ENS 52000: Difference between revisions
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| event date = 06/12/2013 20:13 EDT | | event date = 06/12/2013 20:13 EDT | ||
| last update date = 06/13/2016 | | last update date = 06/13/2016 | ||
| title = Technical Specification Required Shutdown | | title = Technical Specification Required Shutdown and Reactor Trip | ||
| event text = At 2013 EDT on 6/12/16, Millstone Unit 3 commenced a Technical Specification (TS) required shutdown due to excessive Reactor Coolant System leakage from the "A" Reactor Coolant Pump (RCP) third stage seal. The leakage from the third stage seal was approximately two gpm which is greater than the Technical Specification (TS) limit of less than one gpm. | | event text = At 2013 EDT on 6/12/16, Millstone Unit 3 commenced a Technical Specification (TS) required shutdown due to excessive Reactor Coolant System leakage from the "A" Reactor Coolant Pump (RCP) third stage seal. The leakage from the third stage seal was approximately two gpm which is greater than the Technical Specification (TS) limit of less than one gpm. | ||
During the shutdown, oscillations developed in the Main Feedwater which required the operator to initiate a manual reactor trip. Unit 3 is currently stable in Mode 3. Decay heat is being released via the Steam Dumps to the Main Condenser. Normal offsite power is available and the unit is in a normal shutdown electrical line-up. The cause of the Main Feedwater oscillations is being investigated. | During the shutdown, oscillations developed in the Main Feedwater which required the operator to initiate a manual reactor trip. Unit 3 is currently stable in Mode 3. Decay heat is being released via the Steam Dumps to the Main Condenser. Normal offsite power is available and the unit is in a normal shutdown electrical line-up. The cause of the Main Feedwater oscillations is being investigated. |
Latest revision as of 20:44, 1 March 2018
Where | |
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Millstone Connecticut (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.37 h-0.0154 days <br />-0.0022 weeks <br />-5.06826e-4 months <br />) | |
Opened: | Walter Orf 23:51 Jun 12, 2013 |
NRC Officer: | Daniel Mills |
Last Updated: | Jun 13, 2016 |
52000 - NRC Website
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