ENS 44089: Difference between revisions

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| event date = 03/23/2008 22:16 EDT
| event date = 03/23/2008 22:16 EDT
| last update date = 03/24/2008
| last update date = 03/24/2008
| title = Manual Reactor Trip - Loss Of Speed On Mbfp
| title = Manual Reactor Trip - Loss of Speed on Mbfp
| event text = The Indian Point Unit 2 reactor was manually tripped from 94% power at 2216 on 3/23/08 due to a loss of speed on 22 main boiler feed pump (MBFP).  Indian Point Unit 2 is currently in mode 3 with all automatic actions for a manual reactor trip occurring as required.  Indian Point Unit 2 was in a coast down in advance of a scheduled refueling outage.
| event text = The Indian Point Unit 2 reactor was manually tripped from 94% power at 2216 on 3/23/08 due to a loss of speed on 22 main boiler feed pump (MBFP).  Indian Point Unit 2 is currently in mode 3 with all automatic actions for a manual reactor trip occurring as required.  Indian Point Unit 2 was in a coast down in advance of a scheduled refueling outage.
The reactor was manually tripped as required by abnormal operating procedure 2-AOP-FW-001.  All control rods inserted on the trip.  No safety or relief valves lifted due to the trip.  The motor driven aux feedwater pumps automatically started on low steam generator level and are being used to maintain steam generator level.  Condenser steam dumps are maintaining reactor temperature.  The Unit 2 electrical lineup is the normal shutdown electrical lineup.  The licensee has notified the state Public Service Commission.
The reactor was manually tripped as required by abnormal operating procedure 2-AOP-FW-001.  All control rods inserted on the trip.  No safety or relief valves lifted due to the trip.  The motor driven aux feedwater pumps automatically started on low steam generator level and are being used to maintain steam generator level.  Condenser steam dumps are maintaining reactor temperature.  The Unit 2 electrical lineup is the normal shutdown electrical lineup.  The licensee has notified the state Public Service Commission.

Latest revision as of 21:14, 1 March 2018

ENS 44089 +/-
Where
Indian Point Entergy icon.png
New York (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-0.33 h-0.0138 days <br />-0.00196 weeks <br />-4.52034e-4 months <br />)
Opened: John Dignam
01:56 Mar 24, 2008
NRC Officer: John Knoke
Last Updated: Mar 24, 2008
44089 - NRC Website
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