ENS 49453: Difference between revisions

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| event date = 10/19/2013 06:43 EDT
| event date = 10/19/2013 06:43 EDT
| last update date = 10/19/2013
| last update date = 10/19/2013
| title = Automatic Reactor Trip Due To Turbine Trip
| title = Automatic Reactor Trip Due to Turbine Trip
| event text = VEGP [Vogtle Electric Generating Plant] unit two was at 100% power, normal activities, when the unit two turbine tripped causing an automatic reactor trip. All control rods fully inserted and nothing unusual was noted. Auxiliary feed water and feedwater isolation actuated as expected. The unit is currently stable in Mode 3 at normal operating temperature and pressure. A forced outage response team has been formed to determine the cause of the turbine trip and determine restart criteria and time of restart.
| event text = VEGP [Vogtle Electric Generating Plant] unit two was at 100% power, normal activities, when the unit two turbine tripped causing an automatic reactor trip. All control rods fully inserted and nothing unusual was noted. Auxiliary feed water and feedwater isolation actuated as expected. The unit is currently stable in Mode 3 at normal operating temperature and pressure. A forced outage response team has been formed to determine the cause of the turbine trip and determine restart criteria and time of restart.
During the transient, no relief valves lifted. The electrical grid is stable and supplying plant safety loads. Decay heat is being removed via steam dumps to the condenser.
During the transient, no relief valves lifted. The electrical grid is stable and supplying plant safety loads. Decay heat is being removed via steam dumps to the condenser.

Latest revision as of 21:52, 1 March 2018

ENS 49453 +/-
Where
Vogtle Southern Nuclear icon.png
Georgia (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.12 h-0.0467 days <br />-0.00667 weeks <br />-0.00153 months <br />)
Opened: Dan Monahon
09:36 Oct 19, 2013
NRC Officer: Howie Crouch
Last Updated: Oct 19, 2013
49453 - NRC Website
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