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HARTFORD, CONNECTICUT 06141-0270 L    L    J C%,[,3C2fC                                                (203) 605-5000 December 4, 1990 Docket No. 50-423 B.11bl.Q Re: 10CFR50.90 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555
 
==Reference:==
(1)    E. J. Mroczka letter to the U.S. Nuclear Regulatory Commission,      Proposed      Revision          to      Technical Specifications,      Cycle  4    Reload      Submittal, dated November 1, 1990.
Gentlemen:
Mill: tone Nuclear Power Station, Unit No. 3 Proposeo Changes to Technical Specifications
[vele 4 Reload Submittai - Boron Dilution Analysis Gn November 1,1990, Northeast Nuclear Energy Company (NNECO) submitted a proposed amendment to Facility Operating License NPF-49 for Millstone Unit No. 3 (Reference (1)).                The proposed amendment would revisa several Technical Specifications in support of refueling and operation for i          Millstone Unit No. 3 with the VANTAGE 5 Hybrid (5H) improved fuel design.
In Reference (1), NNECO also indicated that the boron dilution analysis was being finalized at that time and the results of the analysis and Technical Specification changes related to the analysis would be submitted in a future submittal. Therefore, pursuant to 10CFR50.90, NNEC0 hereby proposes to amend Operating License NPF-49 by incorporating the attached proposed changes into the Technical Specifications of Millstone Unit No. 3.                                A description of the proposed change is provided in Attachment 1.                                The revised pages of the Technical Specifications are provided in Attachment 2.
Discussion The plant safety evaluation presented in Reference (1)                              includes all accident evaluations except an evaluation for uncontrolled boron dilution.
Attachment 3 provides the results of the boron dilution analysis in Mooes 1 through 6 performed for Millstone Unit No. 3 as part of the upgrade to VANTAGE SH fuel.              The analysis presented in Attachment 3 includes an identification of causes and a description of the accident, limiting dilution flow path description, safety functions and mitigating systems, safety analysis criteria & regulatory requirements, method of analysis, and rele, ant conclusions.                For operating Modes 1 through 5, the results l          presented in Attachment 3 show that adequate time is available for the i          operator to manually terminate the source of dilution flow, assuming the j          specified shutdown margin requirements are met.
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U.S. Nuclear Regulatory Commission B13678/Page 2 December 4, 1990 Following termination of the dilution flow, the operator can initiate reboration to recover the shutdown margin.        No analysis is presented for Mode 6 operation, since dilution during refueling is precluded by the indicated administrative controls, similar to those used for Technical Specification 3.6.1.1.
Sionificant Hazards Consideration NNECO has reviewed the proposed changes in accordance with 10CFR50.92(c) and has concluded that the changes do not involve a significant hazards consideration. The basis for this conclusion is that the three criteria of 10CFR50.92(c) are not compromised. The proposed changes do not involve a significant hazards consideration because the changes would not:
: 1. Involve a significant increase in the probability or consequences of an accident previously analyzed.
To determine any potential impact, the proposed changes can be grouped into two categories. These are:
: a. Changes    to Technical Specifications due to boron dilution analysis performed as part of the upgrade to VANTAGE 5H fuel.
: b. Changes that are not related to the boron dilution analysis and are administrative in nature such as renumbering of pages from the existing Technical    Specifications    to accommodate  a new l            Technical Specification and to allow removal of " intentionally blank" pages from Technical Specifications.
Each of these groups of changes is discussed below:
: a. As discussed above and in Attachment 3, the boron dilution analysis was performed for Modes 1 through 6 for Millstone Unit No. 3 as part of the upgrade to VANTAGE SH fuel. The boron dilution in the Modes 1 through 5 calculation determines the amount of time a vallable for operator mitigation of the dilution prior to the loss of shutdown margin. Acceptable response time l            .for the various modes must be greater than or equal to the following (as per Standard Review Plan 15.4.6):
Mode 6        Refueling            30 Minutes Mode 5        Cold Shutd)wn        15 Minutes Mode 4        Hot Shutdoin          15 Minutes Mode 3        Hot Standby          15 Minutes Mode 2        Startup              15 Minutes Mode 1        Power                15 Minutes for Operating Modes 1 through 5, the results presented in Attachment 3 show that adequate time is available for the
 
U.S. Nuclear Regulatory Commission B13678/Page 3 December 4, 1990 operator to manually terminate the source of dilution fl ow.
Meeting these operator response times verifies that the condition of the plant at any point in the transient is within the bounds of those calculated for other Final Safety Analysis Report (FSAR)
Condition 11 transients. No analysis is presented for Mode 6 operation, since dilution during refueling is precluded by the indicated    administrative control s.                    Therefore, there is no increase in the consequences due to the boron dilution accident.
The probability of occurrence is not affected since dilution sources are not changed. Moreover, in the cases of Mode 5 drained or Mode 6 where dilution source valves are secured, occurrence of a dilution event is precluded by the indicated administrative controls similar to those used for Technical Specification 3.6.1.1.                    As stated in Attachment 3, the existing design for the detection of an inadvertent boron dilution event is a temporary system that is set up within the control room. A new system will be provided as a permanent Class lE installation.
The failure of these monitors will not change the probability of the occurrence of the boron dilution accident. In fact, this system will improve the accuracy and reliability over the existing system.
: b. The renumbering of pages and removal of blank pages do not reduce the effectiveness of the Technical Specifications.                      Also, these changes    do  not affect the existing or proposed limiting conditions      for operation or                      surveillance    requirements.
Therefore, there is no impact on the design basis accidents.
On the basis of this review, NNECO concludes that there is no significant increase in the probability or consequences of an accident previously analyzed.
: 2. Create the possibility of a new or different kind of accident from any previously analyzed.
: a. The failure modes associated with the new shutdown margin monitor cannot be an initiating event for the design basis accident.
Therefore, the failure raodes associated with the shutdown margin monitor do not represent a new unanalyzed accident. The existing boron dilution analysis fully covers all existing failure modes.
There are no new failure modes introduced by these changes.
: b. Since these changes do not affect plant operation, the potential for an unanalyzed accident is not created. No new failure modes are introduced. Based on the above, NNECO concludes that the proposed changes do not create any new or different kind of accident from those previously analyzed.
 
l U.S. Nuclear Regulatory Commission B13678/Page 4 December 4, 1990
: 3. Involve a significant reduction in a margin of safety.
: a. No increase in consequences was identified above as a result of the proposed changes.                                Therefore, the impact of the consequences on the protective boundaries is unchanged. The boron dilution analysis included in Attachment 3 has confirmed that the operator has adequate time to manually terminate the source of dilution fl ow. Meeting these operator response times verifies that the condition of the plant at any point in the transient is within the bounds of those calculated for other FSAR Condition 11 iransients. Therefore, verification of no change in margin of safety is encompassed in meeting the required operator response times,
: b. Since the proposed changes do not affect the consequences of any accident previously anal"'ed, there is no reduction in the margin of safety.
Moreover, the Commission has provided guidance concerning the application of the standards in 10CFR50.92 by providing certain examples (March 6, 1986, SIFR7751) of amendments that are considered not likely to involve a significant hazards consideration.                                                                    Although the proposed changes are not enveloped by a specific example, the proposed changes related to the boron dilution analysis would not involve a significant                                                                                  increase in the probability or consequences of an accident previously analyzed.                                                                                  For 03erating Modes 1 through 5, the results presented in Attachment 3 show tlat adequate time is available for the operator to manually terminate the source of dilution flow. No specific analysis is presented for Mode 6 operation, since dilution during refueling is precluded by the indicated administrative controls similar to those used for Technical                                                                                  Specifi-cation 3.6.1.1. For other Technical Specification changes, there is no increase in the consequences of an accident previously analyzed.
Therefore, based on the above, NNECO concludes that the proposed Technical Specification changes do not involve a significant hazards consideration.
Based    upon      the  information                              contained                                              in this submittal  and the environmental assessment for Millstone Unit No. 3, there are no significant radiological or nonradiological                                                            impacts associated with the proposed action, and that the proposed license amendment will not have a significant affect on the quality of the human environment.
The Millstone Unit No. 3 Nuclear Review Board has reviewed and approved the attached    proposed      revisions and has concurred with the above determinations.
In accordance with 10CFR50.91(b), we are providing the State of Connecticut 4
with a copy of the proposed amendment.
 
                                                                                    )
V.S. Nuclear Regulatory Commission B13678/Page 5 December 4, 1990 We believe the above information, coupled with the information provided in Reference (1), provides a complete basis for approval of the requested amendment. Of course, should the Staff have any additional questiens, we remain available to discuss the Staff's concerns.
Very truly yours, NORTHEAST NVCLEAR ENERGY COMPANY
                                                            /
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Senio,r Vice President cc:    T. T. Martin, Region 1 Administrator D. H. Jaffe, NRC Project Manager, Millstone Unit No. 3 W. J. Raymond, Senior Resident Inspector, Millstone Unit Nos. 1, 2, and 3 Mr. Kevin McCarthy Director, Radiation Control Unit Department of Environmental Protection Hartford, CT 06116 STATE Of CONNECTICUT)
                              ) ss. Berlin COUNTY OF HARTFORD )
Then personally appeared before me, E. J. Mroczka, who being duly sworn, did state that he is Senior Vice President of Northeast Nuclear Energy Company, a Licensee herein, that he is authorized to execute and file the foregoing information in the name and on behalf of the Licensee herein, and that the statements contained in said information are true and correct to the best of his knowledge and belief.
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Docket ' . 50-423 B13678 Attachment 1 Millstone Nuclear Power Station, Unit No. 3 Description of Proposed Technical Specification Changes Cycle 4 December 1990
 
s Attachment 1 B13678/Page 1                                                                                1 December 4, 1990                                                                              ,
Millstone Nuclear Power Station, Unit No. 3 Description of Proposed Technical Soecification Chanaes. Cycle 4 In a letter dated November              1, 1990, Northeast Nuclear Energy Company (NNECO) submitted a proposei license amendment for Millstone Unit No. 3.                      ,
The proposed amendment would revise several Technical Specifications in support of_ refueling snd operation for Millstone Unit No. 3 with the VANTAGE 5 Hybrid (SH) improved fuel design.                In that letter, NNECO indi-cated that the boron dilution analysis was being finalized and the results of the analysis and corresponding Technical' Specification changes would be provided in a future submittal. Westinghouse under the contract of NNEC0 has completed the boron dilution analysis in. Modes 1 through 6 for Millstone Unit No. 3 as part of ' the upgrade to VANTAGE SH fuel. The proposed Technical Specification changes related to the boron dilution analysis are summarized below:
A .-      Technical Specification Chances Due to 'the Boron Dilution Analysis
: 1.  -Section 3.1.1.1.2. Shutdown Marain' Modes 3. 4. and 5 Loops Filled Section 3.1.1.1, Boration Control has been split into two; one for Modes 1 and 2 and the other for Modes 3,- 4 and 5 with loops filled. The Technical Specification changes related to Modes 1 and 2 were described in Reference (1). For Modes 3, 4 and 5, the shutdown margin is provided in Figures 3.1-1 (four loops--
Mode 3), 3.1-2 -(three loops--Mode 3), 3.1-3 (Mode 4) and 3.1-4 (Mode 5 with Loops Filled). These figures show the required shutdown margin, as a function of critical boron concentration, to ensure at least 15 minutes from the time of the flux multipli-cation alarm to loss of shutdown margin. A 10-second response '
time is considered in the development of the shutdown margin requirements.
!                          2. Section 3.l'.l.2. Shutdown Marain--Cold Shutdown--Looos Not Filled In Mode 5 drained (loops not filled) an . option is available to either require a larger shutdown margin per Figure 3.1 (new figure) or-preclude a boron dilution accident by securing 'dilu-tion flow paths 'and - maintaining the same L shutdown margin as required for. Mode 5 with loops filled per Figure 3.1-4.
: 3. Section 3.1.2.1. Boration Systems--Flow Path--Shutdown Section 3.1.2.2. Boration Systems--Flow Paths--0Deratina The proposed change of wording tof Specifications 3.1.2.1.a and 3.1.2.2.a are necessary to make these specifications consistent with- the Millstone Unit No. 3 design and the wording of specifications 3.1.2.5 and 3.1.2.6.          This snecification will allow the use of either one boric acid tank or two.
L
 
  . --            .    .- .      -. . - - .                    . - . . - . _ ~        -..      .- . -    - -  - - .
1 Attachment 1L B13678/Page 2 December 4, 1990 in addition, the Specification 3.1.2.2 ACTION statement has been revised to reflect the new figure 3.1-4.
: 4. Section 3.1.2.4. Charaina Pumos. Operatino-The Specification 3.1.2.4 ACTION Statement has been revised to reflect the new Figure 3.1-4.
: 5. Section 3.1.2.6. Borated Water Sources. Operatina A revision to Section 3.1.2.6 was submitted in Reference (1).
Additional changes are necessary as a result of the boron dilution analysis.          The Specification 3.1.2.6 ACTION Statement has ~ been revised to reflect the new figure 3.1-4. A change of                                    .
                      " contained          volume"  to    " usable              volume"    is proposed in              !
  ,                  Specification 3.1.2.6.a to allow use of both tanks or one.                        The minimum volume required depends upon the usable volume in the                                      i boric acid storage tanks and the number of tanks in use.                            A usable volume of 21,020 gallons sheuld be required in Modes 1, 2, 3 and 4' for Specification 3.6.1.2.a. The unusable volume in each boric- acid storage tank is 1300 gallons.
: 6. Table 3.3-1. Reactor. Trio Instrumentation Table 4.3-1. Reactor Trio- Instrumentation Surveillance Reauire-ments Mills ne Unit No. 3 will be installing a new shutdown margin
                    . monitor which will be used in place of the existing (function unit 6b -of' Table 3.3-1) manual high flux monitor at -shutdown.
The new shutdown margin monitor has two channels for redundancy and provides an alarm which alerts the operator to a boron dilution. Therefore, Table 3.3-1 functional unit 6b has been deleted and functional unit 21 has been added to Table 3.3-1.
Functional Unit 6C has been relabeled as 6b. - In addition, ACTION statements are -proposed -for one .-less than minimum and for no
,                    channels operable. ~ The proposed surveillance requirements- for l:                    this. new shutdown margin monitor. in Table 4.3-1 are consistent l
with the general philosophy - of the -Westinghouse Standard
                    --Technical Specifications. In addition, the : alarm setpoint for the- shutdown margin monitor will                          be; included in the Core Operating Limits' Report (COLR).                Note 9 to Table 4.3-1 has been revised to delete reference to the previous high flux at shutdown alarm and a new Note 19 to Table 4.3-1 has been added to reflect the surveillance requirement' of a new shutdown margin monitor.
1
 
Attachment 1 B13678/Page 3 December 4, 1990
: 7. Section 3.4.1.4.2. Cold Shutdown--Looos Not Filled Section 3.9.1.1. Refuelina Operations--Boron Concentration A revision to Section 3.9.1.1 was submitted in Reference (1).
Additional changes are necessary as a result of the boron dilution analysis.
The limiting condition for operation has been revised that will require certain valves in the chemical and volume control system (CVCS) to be secured to preclude a boron dilution event.            A list of the valves is included in this specification that requires verification at least once per 31 days that these valves are closed and locked or under administrative controls.
: 8. Section 3.4.1.6. Isolated looo Startuo A revision to Section 3.4.1.6 was submitted in Reference (1).
Additional changes are necessary as a result of the boron dilution analysis. Specification 3.4.1.6.d and Surveillance 4.4.1.6.2 have been revised to make this specification consistent with Specification 3.1.1.1.2 and 3.1.1.2 and 3.9.1.1.
: 9. Bases Sections 3/4.1.1.1 and 3/4.1.1.2. Shutdown Marain Bases Section 3/4.1.2. Boration Systems Bases Section 3/4.4.1. Reactor Coolant loops and Coolant Circula-11011 Base Section 3/4.9.1 Boron Concentration A revision to the above sections was submitted in Reference (1).
Additional changes to these sections are being proposed to reflect the proposed Technical Specifications.
B. Other Technical Soecification Chanaes
: 1. Renumberir.a of Technical Specification Paaes Pages 3/4 1-1 through 3/4 1-23 are being renumbered to accom-modata the new Specification 3.1.1.1.2 and to delete the blank page; from Technical Specifications which were left by Amendment
: 50. As a result of the above, appropriate pages of the Technical Spucification Index were also revised.              Page 3/4 1-17 (Section 3.1.2.5), and Page 3/4 1-25 (Section 3.1.3.4) were submitted in Reference (1). These two pages are being resubmitted as a result of the renumbering of pages. In addition, Page 3/4 2-26 was also submitted in Reference (1) and is being resubmitted to reflect recently approved Amendment No. 57.
 
                                                                              .i o
4 Attachment 1 B13678/Page 4 December 4, 1990
 
==Reference:==
(1) E. J. Mroczka letter to the U.S. Nuclear Regulatory Commission,  Cycle 4,    Reload Submittal,  dated November 1, 1990.
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Latest revision as of 04:42, 6 January 2021

Application for Amend to License NPF-49,changing Tech Specs Re Boron Dilution Analysis for Cycle 4 Reload
ML20065P179
Person / Time
Site: Millstone Dominion icon.png
Issue date: 12/04/1990
From: Mroczka E
NORTHEAST NUCLEAR ENERGY CO., NORTHEAST UTILITIES
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20065P184 List:
References
B13678, NUDOCS 9012130146
Download: ML20065P179 (10)


Text

- . .

4 EAST UTILtTIES con , i Omc. . se.n sire.i, eernn. connecncui 1 .w. .u. e. u m u, '

P O BOX 270

.u m 9. .w . r.-~

HARTFORD, CONNECTICUT 06141-0270 L L J C%,[,3C2fC (203) 605-5000 December 4, 1990 Docket No. 50-423 B.11bl.Q Re: 10CFR50.90 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555

Reference:

(1) E. J. Mroczka letter to the U.S. Nuclear Regulatory Commission, Proposed Revision to Technical Specifications, Cycle 4 Reload Submittal, dated November 1, 1990.

Gentlemen:

Mill: tone Nuclear Power Station, Unit No. 3 Proposeo Changes to Technical Specifications

[vele 4 Reload Submittai - Boron Dilution Analysis Gn November 1,1990, Northeast Nuclear Energy Company (NNECO) submitted a proposed amendment to Facility Operating License NPF-49 for Millstone Unit No. 3 (Reference (1)). The proposed amendment would revisa several Technical Specifications in support of refueling and operation for i Millstone Unit No. 3 with the VANTAGE 5 Hybrid (5H) improved fuel design.

In Reference (1), NNECO also indicated that the boron dilution analysis was being finalized at that time and the results of the analysis and Technical Specification changes related to the analysis would be submitted in a future submittal. Therefore, pursuant to 10CFR50.90, NNEC0 hereby proposes to amend Operating License NPF-49 by incorporating the attached proposed changes into the Technical Specifications of Millstone Unit No. 3. A description of the proposed change is provided in Attachment 1. The revised pages of the Technical Specifications are provided in Attachment 2.

Discussion The plant safety evaluation presented in Reference (1) includes all accident evaluations except an evaluation for uncontrolled boron dilution.

Attachment 3 provides the results of the boron dilution analysis in Mooes 1 through 6 performed for Millstone Unit No. 3 as part of the upgrade to VANTAGE SH fuel. The analysis presented in Attachment 3 includes an identification of causes and a description of the accident, limiting dilution flow path description, safety functions and mitigating systems, safety analysis criteria & regulatory requirements, method of analysis, and rele, ant conclusions. For operating Modes 1 through 5, the results l presented in Attachment 3 show that adequate time is available for the i operator to manually terminate the source of dilution flow, assuming the j specified shutdown margin requirements are met.

h b,i os34n nty 4-es 9012130146 901204 DR ADOCK 0500 3 p

U.S. Nuclear Regulatory Commission B13678/Page 2 December 4, 1990 Following termination of the dilution flow, the operator can initiate reboration to recover the shutdown margin. No analysis is presented for Mode 6 operation, since dilution during refueling is precluded by the indicated administrative controls, similar to those used for Technical Specification 3.6.1.1.

Sionificant Hazards Consideration NNECO has reviewed the proposed changes in accordance with 10CFR50.92(c) and has concluded that the changes do not involve a significant hazards consideration. The basis for this conclusion is that the three criteria of 10CFR50.92(c) are not compromised. The proposed changes do not involve a significant hazards consideration because the changes would not:

1. Involve a significant increase in the probability or consequences of an accident previously analyzed.

To determine any potential impact, the proposed changes can be grouped into two categories. These are:

a. Changes to Technical Specifications due to boron dilution analysis performed as part of the upgrade to VANTAGE 5H fuel.
b. Changes that are not related to the boron dilution analysis and are administrative in nature such as renumbering of pages from the existing Technical Specifications to accommodate a new l Technical Specification and to allow removal of " intentionally blank" pages from Technical Specifications.

Each of these groups of changes is discussed below:

a. As discussed above and in Attachment 3, the boron dilution analysis was performed for Modes 1 through 6 for Millstone Unit No. 3 as part of the upgrade to VANTAGE SH fuel. The boron dilution in the Modes 1 through 5 calculation determines the amount of time a vallable for operator mitigation of the dilution prior to the loss of shutdown margin. Acceptable response time l .for the various modes must be greater than or equal to the following (as per Standard Review Plan 15.4.6):

Mode 6 Refueling 30 Minutes Mode 5 Cold Shutd)wn 15 Minutes Mode 4 Hot Shutdoin 15 Minutes Mode 3 Hot Standby 15 Minutes Mode 2 Startup 15 Minutes Mode 1 Power 15 Minutes for Operating Modes 1 through 5, the results presented in Attachment 3 show that adequate time is available for the

U.S. Nuclear Regulatory Commission B13678/Page 3 December 4, 1990 operator to manually terminate the source of dilution fl ow.

Meeting these operator response times verifies that the condition of the plant at any point in the transient is within the bounds of those calculated for other Final Safety Analysis Report (FSAR)

Condition 11 transients. No analysis is presented for Mode 6 operation, since dilution during refueling is precluded by the indicated administrative control s. Therefore, there is no increase in the consequences due to the boron dilution accident.

The probability of occurrence is not affected since dilution sources are not changed. Moreover, in the cases of Mode 5 drained or Mode 6 where dilution source valves are secured, occurrence of a dilution event is precluded by the indicated administrative controls similar to those used for Technical Specification 3.6.1.1. As stated in Attachment 3, the existing design for the detection of an inadvertent boron dilution event is a temporary system that is set up within the control room. A new system will be provided as a permanent Class lE installation.

The failure of these monitors will not change the probability of the occurrence of the boron dilution accident. In fact, this system will improve the accuracy and reliability over the existing system.

b. The renumbering of pages and removal of blank pages do not reduce the effectiveness of the Technical Specifications. Also, these changes do not affect the existing or proposed limiting conditions for operation or surveillance requirements.

Therefore, there is no impact on the design basis accidents.

On the basis of this review, NNECO concludes that there is no significant increase in the probability or consequences of an accident previously analyzed.

2. Create the possibility of a new or different kind of accident from any previously analyzed.
a. The failure modes associated with the new shutdown margin monitor cannot be an initiating event for the design basis accident.

Therefore, the failure raodes associated with the shutdown margin monitor do not represent a new unanalyzed accident. The existing boron dilution analysis fully covers all existing failure modes.

There are no new failure modes introduced by these changes.

b. Since these changes do not affect plant operation, the potential for an unanalyzed accident is not created. No new failure modes are introduced. Based on the above, NNECO concludes that the proposed changes do not create any new or different kind of accident from those previously analyzed.

l U.S. Nuclear Regulatory Commission B13678/Page 4 December 4, 1990

3. Involve a significant reduction in a margin of safety.
a. No increase in consequences was identified above as a result of the proposed changes. Therefore, the impact of the consequences on the protective boundaries is unchanged. The boron dilution analysis included in Attachment 3 has confirmed that the operator has adequate time to manually terminate the source of dilution fl ow. Meeting these operator response times verifies that the condition of the plant at any point in the transient is within the bounds of those calculated for other FSAR Condition 11 iransients. Therefore, verification of no change in margin of safety is encompassed in meeting the required operator response times,
b. Since the proposed changes do not affect the consequences of any accident previously anal"'ed, there is no reduction in the margin of safety.

Moreover, the Commission has provided guidance concerning the application of the standards in 10CFR50.92 by providing certain examples (March 6, 1986, SIFR7751) of amendments that are considered not likely to involve a significant hazards consideration. Although the proposed changes are not enveloped by a specific example, the proposed changes related to the boron dilution analysis would not involve a significant increase in the probability or consequences of an accident previously analyzed. For 03erating Modes 1 through 5, the results presented in Attachment 3 show tlat adequate time is available for the operator to manually terminate the source of dilution flow. No specific analysis is presented for Mode 6 operation, since dilution during refueling is precluded by the indicated administrative controls similar to those used for Technical Specifi-cation 3.6.1.1. For other Technical Specification changes, there is no increase in the consequences of an accident previously analyzed.

Therefore, based on the above, NNECO concludes that the proposed Technical Specification changes do not involve a significant hazards consideration.

Based upon the information contained in this submittal and the environmental assessment for Millstone Unit No. 3, there are no significant radiological or nonradiological impacts associated with the proposed action, and that the proposed license amendment will not have a significant affect on the quality of the human environment.

The Millstone Unit No. 3 Nuclear Review Board has reviewed and approved the attached proposed revisions and has concurred with the above determinations.

In accordance with 10CFR50.91(b), we are providing the State of Connecticut 4

with a copy of the proposed amendment.

)

V.S. Nuclear Regulatory Commission B13678/Page 5 December 4, 1990 We believe the above information, coupled with the information provided in Reference (1), provides a complete basis for approval of the requested amendment. Of course, should the Staff have any additional questiens, we remain available to discuss the Staff's concerns.

Very truly yours, NORTHEAST NVCLEAR ENERGY COMPANY

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Senio,r Vice President cc: T. T. Martin, Region 1 Administrator D. H. Jaffe, NRC Project Manager, Millstone Unit No. 3 W. J. Raymond, Senior Resident Inspector, Millstone Unit Nos. 1, 2, and 3 Mr. Kevin McCarthy Director, Radiation Control Unit Department of Environmental Protection Hartford, CT 06116 STATE Of CONNECTICUT)

) ss. Berlin COUNTY OF HARTFORD )

Then personally appeared before me, E. J. Mroczka, who being duly sworn, did state that he is Senior Vice President of Northeast Nuclear Energy Company, a Licensee herein, that he is authorized to execute and file the foregoing information in the name and on behalf of the Licensee herein, and that the statements contained in said information are true and correct to the best of his knowledge and belief.

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Docket ' . 50-423 B13678 Attachment 1 Millstone Nuclear Power Station, Unit No. 3 Description of Proposed Technical Specification Changes Cycle 4 December 1990

s Attachment 1 B13678/Page 1 1 December 4, 1990 ,

Millstone Nuclear Power Station, Unit No. 3 Description of Proposed Technical Soecification Chanaes. Cycle 4 In a letter dated November 1, 1990, Northeast Nuclear Energy Company (NNECO) submitted a proposei license amendment for Millstone Unit No. 3. ,

The proposed amendment would revise several Technical Specifications in support of_ refueling snd operation for Millstone Unit No. 3 with the VANTAGE 5 Hybrid (SH) improved fuel design. In that letter, NNECO indi-cated that the boron dilution analysis was being finalized and the results of the analysis and corresponding Technical' Specification changes would be provided in a future submittal. Westinghouse under the contract of NNEC0 has completed the boron dilution analysis in. Modes 1 through 6 for Millstone Unit No. 3 as part of ' the upgrade to VANTAGE SH fuel. The proposed Technical Specification changes related to the boron dilution analysis are summarized below:

A .- Technical Specification Chances Due to 'the Boron Dilution Analysis

1. -Section 3.1.1.1.2. Shutdown Marain' Modes 3. 4. and 5 Loops Filled Section 3.1.1.1, Boration Control has been split into two; one for Modes 1 and 2 and the other for Modes 3,- 4 and 5 with loops filled. The Technical Specification changes related to Modes 1 and 2 were described in Reference (1). For Modes 3, 4 and 5, the shutdown margin is provided in Figures 3.1-1 (four loops--

Mode 3), 3.1-2 -(three loops--Mode 3), 3.1-3 (Mode 4) and 3.1-4 (Mode 5 with Loops Filled). These figures show the required shutdown margin, as a function of critical boron concentration, to ensure at least 15 minutes from the time of the flux multipli-cation alarm to loss of shutdown margin. A 10-second response '

time is considered in the development of the shutdown margin requirements.

! 2. Section 3.l'.l.2. Shutdown Marain--Cold Shutdown--Looos Not Filled In Mode 5 drained (loops not filled) an . option is available to either require a larger shutdown margin per Figure 3.1 (new figure) or-preclude a boron dilution accident by securing 'dilu-tion flow paths 'and - maintaining the same L shutdown margin as required for. Mode 5 with loops filled per Figure 3.1-4.

3. Section 3.1.2.1. Boration Systems--Flow Path--Shutdown Section 3.1.2.2. Boration Systems--Flow Paths--0Deratina The proposed change of wording tof Specifications 3.1.2.1.a and 3.1.2.2.a are necessary to make these specifications consistent with- the Millstone Unit No. 3 design and the wording of specifications 3.1.2.5 and 3.1.2.6. This snecification will allow the use of either one boric acid tank or two.

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1 Attachment 1L B13678/Page 2 December 4, 1990 in addition, the Specification 3.1.2.2 ACTION statement has been revised to reflect the new figure 3.1-4.

4. Section 3.1.2.4. Charaina Pumos. Operatino-The Specification 3.1.2.4 ACTION Statement has been revised to reflect the new Figure 3.1-4.
5. Section 3.1.2.6. Borated Water Sources. Operatina A revision to Section 3.1.2.6 was submitted in Reference (1).

Additional changes are necessary as a result of the boron dilution analysis. The Specification 3.1.2.6 ACTION Statement has ~ been revised to reflect the new figure 3.1-4. A change of .

" contained volume" to " usable volume" is proposed in  !

, Specification 3.1.2.6.a to allow use of both tanks or one. The minimum volume required depends upon the usable volume in the i boric acid storage tanks and the number of tanks in use. A usable volume of 21,020 gallons sheuld be required in Modes 1, 2, 3 and 4' for Specification 3.6.1.2.a. The unusable volume in each boric- acid storage tank is 1300 gallons.

6. Table 3.3-1. Reactor. Trio Instrumentation Table 4.3-1. Reactor Trio- Instrumentation Surveillance Reauire-ments Mills ne Unit No. 3 will be installing a new shutdown margin

. monitor which will be used in place of the existing (function unit 6b -of' Table 3.3-1) manual high flux monitor at -shutdown.

The new shutdown margin monitor has two channels for redundancy and provides an alarm which alerts the operator to a boron dilution. Therefore, Table 3.3-1 functional unit 6b has been deleted and functional unit 21 has been added to Table 3.3-1.

Functional Unit 6C has been relabeled as 6b. - In addition, ACTION statements are -proposed -for one .-less than minimum and for no

, channels operable. ~ The proposed surveillance requirements- for l: this. new shutdown margin monitor. in Table 4.3-1 are consistent l

with the general philosophy - of the -Westinghouse Standard

--Technical Specifications. In addition, the : alarm setpoint for the- shutdown margin monitor will be; included in the Core Operating Limits' Report (COLR). Note 9 to Table 4.3-1 has been revised to delete reference to the previous high flux at shutdown alarm and a new Note 19 to Table 4.3-1 has been added to reflect the surveillance requirement' of a new shutdown margin monitor.

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Attachment 1 B13678/Page 3 December 4, 1990

7. Section 3.4.1.4.2. Cold Shutdown--Looos Not Filled Section 3.9.1.1. Refuelina Operations--Boron Concentration A revision to Section 3.9.1.1 was submitted in Reference (1).

Additional changes are necessary as a result of the boron dilution analysis.

The limiting condition for operation has been revised that will require certain valves in the chemical and volume control system (CVCS) to be secured to preclude a boron dilution event. A list of the valves is included in this specification that requires verification at least once per 31 days that these valves are closed and locked or under administrative controls.

8. Section 3.4.1.6. Isolated looo Startuo A revision to Section 3.4.1.6 was submitted in Reference (1).

Additional changes are necessary as a result of the boron dilution analysis. Specification 3.4.1.6.d and Surveillance 4.4.1.6.2 have been revised to make this specification consistent with Specification 3.1.1.1.2 and 3.1.1.2 and 3.9.1.1.

9. Bases Sections 3/4.1.1.1 and 3/4.1.1.2. Shutdown Marain Bases Section 3/4.1.2. Boration Systems Bases Section 3/4.4.1. Reactor Coolant loops and Coolant Circula-11011 Base Section 3/4.9.1 Boron Concentration A revision to the above sections was submitted in Reference (1).

Additional changes to these sections are being proposed to reflect the proposed Technical Specifications.

B. Other Technical Soecification Chanaes

1. Renumberir.a of Technical Specification Paaes Pages 3/4 1-1 through 3/4 1-23 are being renumbered to accom-modata the new Specification 3.1.1.1.2 and to delete the blank page; from Technical Specifications which were left by Amendment
50. As a result of the above, appropriate pages of the Technical Spucification Index were also revised. Page 3/4 1-17 (Section 3.1.2.5), and Page 3/4 1-25 (Section 3.1.3.4) were submitted in Reference (1). These two pages are being resubmitted as a result of the renumbering of pages. In addition, Page 3/4 2-26 was also submitted in Reference (1) and is being resubmitted to reflect recently approved Amendment No. 57.

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4 Attachment 1 B13678/Page 4 December 4, 1990

Reference:

(1) E. J. Mroczka letter to the U.S. Nuclear Regulatory Commission, Cycle 4, Reload Submittal, dated November 1, 1990.

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