ML17252A878: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
| Line 21: | Line 21: | ||
* auxiliary boiler .feed pumps. The feedwater regulating valves | * auxiliary boiler .feed pumps. The feedwater regulating valves | ||
* for these pumps were preset at 50%, thereby initating flow to all four steam generators. Shortly after the turbine trip, the Operations Engineer was at the,location of the regulating valves investigating the cause of the high levei in No. 23 steam generator which initiated the trip, when -he observed that the feedwater line ... ... | * for these pumps were preset at 50%, thereby initating flow to all four steam generators. Shortly after the turbine trip, the Operations Engineer was at the,location of the regulating valves investigating the cause of the high levei in No. 23 steam generator which initiated the trip, when -he observed that the feedwater line ... ... | ||
y .. * .**** *. *. ' ' . * ' ,', *.*.:'-.c.* *,*.*.* .* *. *.. . *" '.°" .,.,_. *.*. ' .e" . " Mr. James P. O'Reilly Atomic Energy Commission ----. '.. . .. :: '..,,: .< '. ": . | y .. * .**** *. *. ' ' . * ' ,', *.*.:'-.c.* *,*.*.* .* *. *.. . *" '.°" .,.,_. *.*. ' .e" . " Mr. James P. O'Reilly Atomic Energy Commission ----. '.. . .. :: '..,,: .< '. ": . -2-* .November* 30, 1973 Re Indian.Point Unit No. 2 Docket No. Facility Operating License No. DPR-26 .to Steam Generator No. 22 experienced a shaking accompanied by a loud noise. At 7:45 a.m., there was a reactor trip due to low-low level in No. 21 steam generator. Following the reactor trip, the primary system temperature (T yq) stabilized at about 533°F, and the steam generator pressure at about 750 psig in all generators * . Subsequent to the start.ing of the motor-driven auxiliary feed pumps, proper steam generator levels were restored in all but No. 22 steam generator. The level in No. 22 steam generator continued to decrease, indicating that sufficient flow from the auxiliary boiler feed pumps was apparently not reaching the steam generator. The Watch Foreman made several checks including verifying system lineup, auxiliary feedwater regulating valve operation, arid discharge pressure in an attempt to verify the apparent lack of flow to Steam Generator No. 22. None of these efforts was successful in restoring Steam* Generator No. 22 level. At approximately 8:30 a.m., a second shaking accompanied by a loud noise was observed in No. 22 line by operating personnel in the auxiliary feed pump bui.lding. At approximately 9:10 a.m., several indications of leakage inside containment were observed by plant operators. The level in the waste holdup tank was increasing. The discharge valves for the containment.sump pumps were shut, and the containment sump level indicators were checked. about 15 ; minutes, there were indications of a rising sump level and the sump pump valves were then put back in the normal Containment temperature was observed to be increasing* to a maximum of 110°F, | ||
* Three of the five containment recirculation fan coolers were in service at the time, and the other two fans were then placed in service and additional cooling water was supplied by opening the bypass around the temperature control valve.* The containment humidity recorder was also indicating increased humidity in containment to a wet-bulb temperature of approximately 90°F, and | * Three of the five containment recirculation fan coolers were in service at the time, and the other two fans were then placed in service and additional cooling water was supplied by opening the bypass around the temperature control valve.* The containment humidity recorder was also indicating increased humidity in containment to a wet-bulb temperature of approximately 90°F, and | ||
* the containment recirculation fan cooler units condensate *collection system weirs indicated rising levels. At about this time, the main isolation valves on No. 22 steam generator, and the manual isolation vaive upstream of No. 22 feedwater regulating valve were At approximately 9:40 a.m., the steam-driven auxiliary feed pump was started. High pump discharge pressure was indicated, and the No. 22 steam generator level did not respond. At the time this , .. . .;.*._ ,.* ... . .* .... .'* -;: | * the containment recirculation fan cooler units condensate *collection system weirs indicated rising levels. At about this time, the main isolation valves on No. 22 steam generator, and the manual isolation vaive upstream of No. 22 feedwater regulating valve were At approximately 9:40 a.m., the steam-driven auxiliary feed pump was started. High pump discharge pressure was indicated, and the No. 22 steam generator level did not respond. At the time this , .. . .;.*._ ,.* ... . .* .... .'* -;: | ||
| Line 40: | Line 40: | ||
* James P | * James P | ||
* 0 ' Re i.11 ye . At9mic Energy Commission Re ;*,*ovember. 30, 1973 Indian Point Unit No. 2 . ' AEC Docket No .. 50--24 7 Facility Operating License No. DPR-26 7. Retrieval and review of past plant operating records and _history . . 8. Survey, examination, and testing of any potentially affected electrical and instrumentation systems. 9. Suivey and of containment liner conditions. 10. Additional investigation as dictated by results of above investigations . . REPAIR WORK UNDERWAY Con Edison is proceeding expeditiously.on the repair work to damaged components, being careful, however, not to interfere* with the investigations underway. Repair work underway is as follows: 1. The failed section of feedwater piping has been removed and is being replaced with a .. new section of feedwater piping. The section to .be replaced extends from the first elbow outside 0£ containment, through the penetration, to near the first elbow inside containment (see Figure A attached to this In addition, the containment penetration end plates and expansion joint are being replaced. The undamaged containment penetration sleeve and penetration cooling coil will be retained. 2. As mentioned previously, the feedwater regulating valve in the feedwater line to Steam Generator No. 22 has been removed and sent to the vendor for inspection and maintenance as necessary. 3. All damaged or removed insulation will be replaced or repaired as necessary .* 4. All piping s*upports and other components and/or structures removed for access will be reinstalled. / *11.,-.*;: '. --. . .. . .;,: ..... ' ; . I **' "* f l \ | * 0 ' Re i.11 ye . At9mic Energy Commission Re ;*,*ovember. 30, 1973 Indian Point Unit No. 2 . ' AEC Docket No .. 50--24 7 Facility Operating License No. DPR-26 7. Retrieval and review of past plant operating records and _history . . 8. Survey, examination, and testing of any potentially affected electrical and instrumentation systems. 9. Suivey and of containment liner conditions. 10. Additional investigation as dictated by results of above investigations . . REPAIR WORK UNDERWAY Con Edison is proceeding expeditiously.on the repair work to damaged components, being careful, however, not to interfere* with the investigations underway. Repair work underway is as follows: 1. The failed section of feedwater piping has been removed and is being replaced with a .. new section of feedwater piping. The section to .be replaced extends from the first elbow outside 0£ containment, through the penetration, to near the first elbow inside containment (see Figure A attached to this In addition, the containment penetration end plates and expansion joint are being replaced. The undamaged containment penetration sleeve and penetration cooling coil will be retained. 2. As mentioned previously, the feedwater regulating valve in the feedwater line to Steam Generator No. 22 has been removed and sent to the vendor for inspection and maintenance as necessary. 3. All damaged or removed insulation will be replaced or repaired as necessary .* 4. All piping s*upports and other components and/or structures removed for access will be reinstalled. / *11.,-.*;: '. --. . .. . .;,: ..... ' ; . I **' "* f l \ | ||
... > ",'.: .' ,. e Mr. James P. O'Reilly Commission | ... > ",'.: .' ,. e Mr. James P. O'Reilly Commission -8-., * *:: .. *., .... , .. < .. :, ... :::f,vernber *30, 1973 .Re Indian Point Unit No. 2 AEC Docket No. 50-247 Facility Operating License No. DPR-26 CONCLUSION The plant is being maintained in a safe shutdown condition while necessary repairs and investigations are being conducted. Inspectors from Regulatory Operations are being kept fully informed of the progress of the investigations and repair effort, and are themselves directly observing several of the inspection efforts that Con Edison is conducting. These efforts by Con Edison personnel (with support of Westinghouse and their personn0l) are directed to assure that Indian Point Unit No. 2 is returned to service in an expeditious manner with full assurance that the health and safety of the public will be protected. Con Edison will continue to keep the Atomic.* Energy Commission informed of the progress of our efforts. | ||
* md Copy to Very truly yours . William J. Cahill, Jr. "Vice President John F. O'Leary, Director Directbrate of Licensing u. S. Atomic Energy Commission Washington, D. C. 20545 *;' .-! -. -.: . ,* *._ :: ,., ..... ., .**;, "* ... , . *. .. : -*. | * md Copy to Very truly yours . William J. Cahill, Jr. "Vice President John F. O'Leary, Director Directbrate of Licensing u. S. Atomic Energy Commission Washington, D. C. 20545 *;' .-! -. -.: . ,* *._ :: ,., ..... ., .**;, "* ... , . *. .. : -*. | ||
,.. .. .... ''. **.:. , .. . *.* :. ' . : .. ' . ; :. . .. *" .. ': OUTSIDE .CONTAINMENT ' ,, CO\.llJ, \ . GOOL\NG EXPA).J$\Ot-.l JOUJT | ,.. .. .... ''. **.:. , .. . *.* :. ' . : .. ' . ; :. . .. *" .. ': OUTSIDE .CONTAINMENT ' ,, CO\.llJ, \ . GOOL\NG EXPA).J$\Ot-.l JOUJT | ||
* PIPE *Figure* A . ! . (. * .. . * ..... . ' u. ':.-( . .. . INSIDE CONTAINMENT. ' .* >* .. : . / .. . * : ; .. , .. * 't/;. ; '*.-*' . '. '. ' .. .::. .. *******--*-.. **--**** -----* -* ... -.*. --** . :.;''' . <<f*.: . . *< ' .. _ * .. --:* :*:**:::, . :-... ; . :: . . .. :;*. *' .*-::.* . | * PIPE *Figure* A . ! . (. * .. . * ..... . ' u. ':.-( . .. . INSIDE CONTAINMENT. ' .* >* .. : . / .. . * : ; .. , .. * 't/;. ; '*.-*' . '. '. ' .. .::. .. *******--*-.. **--**** -----* -* ... -.*. --** . :.;''' . <<f*.: . . *< ' .. _ * .. --:* :*:**:::, . :-... ; . :: . . .. :;*. *' .*-::.* . | ||
}} | }} | ||
Revision as of 01:15, 2 May 2018
| ML17252A878 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 11/30/1973 |
| From: | Cahill W J Consolidated Edison Co of New York |
| To: | O'Reilly J P US Atomic Energy Commission (AEC) |
| References | |
| Download: ML17252A878 (9) | |
Text
'r . *' .* ; ** > * : .. ** ,, * .. :;.t, * .* * .,,:,, "' ;;;;. , *)f.,,, <'*.**, .*. ,,,.."; ;: Consolidated Edison Company of New York. Inc. * ,,, *** * ,_._. . : *'**.*:.'"' -.-* -* * * * .. .* : . 4 Irving Place. New York. N Y 10003 . Telephone (212) 460*3819 ::_<,. ** .**" .,,": , . *. *-, Mi. James P. O'Reilly, Director 'Directorate of Regulatory Operations . u*. S. Atomic Energy Commission *Region*l *631 Park Avenue King of Prussia, Penn. 19406
Dear Mr. O'Reilly . * *November 30,
1973 *. *Re Indian Point Unit No. 2 *Docket No. 50-247 . Facility Operating License No. DPR-26 In accordance with the discussion held on November 27, 1973 with 1-;ir. Brunner of your office, this letter.is to provide you with supplemental information concerning the* incident which occurred at Indian Point Unit No. 2 on November 13, 1973. * ... -SEQUENCE OF EVENTS AND PLANT CONDITIONS *Supplementing the sequence of *events which was provided in our letter of November 14, 1973, a detailed review of instrument strip charts computer log printout confirms the sequence presented in our letter with the additional information pre-.. sented below: . -The initial conditions prior to the incident were as follows: * *. *The reactor was critical at _approximately 7% power with reactor coolant system temperature at 547°F. The steam and feedwater system was warmed up with the main turbine at approximately 1750 rpm preparatory to synchronization of the unit to the system. The level in No. 22 steam generator was approximately 40%. At 7 :40 a.m., there wa.s a turbine trip due to. high level in No. 23 steam generator. This resulted in the shutdown of the in-service No. 21 main boiler feed pump. All generator levels started decreasing. The turbine trip resulted in the starting of the two motor-driven ***
- auxiliary boiler .feed pumps. The feedwater regulating valves
- for these pumps were preset at 50%, thereby initating flow to all four steam generators. Shortly after the turbine trip, the Operations Engineer was at the,location of the regulating valves investigating the cause of the high levei in No. 23 steam generator which initiated the trip, when -he observed that the feedwater line ... ...
y .. * .**** *. *. ' ' . * ' ,', *.*.:'-.c.* *,*.*.* .* *. *.. . *" '.°" .,.,_. *.*. ' .e" . " Mr. James P. O'Reilly Atomic Energy Commission ----. '.. . .. :: '..,,: .< '. ": . -2-* .November* 30, 1973 Re Indian.Point Unit No. 2 Docket No. Facility Operating License No. DPR-26 .to Steam Generator No. 22 experienced a shaking accompanied by a loud noise. At 7:45 a.m., there was a reactor trip due to low-low level in No. 21 steam generator. Following the reactor trip, the primary system temperature (T yq) stabilized at about 533°F, and the steam generator pressure at about 750 psig in all generators * . Subsequent to the start.ing of the motor-driven auxiliary feed pumps, proper steam generator levels were restored in all but No. 22 steam generator. The level in No. 22 steam generator continued to decrease, indicating that sufficient flow from the auxiliary boiler feed pumps was apparently not reaching the steam generator. The Watch Foreman made several checks including verifying system lineup, auxiliary feedwater regulating valve operation, arid discharge pressure in an attempt to verify the apparent lack of flow to Steam Generator No. 22. None of these efforts was successful in restoring Steam* Generator No. 22 level. At approximately 8:30 a.m., a second shaking accompanied by a loud noise was observed in No. 22 line by operating personnel in the auxiliary feed pump bui.lding. At approximately 9:10 a.m., several indications of leakage inside containment were observed by plant operators. The level in the waste holdup tank was increasing. The discharge valves for the containment.sump pumps were shut, and the containment sump level indicators were checked. about 15 ; minutes, there were indications of a rising sump level and the sump pump valves were then put back in the normal Containment temperature was observed to be increasing* to a maximum of 110°F,
- Three of the five containment recirculation fan coolers were in service at the time, and the other two fans were then placed in service and additional cooling water was supplied by opening the bypass around the temperature control valve.* The containment humidity recorder was also indicating increased humidity in containment to a wet-bulb temperature of approximately 90°F, and
- the containment recirculation fan cooler units condensate *collection system weirs indicated rising levels. At about this time, the main isolation valves on No. 22 steam generator, and the manual isolation vaive upstream of No. 22 feedwater regulating valve were At approximately 9:40 a.m., the steam-driven auxiliary feed pump was started. High pump discharge pressure was indicated, and the No. 22 steam generator level did not respond. At the time this , .. . .;.*._ ,.* ... . .* .... .'* -;:
. *. '* James P. i Re.illy e Atomic.Energy Commission .. * * *. :: : .vernber . 3 o , 19 7 3 .Re Indian Point Unit No. 2 AEC Docket No. 50-247 Facility Operating License No. DPR-26 .Pl.lrnP was placed in service, additional shaking accompanied by a loud noise was observed on the No. 22 feedwater line. The situation was analyzed as being a probable break in the feedwater line to No. steam generator inside containment, and the decision was made to cool down the primary system. At the same tirnef it was decided to make a containment entry to verify and locate the break. Cooldown commenced at approximately lO:iO a.rn, to bring the plant to the cold shutdown condition. A containment entry was made at 10:15 and .visual observation indicated a possible break in the feedwater line *in the vicinity of the containment penetration. At approximately .10:45 a.rn., while cooling down the primary system, a safety injection *signal was initiated due to high differential steam pressure between No. 22 steam generator and the other three steam generators. At *approximately 11:05 a.rn., No. 22 steam generator was completely by shutting the manual stop valves in *the auxiliary . water and chemical feed lines. This steam generator showed
- rnately 2% level by the wide range instrumentation at this time. *The reactor coolant system temperature had decreased to . . rnately 4 50 ° F. EFFECTS OF INCIDENT ON PLANT EQUIPMENT . Feedwater Piping to No. 22 Stearn Generator A visual inspection of the 18-inch diameter feedwater line *.inside containment indicated a fracture* adjacent to a fi'llet weld . between the line and the end plate which is welded into
- _the penetration sleeve in the wall. The fracture *extended approximately 180° around the pipe. The origin of the fracture was at the 3 to 4 61clock position (from inside .the coptainrnent when facing the containment wall)
- At the 3 to 4 . o'clock location, the fracture was at the toe of the fillet weld . . *The fracture appeared to have propagated up to the 12 o'clock .position, and.down to the 6 o'clock position, and its path led *away from the toe of the weld approximately 1/2 inch. Immediately above the 3 o'clock position, a short branch of the crack traveled *along the toe of the weld. The fractured portion of the pipe was off set from that portion . remaining in the penetrat.ion so that at the 12 o'clock and at the 3 o'clock positions, it was raised 1/4 of an inch. The maximum measured width of the crack was 5/32 of an inch * . ' * .. ...... ,* .. .[ ..
v . Mr, James P. O'Reill; -* * .. -*-.. ,' .. -Energy Commission * .. ;,.. . . . * :: 7:?.-:( .. 30,
- 19 73 Re Indian Point Unit No. 2 AEC Docket No. 50-247 Facility Operating License No. DPR-26 A survey of the feedwater piping to Steam Generator No. 22 inside containment included removal of insulation at Steam Generator No. 22 feedwater pipe nozzle are.a, points of restraint (hangers, snubbers, pipe whip restraints) and elbow welds. Visual and magnetic particle inspections performed at these critical.areas indicated no malities. In addition, two 5 radius sweeps of piping (about 13 .feet of pipe per sweep) were stripped of insulation and visual and magnetic particle inspections indicated no abnormalities, tion of pipe alignment was performed using surveying equipment. This survey indicated that* movement had occurred with a small permanent deformation shown by an approximate 3/4 inch clearance at the elbow restraint near the penetration (prior clearance had been nominally zero)
- Radiography was performed at the Steam Generator No. 22 feedwater nozzle to pipe weld and two elbow welds. No unacceptable indications were found by these inspections, Visual examination of the feedwater piping indicated some relative movement of insulation had occurred, but these indications were not necessarily related to this incident (some relative movement of insulation can be expected with normal heatup and cooldown expansion of feedwater piping)
- A survey of feedwater piping to Steam Generator No. 22 outside of tainment inqicated local cracking and spalling of insulation.on piping immediately outside the penetration However, visual examination of the balance, of the piping revealed no abnormalities .. Valves Inspections to date of valves have indicated no external damage, The regulating valve in the main feedwater piping to No, 22 Steam Generator was opened and inspected and no incident-related damage observed; ever, the valve has been removed from the svstem and sent to the manufacturer for more detailed inspection, and any required adjust-.ments or maintenance. *Auxiliary Boiler *Feed Lines* The auxiliary boiler feed lines and valves were inspected and no abnormalities were-found. / -i . ' '
- f ** -** ...
., ,,._ e. Mr. P. O'Reilly -s:...* .... :* * * , 30, 1973 .. ** . Aton.lie Energy Commission Electrical Equipment Re Indian Point Unit No. 2 AEC Docket No. 50-/.47 Facility Operating License No. An inspection after the incident was made to determine the condition of electrical equipment within containment. At Elevation 68 feet, a few minor traces of water were noticed, but the area otherwise appeared dry. At Elevation 46 feet, the presence of approximately 6 to 8 inches of water over the entire floor area was observed. -An inspection of the cables and electrical equipment in the area *of the electrical penetrations indicated _that the lowest cable tray running on the floor along the missile shield wall was partially submerged in water (the cable in this tray, however, is designed and tested for such conditions). The cabling in the upper trays appeared dry. The level of the cable tray immediately above the lowest tray was observed to contain moisture on the bottom of the cables, but appeared dry on top. The e+ectrical penetration area appeared intact. The lowest tray in this area was above the water level. The cabling did exhibit evidence of having been sprayed with water. There were a number of splices in this area in cabling, but no obvious water damage to the splices. An inspection of other* areas within containment indic_ated that. all valve operators, mitters and two drain tank pump motors were located well above the water level, and the equipment, including fittings, appeared dry. The electrical equipment inside appears to have suffered no adverse effects from the feedwater line leak. No electrical equipment is located in the immediate vicinity of the feedwater piping penetrations. It should be noted that all guards related equipment inside containment is designed to operate under substantially more severe containment moisture and heat conditions than those resulting from the leak in the No. 22 water line. Containment Liner Areas of the containment liner above the feedwater pipe penetrations -showed slight inward deformations. The areas where. these local deformations were observed extend from approximately Elevation 73 feet to Elevat*ion 75 feet, and cover a length of approximately 40 feet, extending clockwise on the northwest side of containment starting in the area of the feedwater line penetrations. There is no visual evidence of any reduction in containment liner integrity. In addition, the weld cha.nnel penetration and pressurization system air consumption in this area of containment following the incident was normal. : ... -; ... -.* " . ,,_ ' . : .. *, -* . . ; _.-. ._, 11_ ' ' I I '*'
.; . * * * .,, > " . . , . * ....... :e.:. :;.{ :". .. .:, : ",,.* . *" . *Mr. James P. O'Reilly * * ., ... ..,,,r:*.;,".*".,.,. .... ,.,,,.,
- Novernber .. 30, 1973 .. * .. At0mic Energy Commission-Re Indian Point Unit No. 2 AEC Docket No. Facility Operating License No. DPR-26 Steam Generator No. 22 *
- An internal inspection of the steam drum and the area above the tube sheet was made through existing inspection openings. In addition, the feedwater ring inside the steam generator was inspected internally by fiber optic means. inspections indicated no abnormalities. Representatives from the manufacturer (Westinghouse) took part in the above inspections as well as spections conducted on the support structure. The results of the support structure inspection also indicated no evidence of distress, .unusual movement or other anomalies. , Investigations Being Conducted 1. Fluid System (Water-Hammer) Analysis and Dvnarnic Stress. Analysis of piping in feedwater line to Stearn Generator *No. 22C"including feedwater ring inside the steam generator and piping supports) . These hydraulic and stress analyses include parametric study of possible modes to postulate worst-case conditions. Preliminary results from these analyses have been used to identify potential -high stress areas for special examination. i. Hydrostatic leakage tests on check valve in the feedwater piping to No. 22 steam generator. Results indicate negligible leakage past the valve seat. * *. 3. Investigations of various mechanisms to determine probable of incident . . 4. Chemical analysis of surface deposits from Stearn Generator No. 22 tube sheet area. 5. Examination of all feedwater piping penetration areas inside containment. *6 Metallurgical exarninat.ion of failed section of feedwater piping. These examinations are being performed at both the Con Edison Metallurgical Laboratory and the Research Center. These cofuplete metallurgical examinations include tensile, and hardness tests, and electron microscopy. (\ y
. , .. : Mr
- James P
- 0 ' Re i.11 ye . At9mic Energy Commission Re ;*,*ovember. 30, 1973 Indian Point Unit No. 2 . ' AEC Docket No .. 50--24 7 Facility Operating License No. DPR-26 7. Retrieval and review of past plant operating records and _history . . 8. Survey, examination, and testing of any potentially affected electrical and instrumentation systems. 9. Suivey and of containment liner conditions. 10. Additional investigation as dictated by results of above investigations . . REPAIR WORK UNDERWAY Con Edison is proceeding expeditiously.on the repair work to damaged components, being careful, however, not to interfere* with the investigations underway. Repair work underway is as follows: 1. The failed section of feedwater piping has been removed and is being replaced with a .. new section of feedwater piping. The section to .be replaced extends from the first elbow outside 0£ containment, through the penetration, to near the first elbow inside containment (see Figure A attached to this In addition, the containment penetration end plates and expansion joint are being replaced. The undamaged containment penetration sleeve and penetration cooling coil will be retained. 2. As mentioned previously, the feedwater regulating valve in the feedwater line to Steam Generator No. 22 has been removed and sent to the vendor for inspection and maintenance as necessary. 3. All damaged or removed insulation will be replaced or repaired as necessary .* 4. All piping s*upports and other components and/or structures removed for access will be reinstalled. / *11.,-.*;: '. --. . .. . .;,: ..... ' ; . I **' "* f l \
... > ",'.: .' ,. e Mr. James P. O'Reilly Commission -8-., * *:: .. *., .... , .. < .. :, ... :::f,vernber *30, 1973 .Re Indian Point Unit No. 2 AEC Docket No. 50-247 Facility Operating License No. DPR-26 CONCLUSION The plant is being maintained in a safe shutdown condition while necessary repairs and investigations are being conducted. Inspectors from Regulatory Operations are being kept fully informed of the progress of the investigations and repair effort, and are themselves directly observing several of the inspection efforts that Con Edison is conducting. These efforts by Con Edison personnel (with support of Westinghouse and their personn0l) are directed to assure that Indian Point Unit No. 2 is returned to service in an expeditious manner with full assurance that the health and safety of the public will be protected. Con Edison will continue to keep the Atomic.* Energy Commission informed of the progress of our efforts.
- md Copy to Very truly yours . William J. Cahill, Jr. "Vice President John F. O'Leary, Director Directbrate of Licensing u. S. Atomic Energy Commission Washington, D. C. 20545 *;' .-! -. -.: . ,* *._ :: ,., ..... ., .**;, "* ... , . *. .. : -*.
,.. .. .... . **.:. , .. . *.* :. ' . : .. ' . ; :. . .. *" .. ': OUTSIDE .CONTAINMENT ' ,, CO\.llJ, \ . GOOL\NG EXPA).J$\Ot-.l JOUJT
- PIPE *Figure* A . ! . (. * .. . * ..... . ' u. ':.-( . .. . INSIDE CONTAINMENT. ' .* >* .. : . / .. . * : ; .. , .. * 't/;. ; '*.-*' . '. '. ' .. .::. .. *******--*-.. **--**** -----* -* ... -.*. --** . :.; . <<f*.: . . *< ' .. _ * .. --:* :*:**:::, . :-... ; . :: . . .. :;*. *' .*-::.* .