ENS 45931: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 05/17/2010 10:17 EDT | | event date = 05/17/2010 10:17 EDT | ||
| last update date = 05/17/2010 | | last update date = 05/17/2010 | ||
| title = Automatic Reactor Trip Due | | title = Automatic Reactor Trip Due to Low Steam Generator Water Level | ||
| event text = System Affected: RPS actuation and reactor trip. Actuation Initiation Signals: AFW auto initiation. Cause: Low level 'C' steam generator. Effect of event on Plant: Reactor and turbine trip. Actions taken or Planned: Standard post trip actions. Additional information: Plant stabilized at NOP/NOT. | | event text = System Affected: RPS actuation and reactor trip. Actuation Initiation Signals: AFW auto initiation. Cause: Low level 'C' steam generator. Effect of event on Plant: Reactor and turbine trip. Actions taken or Planned: Standard post trip actions. Additional information: Plant stabilized at NOP/NOT. | ||
The licensee experienced a feedwater transient which initiated the event. All safety systems are available. All control rods fully inserted. The electrical lineup is normal. The decay heat path is through the condenser steam dumps. There were no relief valve or safety valve lifted during the transient. Primary plant temperature is 555 degrees Fahrenheit, and primary plant pressure is 2250 psig. The licensee is investigating the cause of the feed transient. | The licensee experienced a feedwater transient which initiated the event. All safety systems are available. All control rods fully inserted. The electrical lineup is normal. The decay heat path is through the condenser steam dumps. There were no relief valve or safety valve lifted during the transient. Primary plant temperature is 555 degrees Fahrenheit, and primary plant pressure is 2250 psig. The licensee is investigating the cause of the feed transient. |
Latest revision as of 22:09, 1 March 2018
Where | |
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Millstone ![]() Connecticut (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.83 h-0.0763 days <br />-0.0109 weeks <br />-0.00251 months <br />) | |
Opened: | Bob Kastner 12:27 May 17, 2010 |
NRC Officer: | Joe O'Hara |
Last Updated: | May 17, 2010 |
45931 - NRC Website
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