IR 05000086/2015011: Difference between revisions

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{{#Wiki_filter:L. Coyl L. Coyle - 2 -
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Distribution: (See next page) DOCUMENT NAME: G:\DRS\Engineering Branch 1\-- Modes\20151117b 05000286_2015011 Indian Point IP 71013.docx ADAMS ACCESSION NUMBER: ML15323A026 SUNSI Review Non-Sensitive Publicly Available OFFICE RI/DRS RI/DRP RI/DRS NAME MModes GDental MGray DATE 11/18/2015 11/09/2015 11/19/2015 OFFICIAL RECORD COPY L. Coyle - 2 - Distribution w/encl: (via e-mail) DDorman, RA DLew, DRA MScott, DRP JColaccino, DRP RLorson, DRS GSuber, DRS GDentel, DRP MDraxton, DRP (actg to 12/12/15) JSchussler, DRP BPinson, DRP BHaagensen, DRP, SRI GNewman, DRP, RI SRich, DRP, RI MModes, DRS MGray, DRS MWentzel, NRR DHochmuth, DRP, AA JJessie, RI OEDO RidsNrrPMIndianPoint Resource RidsNrrDorlLpl1-1 Resource ROPReports Resources i Enclosure U.S. NUCLEAR REGULATORY COMMISSION ii .1 2 .2 .3 .4 .5 5 The inspector reviewed 59 underground piping examinations implemented for Unit 3 and noted that corrective actions for coating degradation were implemented in 23 cases (39%). The inspector selected a number of the corrective actions and an ultrasonic test report for revie The inspector noted the ultrasonic thickness test (Report IP3-UT-15-line 408 over the discharge canal resulted in thickness readings below nominal of -IP3-2015-04410 recommended the coating be repaired to prevent further corrosio Condition Reports CR-IP3-2014-02382, -02878, and -03244 were also reviewe .6 A-1 Attachment A-2 A-3 A-4    ressurized Thermal Shock Pressurized Thermal Shock Reference Temperature
 
ML15323A026 SUNSI Review Non-Sensitive Publicly Available OFFICE RI/DRS RI/DRP RI/DRS NAME MModes GDental MGray DATE 11/18/2015 11/09/2015 11/19/2015 L. Coyle - 2 - Distribution w/encl: (via e-mail) DDorman, RA DLew, DRA MScott, DRP JColaccino, DRP RLorson, DRS GSuber, DRS GDentel, DRP MDraxton, DRP (actg to 12/12/15) JSchussler, DRP BPinson, DRP BHaagensen, DRP, SRI GNewman, DRP, RI SRich, DRP, RI MModes, DRS MGray, DRS MWentzel, NRR DHochmuth, DRP, AA JJessie, RI OEDO RidsNrrPMIndianPoint Resource RidsNrrDorlLpl1-1 Resource ROPReports Resources i Enclosure U.S. NUCLEAR REGULATORY COMMISSION ii .1 2 .2 .3 .4 .5 5 The inspector reviewed 59 underground piping examinations implemented for Unit 3 and noted that corrective actions for coating degradation were implemented in 23 cases (39%). The inspector selected a number of the corrective actions and an ultrasonic test report for revie The inspector noted the ultrasonic thickness test (Report IP3-UT-15-line 408 over the discharge canal resulted in thickness readings below nominal of -IP3-2015-04410 recommended the coating be repaired to prevent further corrosio Condition Reports CR-IP3-2014-02382, -02878, and -03244 were also reviewe .6 A-1 Attachment A-2 A-3 A-4    ressurized Thermal Shock Pressurized Thermal Shock Reference Temperature
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Revision as of 11:22, 1 June 2018

Indian Point Unit 3 Inspection Report 0500086/2015011, License Renewal Inspection
ML15335A573
Person / Time
Site: Indian Point, 05000086  Entergy icon.png
Issue date: 11/19/2015
From: Mel Gray
Engineering Region 1 Branch 1
To: Lawrence Coyle
Entergy Nuclear Operations
SECY RAS
Shared Package
ML15335A571 List:
References
50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01, RAS 28601 IR 2015011
Download: ML15335A573 (19)


Text

L. Coyl L. Coyle - 2 -

ML15323A026 SUNSI Review Non-Sensitive Publicly Available OFFICE RI/DRS RI/DRP RI/DRS NAME MModes GDental MGray DATE 11/18/2015 11/09/2015 11/19/2015 L. Coyle - 2 - Distribution w/encl: (via e-mail) DDorman, RA DLew, DRA MScott, DRP JColaccino, DRP RLorson, DRS GSuber, DRS GDentel, DRP MDraxton, DRP (actg to 12/12/15) JSchussler, DRP BPinson, DRP BHaagensen, DRP, SRI GNewman, DRP, RI SRich, DRP, RI MModes, DRS MGray, DRS MWentzel, NRR DHochmuth, DRP, AA JJessie, RI OEDO RidsNrrPMIndianPoint Resource RidsNrrDorlLpl1-1 Resource ROPReports Resources i Enclosure U.S. NUCLEAR REGULATORY COMMISSION ii .1 2 .2 .3 .4 .5 5 The inspector reviewed 59 underground piping examinations implemented for Unit 3 and noted that corrective actions for coating degradation were implemented in 23 cases (39%). The inspector selected a number of the corrective actions and an ultrasonic test report for revie The inspector noted the ultrasonic thickness test (Report IP3-UT-15-line 408 over the discharge canal resulted in thickness readings below nominal of -IP3-2015-04410 recommended the coating be repaired to prevent further corrosio Condition Reports CR-IP3-2014-02382, -02878, and -03244 were also reviewe .6 A-1 Attachment A-2 A-3 A-4 ressurized Thermal Shock Pressurized Thermal Shock Reference Temperature