ENS 45946: Difference between revisions

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| event date = 05/22/2010 16:34 CDT
| event date = 05/22/2010 16:34 CDT
| last update date = 05/22/2010
| last update date = 05/22/2010
| title = Manual Reactor Trip Due To Loss Of Steam Generator Water Level Control
| title = Manual Reactor Trip Due to Loss of Steam Generator Water Level Control
| event text = Unit 2 was operating at 100% power in the normal operating procedure, FNP-2-UOP-3.1, Power Operation, when multiple alarms were received associated with 2C Steam Generator (S/G) level, and a process cabinet failure. The control room team noticed there was no power or control capability on the 2C S/G Feedwater Regulating Control Valve (FRV), and 2C S/G level was decreasing. The control room team attempted to take manual control of the 2C FRV, which did not respond. The reactor was manually tripped when 2C S/G narrow range level reached 40%. The automatic trip set point for S/G level is 28%. All systems responded properly for the reactor trip and there were no complications.
| event text = Unit 2 was operating at 100% power in the normal operating procedure, FNP-2-UOP-3.1, Power Operation, when multiple alarms were received associated with 2C Steam Generator (S/G) level, and a process cabinet failure. The control room team noticed there was no power or control capability on the 2C S/G Feedwater Regulating Control Valve (FRV), and 2C S/G level was decreasing. The control room team attempted to take manual control of the 2C FRV, which did not respond. The reactor was manually tripped when 2C S/G narrow range level reached 40%. The automatic trip set point for S/G level is 28%. All systems responded properly for the reactor trip and there were no complications.
The investigation indicates there was an Nuclear Controller Driver (NCD) card failure in Process Control Cabinet 8. The controller card controls the 2C S/G FRV controller, which prevented any automatic, or manual control of the 2C S/G FRV, or 2C S/G level.
The investigation indicates there was an Nuclear Controller Driver (NCD) card failure in Process Control Cabinet 8. The controller card controls the 2C S/G FRV controller, which prevented any automatic, or manual control of the 2C S/G FRV, or 2C S/G level.

Latest revision as of 22:09, 1 March 2018

ENS 45946 +/-
Where
Farley Southern Nuclear icon.png
Alabama (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
LER: 05000364/LER-2010-002
Time - Person (Reporting Time:+-2.4 h-0.1 days <br />-0.0143 weeks <br />-0.00329 months <br />)
Opened: Rick Lulling
19:10 May 22, 2010
NRC Officer: John Knoke
Last Updated: May 22, 2010
45946 - NRC Website
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