ENS 43313: Difference between revisions

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| event date = 04/23/2007 10:24 EDT
| event date = 04/23/2007 10:24 EDT
| last update date = 04/23/2007
| last update date = 04/23/2007
| title = Automatic Reactor Trip Due To Generator Ground Relay Actuation
| title = Automatic Reactor Trip Due to Generator Ground Relay Actuation
| event text = Vogtle Unit 2 tripped from 53% power due to a turbine trip /P9 reactor trip RPS actuation during power ascension following completion of refueling outage 2R12.  Initial investigation indicates that a generator neutral ground relay actuated causing an automatic main generator turbine trip.  No visual damage is apparent on any plant equipment.
| event text = Vogtle Unit 2 tripped from 53% power due to a turbine trip /P9 reactor trip RPS actuation during power ascension following completion of refueling outage 2R12.  Initial investigation indicates that a generator neutral ground relay actuated causing an automatic main generator turbine trip.  No visual damage is apparent on any plant equipment.
All systems responded as expected.  Both motor driven auxiliary feedwater pumps and the turbine driven started on lo-lo steam generator level and AMSAC.
All systems responded as expected.  Both motor driven auxiliary feedwater pumps and the turbine driven started on lo-lo steam generator level and AMSAC.

Latest revision as of 22:16, 1 March 2018

ENS 43313 +/-
Where
Vogtle Southern Nuclear icon.png
Georgia (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.98 h-0.124 days <br />-0.0177 weeks <br />-0.00408 months <br />)
Opened: Mark Slivka
11:25 Apr 23, 2007
NRC Officer: Steve Sandin
Last Updated: Apr 23, 2007
43313 - NRC Website
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