ENS 45888: Difference between revisions

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| event date = 04/30/2010 16:48 CDT
| event date = 04/30/2010 16:48 CDT
| last update date = 06/29/2010
| last update date = 06/29/2010
| title = Light Socket Short Causes Isolation Systems To Actuate
| title = Light Socket Short Causes Isolation Systems to Actuate
| event text = At 1648 CDT, while the Control Bay AUO [Auxiliary Unit Operator] was attempting to change a light bulb for 1-IL-99-1AA, 1A [Reactor Protection System] RPS [Motor Generator] MG Set available light, the light socket shorted causing the loss of 1A RPS.  The loss of 1A RPS resulted in Groups 2, 3, 6, and 8 primary containment isolations and initiated Standby Gas Treatment and Control Room Emergency Ventilation.  All systems responded as designed.  The Control Room operators entered the appropriate abnormal operating instruction, 1-AOI-99-1, to restore the affected systems.  Operations entered TS LCO 3.3.1.1 conditions A.1 (place channel in Trip in 12 hours) and C.1 (restore RPS trip capability in 1 hr).  At 1734 CDT, Operations exited TS LCO 3.3.1.1 upon restoration of 1A RPS per 1-AOI-99-1.
| event text = At 1648 CDT, while the Control Bay AUO [Auxiliary Unit Operator] was attempting to change a light bulb for 1-IL-99-1AA, 1A [Reactor Protection System] RPS [Motor Generator] MG Set available light, the light socket shorted causing the loss of 1A RPS.  The loss of 1A RPS resulted in Groups 2, 3, 6, and 8 primary containment isolations and initiated Standby Gas Treatment and Control Room Emergency Ventilation.  All systems responded as designed.  The Control Room operators entered the appropriate abnormal operating instruction, 1-AOI-99-1, to restore the affected systems.  Operations entered TS LCO 3.3.1.1 conditions A.1 (place channel in Trip in 12 hours) and C.1 (restore RPS trip capability in 1 hr).  At 1734 CDT, Operations exited TS LCO 3.3.1.1 upon restoration of 1A RPS per 1-AOI-99-1.
This event is reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) 'Any event or condition that results in a valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) [b. General Containment Isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs)], except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A).
This event is reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) 'Any event or condition that results in a valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) [b. General Containment Isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs)], except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A).

Latest revision as of 22:09, 1 March 2018

ENS 45888 +/- *RETRACTED*
Where
Browns Ferry Tennessee Valley Authority icon.png
Alabama (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+0.72 h0.03 days <br />0.00429 weeks <br />9.86256e-4 months <br />)
Opened: Tim Taylor
22:31 Apr 30, 2010
NRC Officer: Pete Snyder
Last Updated: Jun 29, 2010
45888 - NRC Website
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