ENS 46801: Difference between revisions

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| event date = 04/28/2011 23:38 CDT
| event date = 04/28/2011 23:38 CDT
| last update date = 04/29/2011
| last update date = 04/29/2011
| title = Primary Containment Isolation System Actuation Due To Loss Of Power From A Diesel Generator
| title = Primary Containment Isolation System Actuation Due to Loss of Power from a Diesel Generator
| event text = At 2338 [CDT] on 04/28/2011, with Browns Ferry Nuclear Unit 1 and Unit 2 in Mode 4, Browns Ferry Nuclear Plant, performed a shutdown of the Unit 1/2 Emergency Diesel Generator 'C,' due to an oil leak coming from its governor causing voltage and frequency fluctuations. Following securing of the Unit 1/2 Diesel Generator 'C,' the 4kV Shutdown Board 'C,' which was being powered by DG 'C,' de-energized. This resulted in a loss of power to the 1B RPS, causing a Primary Containment Isolation System (PCIS) actuation and the automatic initiation of the three trains of Standby Gas and 1 train of CREV [Control Room Emergency Ventilation System]. The PCIS isolation (Group 2) also caused a loss of Shutdown Cooling on Unit 1 which was restored at 0025 [CDT] 04/29/2011 .
| event text = At 2338 [CDT] on 04/28/2011, with Browns Ferry Nuclear Unit 1 and Unit 2 in Mode 4, Browns Ferry Nuclear Plant, performed a shutdown of the Unit 1/2 Emergency Diesel Generator 'C,' due to an oil leak coming from its governor causing voltage and frequency fluctuations. Following securing of the Unit 1/2 Diesel Generator 'C,' the 4kV Shutdown Board 'C,' which was being powered by DG 'C,' de-energized. This resulted in a loss of power to the 1B RPS, causing a Primary Containment Isolation System (PCIS) actuation and the automatic initiation of the three trains of Standby Gas and 1 train of CREV [Control Room Emergency Ventilation System]. The PCIS isolation (Group 2) also caused a loss of Shutdown Cooling on Unit 1 which was restored at 0025 [CDT] 04/29/2011 .
In addition, the loss of power to the 4kV Shutdown Board 'C.' also caused the loss of 2B RHR Pump, leading to a momentary suspension of shutdown cooling to Unit 2. Shutdown cooling was immediately restored to Unit 2 using the 2D RHR Pump at 2342 [CDT].
In addition, the loss of power to the 4kV Shutdown Board 'C.' also caused the loss of 2B RHR Pump, leading to a momentary suspension of shutdown cooling to Unit 2. Shutdown cooling was immediately restored to Unit 2 using the 2D RHR Pump at 2342 [CDT].

Latest revision as of 22:07, 1 March 2018

ENS 46801 +/-
Where
Browns Ferry Tennessee Valley Authority icon.png
Alabama (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+2.8 h0.117 days <br />0.0167 weeks <br />0.00384 months <br />)
Opened: William Baker
07:26 Apr 29, 2011
NRC Officer: Dong Park
Last Updated: Apr 29, 2011
46801 - NRC Website
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