ML20065T862: Difference between revisions

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VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION               ,
VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT MONTH OCTOBER YEAR 1981 (Revised 12-03-81)
MONTHLY OPERATING REPORT MONTH   OCTOBER       YEAR 1981 (Revised 12-03-81)
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APPROVED:
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STATION MANAGER     /
STATION MANAGER
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l                                      T 8211030166 811218               '
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8211030166 811218 T
DR ADDCK 05000338 PDR
DR ADDCK 05000338 PDR


_ . _ . - . - - . . _ . _ . _ . _ . .                  . _ , . _ . _  .m             .
.m OPERATING DATA REPORT DOCKET NO.
OPERATING DATA REPORT DOCKET NO. 50-339 DATE     12-03-81 COMPLETED BY     L.L. Rogers       _
50-339 DATE 12-03-81 COMPLETED BY L.L. Rogers TELEPHONE (703) 894-5151 X2510 OPERATING STATUS i
TELEPHONE (703) 894-5151 X2510 OPERATING STATUS                                                                                 i Notes
Notes
* Reflects corrected
* Reflects corrected 1.
: 1.     Unit Name:                   North Anna 2                                     number of hours             i
Unit Name:
: 2.       Reporting Period:         October 1981 (Revised 12-03-81)                     generator on line.         l
North Anna 2 number of hours i
: 3.       Licensed Thermal Power (MWt):                           2775
2.
: 4.       Nameplate Rating (Gross MWe):                           947
Reporting Period:
: 5.       Design Electrical Rating (Net MWe):                     907
October 1981 (Revised 12-03-81) generator on line.
: 6.       Maximum Dependable Capacity (Gross NWe):               939
3.
: 7.       Maximum Dependable Capacity (Net HWe):                 890
Licensed Thermal Power (MWt):
: 8.       If Changes Occur in Capacity Ratings (Items No. 3 thru 7) Since Last Report, Give Reasons l Corrects re-evaluation of auxiliary load consumption dated May 1981.
2775 4.
l
Nameplate Rating (Gross MWe):
: 9.       Power Level To Which Restricted, If Any (Net NWe):                                 N/A                     1
947 5.
: 10. Reasons For Restrictions, If Any:                                                       N/A                     l l
Design Electrical Rating (Net MWe):
6el h                   it4 0 M r 9/ ~ 3 9 0
907 6.
This Month         Yr.-to-Date         Cumulative     ,
Maximum Dependable Capacity (Gross NWe):
: 11.       Hours In Reporting Period                                 745           7,296               7,728     i
939 7.
: 12.       Number of Hours Reactor Was Critical                       733.2         5,524.3             5,953.2   l
Maximum Dependable Capacity (Net HWe):
: 13. Reactor Reserve Shutdown Hours                         7/3, .4   17m1         1.358.5_             1,638.5
890 8.
: 14.       Hours Generator On-Line                     Ok         (*?!; 23       d5,362.M             ,*5,775 >   !
If Changes Occur in Capacity Ratings (Items No. 3 thru 7) Since Last Report, Give Reasons l Corrects re-evaluation of auxiliary load consumption dated May 1981.
: 15.       Unit Reserve Shutdown Hours                 88 4               0             0               . 0
9.
: 16.       Gross Thermal Energy Generated (MWH)             1,898,994         13,802,996         14,889,993
Power Level To Which Restricted, If Any (Net NWe):
: 17.       Gross Electrical Energy Generated (MWH)             643,948         4,653,876           5,022,307
N/A 1
: 18.       Net Electrical Energy Generated (MWH)               611,338         4,402,998           4,752,642
: 10. Reasons For Restrictions, If Any:
: 19.       Unit Service Factor                                       *95.7           *73.5                 *74.7
N/A 6el h it4 0 M r 9/ ~ 3 9 0
: 20. Unit Availability Factor                                           *95.7           *73.5                 *74.7   ;
This Month Yr.-to-Date Cumulative 11.
: 21. Unit Capacity Factor (Using MDC Net)                               92.2           67.8                 69.1   !
Hours In Reporting Period 745 7,296 7,728 12.
: 22. Unit Capacity Factor (Using DER Net)                               90.5           66.5                 67.8   '
Number of Hours Reactor Was Critical 733.2 5,524.3 5,953.2
: 23. Unit Forced Outage Rate                                             *4.3           *23.3                 *22.2
: 13. Reactor Reserve Shutdown Hours 7/3,.4 17m1 1.358.5_
1,638.5 14.
Hours Generator On-Line Ok
(*?!; 23 d5,362.M
,*5,775 >
15.
Unit Reserve Shutdown Hours 88 4 0
0 0
16.
Gross Thermal Energy Generated (MWH) 1,898,994 13,802,996 14,889,993 17.
Gross Electrical Energy Generated (MWH) 643,948 4,653,876 5,022,307 18.
Net Electrical Energy Generated (MWH) 611,338 4,402,998 4,752,642 19.
Unit Service Factor
*95.7
*73.5
*74.7 20.
Unit Availability Factor
*95.7
*73.5
*74.7 21.
Unit Capacity Factor (Using MDC Net) 92.2 67.8 69.1
: 22. Unit Capacity Factor (Using DER Net) 90.5 66.5 67.8
: 23. Unit Forced Outage Rate
*4.3
*23.3
*22.2
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
1 Refueling Outane 05-82 thru 05-14-82 l
1 Refueling Outane 05-82 thru 05-14-82 25.
: 25.         If Shut Down At End Of Report Period, Estimated Date of Startup:                         N/A
If Shut Down At End Of Report Period, Estimated Date of Startup:
N/A
: 26. Units In Test Status (Prior to Commercial Operation):
: 26. Units In Test Status (Prior to Commercial Operation):
Forecast
Forecast
                                                                                                        \. Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
\\.
* corrects duratica of shutdown 81-38' j
Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
Page 1 of 2 I
* corrects duratica of shutdown 81-38' Page 1 of 2 j
i                                                UNIT SHUTDOWNS AND POWER REDUCTIONS                                             DOCKET NO.                     50-339 UNIT NAME                       North Anna 2 DATE       12-03-81 REPORT MONTH   OCTOBER     (Revised)                             COMPLETED BY                             L. L. ROGERS TELEPHONE                 (703) 894-5151 X2510 2                                               Component              Cause & Corrective No. Date       Typel Duration Reason         Method of     Licensee     System (Hours)           Shutting     Event         Code               Code                                         Action to 3                             4           5 Down Reactor Report #                                               Prevent Recurrence 81-37 811001       F         N/A   F           5         N/A               N/A             N/A               Reduced load to 90% due to "B" Transformer hi alarm and No. 4
I i
                                                                                                                ,              governor valve cycling.
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
81-38 811003       F       *26.8 *A             3         N/A                 N/A           N/                 Reactor trip due to ENC line rupture on No.4 governor.
50-339 UNIT NAME North Anna 2 DATE 12-03-81 REPORT MONTH OCTOBER (Revised)
COMPLETED BY L. L. ROGERS TELEPHONE (703) 894-5151 X2510 l
2 No. Date Type Duration Reason Method of Licensee System Component Cause & Corrective (Hours)
Shutting Event Code Code Action to 3
4 5
Down Reactor Report #
Prevent Recurrence 81-37 811001 F
N/A F
5 N/A N/A N/A Reduced load to 90% due to "B" Transformer hi alarm and No. 4 governor valve cycling.
81-38 811003 F
*26.8
*A 3
N/A N/A N/
Reactor trip due to ENC line rupture on No.4 governor.
ld M
ld M
                  ^
,(
                          ,(                                                                                                   Closed No. 4 governor valve and Mk -
Closed No. 4 governor valve and
installed new supports l.
^
81-39 811004       F         5.0 . A           3         N/A                   N/A         N/A                 Reactor Trip due to generator leads differential.
l.
Reduced load to 91% due to "B" 81-40 811005       F         N/A     F           5         N/A                   N/A         N/A Transformer hi temperature i                                                                                                                                 alarm.
Mk -
!          81-41 811006       F         N/A     F           5         N/A                   N/A         N/A             ' Reduced load to 90% due to "B" Transformer hi temperature alarm.
installed new supports 81-39 811004 F
;                        /
5.0 A
1           1                 2                                             3                                       4 F: Forced       Reason:                                       Method:                                 Exhibit F - Instructions 8: Scheduled A-Equipment Failure (Explain)                     1-Manual                               for Preparation of Data i                           B-Maintenance or Test                         2-Maiinh1 Scram.                       Entry Sheets for Licensee C-Refueling                                   3-Automatic Scram                       Event Report (LER) File l
3 N/A N/A N/A Reactor Trip due to generator leads differential.
D-Regulatory Restriction                     4-Continuations                         (NUREG-0161)
81-40 811005 F
  ;                            E-Operator Training & License Examination 5-Load Reduction F-Administrative                             9-Other
N/A F
  '                          G-Operational Error (Explain)
5 N/A N/A N/A Reduced load to 91% due to "B" Transformer hi temperature i
H-Other (Explain)                                                                     Exhibit H - Same Source
alarm.
_ _ - - _      _ _      __            _ _ _ _ _ _ _ _ _ _ _ _ _        _}}
81-41 811006 F
N/A F
5 N/A N/A N/A
' Reduced load to 90% due to "B" Transformer hi temperature alarm.
/
1 1
2 3
4 F: Forced Reason:
Method:
Exhibit F - Instructions 8: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data i
B-Maintenance or Test 2-Maiinh1 Scram.
Entry Sheets for Licensee l
C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuations (NUREG-0161)
E-Operator Training & License Examination 5-Load Reduction F-Administrative 9-Other G-Operational Error (Explain)
H-Other (Explain)
Exhibit H - Same Source
- -}}

Latest revision as of 18:50, 16 December 2024

Corrected Monthly Operating Rept for Oct 1981
ML20065T862
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 12/03/1981
From: Rogers L
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
Shared Package
ML20065T858 List:
References
NUDOCS 8211030166
Download: ML20065T862 (3)


Text

.. _ _ _.. _ _ - -

VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT MONTH OCTOBER YEAR 1981 (Revised 12-03-81)

-f

\\

f APPROVED:

J l

l J

STATION MANAGER

/

l l

8211030166 811218 T

DR ADDCK 05000338 PDR

.m OPERATING DATA REPORT DOCKET NO.

50-339 DATE 12-03-81 COMPLETED BY L.L. Rogers TELEPHONE (703) 894-5151 X2510 OPERATING STATUS i

Notes

  • Reflects corrected 1.

Unit Name:

North Anna 2 number of hours i

2.

Reporting Period:

October 1981 (Revised 12-03-81) generator on line.

3.

Licensed Thermal Power (MWt):

2775 4.

Nameplate Rating (Gross MWe):

947 5.

Design Electrical Rating (Net MWe):

907 6.

Maximum Dependable Capacity (Gross NWe):

939 7.

Maximum Dependable Capacity (Net HWe):

890 8.

If Changes Occur in Capacity Ratings (Items No. 3 thru 7) Since Last Report, Give Reasons l Corrects re-evaluation of auxiliary load consumption dated May 1981.

9.

Power Level To Which Restricted, If Any (Net NWe):

N/A 1

10. Reasons For Restrictions, If Any:

N/A 6el h it4 0 M r 9/ ~ 3 9 0

This Month Yr.-to-Date Cumulative 11.

Hours In Reporting Period 745 7,296 7,728 12.

Number of Hours Reactor Was Critical 733.2 5,524.3 5,953.2

13. Reactor Reserve Shutdown Hours 7/3,.4 17m1 1.358.5_

1,638.5 14.

Hours Generator On-Line Ok

(*?!; 23 d5,362.M

,*5,775 >

15.

Unit Reserve Shutdown Hours 88 4 0

0 0

16.

Gross Thermal Energy Generated (MWH) 1,898,994 13,802,996 14,889,993 17.

Gross Electrical Energy Generated (MWH) 643,948 4,653,876 5,022,307 18.

Net Electrical Energy Generated (MWH) 611,338 4,402,998 4,752,642 19.

Unit Service Factor

  • 95.7
  • 73.5
  • 74.7 20.

Unit Availability Factor

  • 95.7
  • 73.5
  • 74.7 21.

Unit Capacity Factor (Using MDC Net) 92.2 67.8 69.1

22. Unit Capacity Factor (Using DER Net) 90.5 66.5 67.8
23. Unit Forced Outage Rate
  • 4.3
  • 23.3
  • 22.2
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

1 Refueling Outane 05-82 thru 05-14-82 25.

If Shut Down At End Of Report Period, Estimated Date of Startup:

N/A

26. Units In Test Status (Prior to Commercial Operation):

Forecast

\\.

Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

  • corrects duratica of shutdown 81-38' Page 1 of 2 j

I i

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-339 UNIT NAME North Anna 2 DATE 12-03-81 REPORT MONTH OCTOBER (Revised)

COMPLETED BY L. L. ROGERS TELEPHONE (703) 894-5151 X2510 l

2 No. Date Type Duration Reason Method of Licensee System Component Cause & Corrective (Hours)

Shutting Event Code Code Action to 3

4 5

Down Reactor Report #

Prevent Recurrence 81-37 811001 F

N/A F

5 N/A N/A N/A Reduced load to 90% due to "B" Transformer hi alarm and No. 4 governor valve cycling.

81-38 811003 F

  • 26.8
  • A 3

N/A N/A N/

Reactor trip due to ENC line rupture on No.4 governor.

ld M

,(

Closed No. 4 governor valve and

^

l.

Mk -

installed new supports 81-39 811004 F

5.0 A

3 N/A N/A N/A Reactor Trip due to generator leads differential.

81-40 811005 F

N/A F

5 N/A N/A N/A Reduced load to 91% due to "B" Transformer hi temperature i

alarm.

81-41 811006 F

N/A F

5 N/A N/A N/A

' Reduced load to 90% due to "B" Transformer hi temperature alarm.

/

1 1

2 3

4 F: Forced Reason:

Method:

Exhibit F - Instructions 8: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data i

B-Maintenance or Test 2-Maiinh1 Scram.

Entry Sheets for Licensee l

C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuations (NUREG-0161)

E-Operator Training & License Examination 5-Load Reduction F-Administrative 9-Other G-Operational Error (Explain)

H-Other (Explain)

Exhibit H - Same Source

- -