

The evaluation concluded that no new accident is created or any existing analyzed accident ismade worse, including the consequences.

There are no new, unanalyzed failures introduced because of this change in design of the number 1 RCP seal insert.

Attachment RA 15-0013Page 5 of 11Evaluation Number: 59 2012-0004 Revision:

0Title: Steam Generator Feed Pump Protection and Control System UpgradeActivity

==

Description:==

The existing WCGS Steam Generator Feed Pump (SGFP) protection and control of theGeneral Electric MDT-20 system and electro-hydraulic controls was upgraded with a Distributed Control System (DCS) supplied by Westinghouse.

The digital replacement system is basedupon the Ovation platform supplied by Emerson Process Management (EPM). The normalfunction of the SGFP protection and control system is to generate position signals for the HighPressure and Low Pressure control valves, the SGFP recirculation valves, and the condensate pump recirculation valves. Changing the position of the steam valves provides the method ofcontrolling the SGFP turbine speed. Using the system, the SGFP turbines are capable ofoperation from a shutdown state to full load.The function and performance of the SGFP protection and control system as described in theUSAR, is not being changed, with the exception being the elimination of the existing electrical overspeed trip valves, associated test solenoid valves, and the mechanical overspeed tripelimination.

The SGFP protection and control system upgrade eliminates existing Single PointVulnerabilities.

50.59 Evaluation:

The SGFP protection and control system is non-safety related and the modification does notchange the function or performance requirements for the system. The SGFP protection andcontrol system upgrade does not change any plant operating parameters that would result inincreased challenges to important safety components or the frequency of any accidentdescribed in the USAR. Furthermore, no new interface requirements with important to safetycomponents that function to limit the consequences of an accident are established by thisupgrade.The removal of the mechanical overspeed trip mechanism and the electrical overspeed tripvalves has no impact on accident mitigation or the consequences of an accident.

The function of tripping the SGFPs is not part of the primary success path for accidentmitigation and does not impact any USAR transient or accident analyses.

The WCGS specific SGFP protection and control system upgrade Software Hazards Analysis(SHA) evaluated the SGFP protection and control system upgrade related system-level hazardsand concluded that the results would be bounded by the results of malfunctions or accidents previously considered in the USAR.The evaluation determined that the results of potential SGFP protection and control systemupgrade failures are enveloped by the current USAR Chapter 15 analyses and no new system-level hazards or failure modes were identified as a result of this review.An SHA evaluation of sub-system level software

failures, including software common causefailures and cyber security events/cyber-attacks, to determine their impact on the identified system-level
hazards, concluded that potential sub-system level software failures are boundedby or do not impact the USAR accident analyses previously considered.

Attachment RA 15-0013Page 6 of 11Evaluation Number: 59 2013-0001 Revision:

0Title: Turbine-Driven Auxiliary Feedwater Pump Controls Replacement Activity

==

Description:==

The analog governor controls for the Turbine Driven Auxiliary Feedwater Pump (TDAFWP) areobsolete.

This change replaced the equipment with a new digital platform for the turbinegovernor controls and replaced the Trip and Throttle (T&T) Valve (FC HV 0312) starter controls.

This change consists of the following:

Replacement of the local control panel with new Original Equipment Manufacturer suppliedcontrols based on a digital platform for governor controls and new motor starter for the DCmotor operator for the T&T Valve.The Operator Manual/Auto stations on the Main Control Board and the Auxiliary ShutdownPanel (RP1 18B) will be replaced with new simplified stations compatible with the new controls.

The electrohydraulic actuator for the governor valve will be replaced with a new electricactuator.

The governor valve linkage arm and bracket will be eliminated with a new actuator bracket,aligning the actuator to a direct linear arrangement with the governor valve stem.Replacement of the Foxboro Spec 200 control loops that supported the old Manual/Auto stations and speed setpoint and provided control signal isolation for Control Room Fire SafeShutdown with a simple isolation device for the 24VDC circuit in the Main Control Board.50.59 Evaluation:

The impact on the Auxiliary Feedwater System and the accidents listed in the USAR Chapter 15were reviewed.

The change to the plant and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.

There is no adverse impact to the provisions to prevent the accumulation of condensate in theturbine steam supply lines and no lessening of the system's ability to operate with steam inletpressures ranging from 92 to 1,290 psia, as defined in the original specification M-021 andverified in the original turbine qualification testing contained in M-021-00087.

The design continues to meet the requirements defined for the exhaust line to remain functional after a Safe Shutdown Earthquake and or to perform its intended function following a postulated hazard, such as internal missile or pipe break.

Attachment RA 15-0013Page 7 of 11Evaluation Number: 59 2013-0002 Revision:

0Title: HKE25 Conveyer Car Operation with Removal of the Hold Down LatchActivity

==

Description:==

The hold down latch on the fuel handling conveyer car was removed as the hold down latchwas not engaging all the time on the reactor end of the system. The fuel bundle needs to beplaced in the horizontal position to allow for transport of the fuel bundle to the spent fuel pool(SFP). The hold down latch is a mechanical latch device on the transfer car that is opened bythe car moving into position in the horizontal position.

The conveyer car was moving intoposition but the latch was not latching when loaded with a bundle and ready to return to the fuelbuilding from the upender pit in the reactor building.

This change removed the hold down latchand allowed positioning the fuel bundle from the vertical to the horizontal position for transport to the SFP.50.59 Evaluation:

The removal of the hold down latch from the conveyer car, with the compensating action ofvisual verification of the car in the proper position for upending, remains a reliable means forhandling the fuel assemblies.

The conveyer car shall be utilized in the manual mode when thehold down latch is removed.

Two redundant interlocks allow a lifting arm operation only whenthe transfer car is at the respective end of its travel on the reactor side as well as on the fuelbuilding side, one of these interlocks is the position switch, the other is the hold down latch thatthis modification is removing.

The position switch is the primary device with the hold down latchbeing the backup. Removal of the hold down latch will remove the redundancy but this featurewill be compensated for by visual examination and verification that the car is at its properposition for upending the fuel by utilizing the positions arrows.The removal of the hold down latch and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.

Attachment RA 15-0013Page 8 of 11Evaluation Number: 59 2013-0002 Revision:

ITitle: HKE25 Conveyer Car Operation with Removal of the Hold Down LatchActivity

==

Description:==

The hold down latch on the -fuel handling conveyer car was removed as the hold down latchwas not engaging all the time on the reactor end of the system. The fuel bundle needs to beplaced in the horizontal position to allow for transport of the fuel bundle to either the spent fuelpool (SFP) or the refueling pool. The hold down latch is a mechanical latch device on thetransfer car that is opened by the car moving into position horizontally.

The conveyer car wasmoving into position but the latch was not actuating, preventing the fuel bundle from pivotingfrom the horizontal to the vertical position.

Removing the hold down latch allowed for upendingthe fuel bundle for transporting it to the SFP or refueling pool. Revision 0 only allowed fuelmovement to the SFP, while revision 1 also allows fuel movement to the refueling pool.50.59 Evaluation:

The removal of the hold down latch from the conveyer car, with the compensating action ofvisual verification of the car in the proper position for upending, provides a reliable means forhandling the fuel assemblies.

The conveyer car shall be utilized in the manual mode when thehold down latch is removed.

Two redundant interlocks allow a lifting arm operation only whenthe transfer car is at the respective end of its travel on the reactor side as well as on the fuelbuilding side, one of these interlocks is the position switch, and the other is the hold down latchthat this modification is removing.

The position switch is the primary device with the hold downlatch being the backup. Removal of the hold down latch will remove the redundancy but thisfeature will be compensated for by visual examination and verification that the car is at itsproper position for upending the fuel by utilizing the positions arrows.The removal of the hold down latch and the implementation activities are bounded by thecurrent WCGS accident and failure analyses.

Attachment RA 15-0013Page 9 of 11Evaluation Number: 59 2013-0003 Revision:

0Title: Probable Maximum Precipitation (PMP) Flood Calculations Activity

==

Description:==

WCGS Flood Calculation XX-C-023 is the Analysis of Record for determining the maximumflood elevation at WCGS. This calculation was updated and replaced by 3 new floodcalculations as listed below: The new flood calculations were developed using the guidanceprovided in NUREG/CR

-7046 so it is compatible with WCGS's Fukushima response toperform a flooding hazard re-evaluation for the site.Calculation 69461-C-001:

determines the Probable Maximum Precipitation (PMP) usingprocedures outlined in Hydrometeorological Report No. 52 for WCGS.Calculation 69461-C-002:

determines the peak discharge associated with the PMP that wascalculated in Calculation No. 69461-C-001 using procedures outlined in Hydrometeorological Report No. 52 for the WCGS. This calculation uses the data developed within the Calculation No. 69461-C-001 as input to the computer program Hydrologic Engineering Center -Hydrologic Modeling System (HEC-HMS) version 3.5.Calculation 69461-C-003:

estimates water surface elevations at WCGS for the PMP event. Thepeak discharges determined from Calculation No. 69461-C-002 are used as input into theUSACE Hydrologic Engineering Center River Analysis System (HEC-RAS) software todetermine the water surface elevations throughout the site.50.59 Evaluation:

NUREG/CR-7046 requires that the water surface elevation near a safety-related buildingproduced by the PMP be less than the floor elevation.

While the calculated water surfaceelevations varied across the site, modeling results indicated that all safety-related buildinglocation flood stages are less than the floor elevation using the methodology and guidanceprovided in NUREG/CR

-7046.The new calculations use methods that have been approved by the NRC for the intendedapplication (NUREG/CR-7046).

Additionally, they do not change how WCGS uses the floodinformation to operate or control SSCs to prevent flood events from adversely affecting SafetyRelated Seismic Category 1 Structures.

The results from the new flood calculations are similarto the existing calculation of record (XX-C-023) except these provide more site-specific information.

Compared with the existing flood calculation the new calculations slightly reducemargin at the north end of the powerblock and improve margin to the south, and are considered conservative or essentially the same and continue to meet the acceptance criteria.

Attachment RA 15-0013Page 10 of 11Evaluation Number: 59 2014-0001 Revision:

0Title: Thermocouple/Core Cooling Monitor UpgradeActivity

==

Description:==

The Thermocouple/Core Cooling Monitor (TCCM) combines the functions of monitoring forexcessive core exit thermocouple temperatures and monitoring both core exit thermocouple temperatures and hot and cold leg temperatures for saturation margin. The TCCM System hasexperienced obsolescence and reliability issues that have caused system components andmodules to be degraded or fail.The WCGS TCCM upgrade involved replacement of the existing microprocessor-based systemsupplied by Westinghouse.

The replacement system is based upon the Advanced LogicSystem (ALS) supplied by Westinghouse.

The ALS platform was installed at WCGS as areplacement of Main Steam and Feedwater Isolation System (MSFIS) equipment.

An ALS Service Unit (ASU) is allocated for each train of the TCCM and resides entirely withinthe TCCM cabinet.

The ASU consists of a PC Node Box and a Flat Panel Display.

ASUdisplays core temperatures, pressures, channel calibration, system status and enables theperformance of system test and calibration activities.

The implementation of the ASU is basedon the Common Qualified (Common Q) Platform defined in Westinghouse WCAP-16097-P-A, "Common Qualified Platform Topical Report."50.59 Evaluation:

NUREG-0737, "Clarification of TMI Action Plan Requirements,"

specifies the functional requirements for the TCCM. WCGS USAR Chapter 18, section 18.2.13 describes how theTCCM complies with NUREG-0737 requirements.

The function and performance of the TCCMas described in the USAR, is not being changed.WCGS USAR Chapter 7, Table 7A-3, addresses TCCM compliance with Regulatory Guide 1.97requirements for post-accident monitoring indication.

No changes are required for Regulatory Guide 1.97 compliance as described in the Table 7A-3 data sheets as a result of the TCCMupgrade because exactly the same functions in the original TCCM are replicated in thereplacement TCCM.Each train of the ALS platform-based TCCM includes an ASU. The ASU consists of a PC NodeBox and a Flat Panel Display.

The implementation of the ASU is based on the Common QPlatform described in WCAP-16097-P-A, "Common Qualified Platform Topical Report."

TheCommon Q platform is a set of commercial-grade hardware and previously developed softwarecomponents dedicated and qualified for use in nuclear power plants. The NRC has reviewedand approved the Common Q system for installation in safety related applications.

WCAP-16097-P-A includes the NRC SER for the Common Q platform.

The built-in diversity features provided by the ALS platform significantly reduces the potential for common cause failures in TCCM functions as compared to the existing microprocessor based TCCM.

Attachment RA 15-0013Page 11 of 11Evaluation Number: 59 2014-0002 Revision:

0Title: ESW Below Ground Plant Tie-In Approval and Component Abandonment Activity

==

Description:==

The Essential Service Water (ESW) system has experienced localized degradation in buriedpiping in the form of tuberculation,

pitting, and through-wall leakage.

WCGS replaced andredesigned the below ground ESW piping.The buried ESW Train "A" and "B" supply and return piping including the warming lines andaccess vaults were replaced and rerouted.

The supply and return piping was routed to the newcirculating water crossing and required seismic support to alleviate potential concern associated with a circulating water line break washing out bedding below the new ESW. The return pipingwas rerouted to a new discharge point located in the ultimate heat sink (UHS). The changeabandoned the original discharge structure.

The warming lines were rerouted from the returnpiping through penetrations into the ESW pumphouse forebays.

New access vaults wereinstalled periodically along the new ESW system piping route.This ESW system change involved revising the current tornado-generated missile protection and freeze protection configuration and seismic support configuration for portions of the ESWbelow ground piping and components.

50.59 Evaluation:

The change to the ESW missile and freeze protection

.configuration, seismic supportconfiguration, and new discharge structure will continue to provide protection against the effectsof natural phenomena, such as earthquakes, tornadoes, hurricanes, floods, and externalmissiles.

The changes do not reduce the capabilities of the ESW system in performance of thefunctions described in the USAR and the system and equipment will continue to meet all of theirexisting safety design bases. The failure modes and effects analysis for the ESW system is notaffected by the change.The USAR was reviewed to identify the accidents/transients previously evaluated that arepotentially affected by the change to ESW piping and the seismic support configuration.

Theyare the steam generator tube rupture (SGTR) and the Loss-of-coolant accident (LOCA)resulting from a spectrum of postulated piping breaks within the reactor coolant pressureboundary.

The Station Blackout (SBO) analysis was also reviewed.

The new ESW missile and freeze protection configuration, seismic support configuration, andnew discharge structure provides all the capabilities and functions present in the existingconfiguration and will not create any additional failure modes. After implementation, the ESWsystem continues to be capable of supplying the minimum flow rates required to remove heatfrom the containment and necessary safety-related components from a postulated design basisaccident (DBA) and dissipate it to the ultimate heat sink, including the SBO coping time of fourhours. The ESW system will continue to be capable of removing heat from plant components necessary to achieve and maintain post-fire or post-accident safe shutdown.

The ESW system will continue to be available for the mitigation of the effects associated withthe limiting DBAs and transients previously evaluated in the USAR. Therefore, all assumptions utilized within USAR-described dose analyses remain valid and bounding.