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                                                                    APPENDIX B
.-
                                                    U.S. NUCLEAR REGULATORY C0f71ISSION
'g
                                                                      REGION IV
'.
                          NRC Inspection Report: 50-458/85-66                   License: NPF-40
: ) -.
                          Docket: 50-458
'
          '
APPENDIX B
U.S. NUCLEAR REGULATORY C0f71ISSION
REGION IV
NRC Inspection Report: 50-458/85-66
License:
NPF-40
>
Docket: 50-458
'
,
Licensee:
-Gulf States Utilites
P.-0. Box 2951
;
Beaumont, Texas 77704
'
Facility Na'me: ' diver Bend Station -
'
'
' Inspection At: River Bend Site, St. Francisville, Louisiana
Inspection Conducted: September 30-October 4,1985
, Inspector:
A
M
/
WW./R. Aenn9(t, Project Engineer, Project
Date
,
,
Section A, Reactor Projects Branch
. Approved:
o2
h
a
O
.
J.p. /auc) tin, Chief, Project Section A
Date
,
LReac' tor [ Projects Branch
>
,
. Inspection Sumary
. Inspection Conducted September 30-October 4,1985 [ Report 50-458/8566)
>
>
                ,
                          Licensee:      -Gulf States Utilites
;                                          P.-0. Box 2951
        '
                                            Beaumont, Texas 77704
        '
                          Facility Na'me: ' diver Bend Station -
  '
                        ' Inspection At: River Bend Site, St. Francisville, Louisiana
                          Inspection Conducted: September 30-October 4,1985
                          , Inspector:                      A            M                      /
                                        WW./R. Aenn9(t, Project Engineer, Project              Date
                                        ,
                                              Section A, Reactor Projects Branch
                                      ,
                          . Approved:                      o2      .      h                    a        O
                                            J.p. /auc) tin, Chief, Project Section A          Date              ,
          >
                                            LReac' tor [ Projects Branch
                                                                                          ,
                          . Inspection Sumary
            >            . Inspection Conducted September 30-October 4,1985 [ Report 50-458/8566)
x
x
                          Areas Inspected:     Routine, unan'nounced inspection of licensee identified'
Areas Inspected:
                          deficiency reports, 10 CFR 50.55(e), IE Bulletin followup,-and operating.               ..
Routine, unan'nounced inspection of licensee identified'
                          procedures. The inspection involved 37_ inspector-hours onsite by'one.NRC       >
deficiency reports, 10 CFR 50.55(e),
n                        inspector.
IE Bulletin followup,-and operating.
        ,          ,      Results: Within the three areas inspected, three. violations were identified
..
                          (failure to update procedures after issuance of'three TCNs, issuance of a TCN
procedures. The inspection involved 37_ inspector-hours onsite by'one.NRC
                        - after final approtal and failure to properly prepare TCNs, paragraph 5).
>
                                                                                                        ,
inspector.
                                      -
n
                      0511250h53 851114                                                                       -
Results: Within the three areas inspected, three. violations were identified
                      PDR       ADOCK 05000458
,
                      O                     PDR
,
                                  -,.
(failure to update procedures after issuance of'three TCNs, issuance of a TCN
- after final approtal and failure to properly prepare TCNs, paragraph 5).
,
-
0511250h53 851114
-
PDR
ADOCK 05000458
O
PDR
-,.


  .
.
                                                  2
2
                                              DETAILS
DETAILS
        1.   Personnel Contacted
1.
          *T. L. Crouse, Manager - Quality Assurance (QA)
Personnel Contacted
                    .
*T. L. Crouse, Manager - Quality Assurance (QA)
          *J. C. Deddens, Vice President
.
          *A.,O. Fredieu, Assistant Operations Supervisor
*J. C. Deddens, Vice President
          *D. R. Gipson, Assistant Plant Manager
*A.,O. Fredieu, Assistant Operations Supervisor
          *P. D. Graham, Assistant Plant Manager
*D. R. Gipson, Assistant Plant Manager
          *B. E. Hey, . Engineer-Licensing
*P. D. Graham, Assistant Plant Manager
            G. R. Kimmell, Supervisor, Operations QA
*B. E. Hey, . Engineer-Licensing
          *G.   V. King, Plant Services Supervisor
G. R. Kimmell, Supervisor, Operations QA
          *
*G. V. King, Plant Services Supervisor
            J. Miller, Senior Nuclear Engineer, Nuclear Plant Engineering (NUPE)
J. Miller, Senior Nuclear Engineer, Nuclear Plant Engineering (NUPE)
            J. E. Spivey, Operations QA Engineer
*J. E. Spivey, Operations QA Engineer
          *R.   B. Stafford, Director Quality Services
*R. B. Stafford, Director Quality Services
          *P. F. Tomlinson, Director Operations QA
*P. F. Tomlinson, Director Operations QA
            W. Trudell, Senior Reactor Operator
W. Trudell, Senior Reactor Operator
          *J. A. Wright, NUPE Supervisor
*J. A. Wright, NUPE Supervisor
            The~NRC inspector also contacted other site personnel including
The~NRC inspector also contacted other site personnel including
            administrative, clerical, operations, and testing personnel.
administrative, clerical, operations, and testing personnel.
          * Denotes those attending the exit interview conducted on October 4, 1985.
* Denotes those attending the exit interview conducted on October 4, 1985.
        2.   Licensee Action on Previous Inspection Findings
2.
            a.     (Closed) Violation (458/8542-01).   Control of Temporary Alterations.
Licensee Action on Previous Inspection Findings
                  Corrective action included deleting the option of not hanging
a.
                  temporary alteration tags if they were required for less than one
(Closed) Violation (458/8542-01).
                  work shift.   The NRC inspector reviewed the temporary alterations log
Control of Temporary Alterations.
'                  and determined that the procedure for temporary alterations is being
Corrective action included deleting the option of not hanging
                  implemented properly.
temporary alteration tags if they were required for less than one
                -This item is considered closed,
work shift.
            b.     (Closed) Open Item (458/8542-02) Implementation of a Spare-Lead
The NRC inspector reviewed the temporary alterations log
                  Identification System.
and determined that the procedure for temporary alterations is being
                  All spare leads in panels in the main control' room have been wrapped
'
                  and tied back. Maintenance work requests have been initiated to wrap
implemented properly.
                  and tie back spare leads in the rest of the plant.
-This item is considered closed,
                  This item is considered closed.
b.
            c.     (Closed) Open Item (458/8432-03) Filling ana Venting Procedures
(Closed) Open Item (458/8542-02) Implementation of a Spare-Lead
                  The NRC inspector reviewed a sample of the syctem operating
Identification System.
                  procedures and determined that instructions fm filling and venting
All spare leads in panels in the main control' room have been wrapped
b   ___
and tied back. Maintenance work requests have been initiated to wrap
and tie back spare leads in the rest of the plant.
This item is considered closed.
c.
(Closed) Open Item (458/8432-03) Filling ana Venting Procedures
The NRC inspector reviewed a sample of the syctem operating
procedures and determined that instructions fm filling and venting
b
___


                                                                  ,
,
                                                                    !
!
        .
<
          <                                        .
.
      ,
,
                                                      3-     ,
.
                                                                                -
3-
                                                                                              '
,
    {
-
                                                                '
{
                                                                              ~
'
                      of systems related to safety.have been incorporated into,the system
'
                      operating procedures.
~
                      This item is considered closed.
of systems related to safety.have been incorporated into,the system
                Licensee Identified Deficiency Reports (DRs), 10 CFR 50.55(e)
operating procedures.
                                              ~
This item is considered closed.
            3 .'
3 .'
                                                                                              >
Licensee Identified Deficiency Reports (DRs), 10 CFR 50.55(e)
                The purpose of this portion of the inspection was to determine the
~
                adequacy of corrective actions taken by the licensee on construction
>
                deficiencies identified to the NRC pursuant to the requirements of
The purpose of this portion of the inspection was to determine the
                10 CFR'50.55(e).
adequacy of corrective actions taken by the licensee on construction
                The NRC inspector reviewed the following " Reportable" DR and it is
deficiencies identified to the NRC pursuant to the requirements of
                considered closed:
10 CFR'50.55(e).
                      DR         SHORT TITLE               INITIAL       GSU FINAL
The NRC inspector reviewed the following " Reportable" DR and it is
                    NUMBER       OR SUBJECT             NOTIFICATION   REPORT LETTER
considered closed:
                    280     Loss of Torque of           07/23/85       RBG 21683-07/24/85
DR
                              Reliance Rotors in
SHORT TITLE
                              Motor-0perated Valves
INITIAL
                              (MOVs)
GSU FINAL
                The NRC inspector determined that the deficiency was properly determined
NUMBER
                to be reportable and that all required reports were made within the
OR SUBJECT
                appropriate time and contained all required information. The licensee
NOTIFICATION
                performed an evaluation of the deficiency. Corrective action consisted of
REPORT LETTER
                making changes to emergency operating procedures relative to these MOVs.
280
                These changes are specified in the operating license for River Bend as
Loss of Torque of
                License Condition 2.b of Attachment 1. The NRC inspector reviewed the
07/23/85
                changes to the emergency operating procedures and License Condition 2.b is
RBG 21683-07/24/85
                considered to be completed satisfactorily.
Reliance Rotors in
                No violations or deviations were identified in this portion of the
Motor-0perated Valves
                inspection.
(MOVs)
            4.   IE Bulletin Followup
The NRC inspector determined that the deficiency was properly determined
                The purpose of this portion of the inspection was to determine the status
to be reportable and that all required reports were made within the
                of IE Bulletins.
appropriate time and contained all required information.
                a.   IE Bulletin 82-03 and Revision 1 - Stress Corrosion Cracking in
The licensee
                      Thick-Wall, Large Diameter, St.'.inless Steel, Recirculation System
performed an evaluation of the deficiency.
                      Piping at BWR Plants.
Corrective action consisted of
                      Item - A plant reported. visually detectable leakage during
making changes to emergency operating procedures relative to these MOVs.
''
These changes are specified in the operating license for River Bend as
                      hydrostatic testing of recirculation system piping.     Visual
License Condition 2.b of Attachment 1.
                      examination revealed pin-hole leaks and cracks in piping which had
The NRC inspector reviewed the
                      been successfully ultrasonically tested 9 months previously. A
changes to the emergency operating procedures and License Condition 2.b is
                      modified ultrasonic test verified these defects and revealed
considered to be completed satisfactorily.
                      additional defects in that piping.
No violations or deviations were identified in this portion of the
inspection.
4.
IE Bulletin Followup
The purpose of this portion of the inspection was to determine the status
of IE Bulletins.
a.
IE Bulletin 82-03 and Revision 1 - Stress Corrosion Cracking in
Thick-Wall, Large Diameter, St.'.inless Steel, Recirculation System
Piping at BWR Plants.
Item - A plant reported. visually detectable leakage during
hydrostatic testing of recirculation system piping.
Visual
''
examination revealed pin-hole leaks and cracks in piping which had
been successfully ultrasonically tested 9 months previously.
A
modified ultrasonic test verified these defects and revealed
additional defects in that piping.
L.,.
L.,.


  , , .
, , .
      , ..n
..n
  '
,
                                                    4
'
4
h
h
r-
r-
"
t"
                    Findings - The licensee identified that the only coolant pressure
Findings - The licensee identified that the only coolant pressure
                    boundary piping which does not conform to NUREG 0313 Revision 1 is
boundary piping which does not conform to NUREG 0313 Revision 1 is
                    small diameter instrument piping. Analysis shows that the
small diameter instrument piping. Analysis shows that the
                    nonconforming piping will not be exposed to temperatures above 200*F,
nonconforming piping will not be exposed to temperatures above 200*F,
                    which is the threshold for intergranular stress corrosion cracking as
which is the threshold for intergranular stress corrosion cracking as
                    stated in Reg. Guide 1.44, for more than 1% of expected plant life.
stated in Reg. Guide 1.44, for more than 1% of expected plant life.
                    This bulletin is considered closed.
This bulletin is considered closed.
            5. Operating Procedures
5.
              The objective of this portion of the inspection was to confirm that the
Operating Procedures
              plant operating procedures are prepared to control safety-related
The objective of this portion of the inspection was to confirm that the
              operations within the applicable regulatory requirements.
plant operating procedures are prepared to control safety-related
              The NRC inspector sampled system operating procedures specifically to
operations within the applicable regulatory requirements.
              determine if filling and venting instructions were incorporated in the
The NRC inspector sampled system operating procedures specifically to
              procedures. River Bend Procedure ADM-0003 requires that a procedure
determine if filling and venting instructions were incorporated in the
              revision be initiated when three TCNs are outstanding against a procedure.
procedures. River Bend Procedure ADM-0003 requires that a procedure
              Eight of the system operating procedures reviewed (50Ps-2, -16, -18, -41,
revision be initiated when three TCNs are outstanding against a procedure.
              -42, -48, -53, and -90) had more than 3 TCNs, which required a permanent
Eight of the system operating procedures reviewed (50Ps-2, -16, -18, -41,
              procedure change, outstanding. S0P-90, " Reactor Water Cleanup System,"
-42, -48, -53, and -90) had more than 3 TCNs, which required a permanent
              Revision 1, dated May'13, 1985, had 12 outstanding TCNS. Six of the eight
procedure change, outstanding. S0P-90, " Reactor Water Cleanup System,"
              S0Ps, were in various stages of procedure revision, however, the revision
Revision 1, dated May'13, 1985, had 12 outstanding TCNS. Six of the eight
              to S0P-90 only. incorporated 6 of the 12 outstanding TCNs. This is an
S0Ps, were in various stages of procedure revision, however, the revision
              apparent violation (458/8566-01). The NRC inspector found several
to S0P-90 only. incorporated 6 of the 12 outstanding TCNs. This is an
              instances (50Ps-35, -42, -48,- and -49) wherein TCNs were issued which did
apparent violation (458/8566-01). The NRC inspector found several
t             not incorporate previously approved TCNs to the same pages. This resulted
instances (50Ps-35, -42, -48,- and -49) wherein TCNs were issued which did
t
not incorporate previously approved TCNs to the same pages. This resulted
'
in two different approved changes to the same page. This is an apparent
.
.
'
violation (458/8566-02). The NRC inspector found one instance
              in two different approved changes to the same page. This is an apparent
(TCN 85-1550 to S0P-0035) where two pages of a TCH were removed and the
              violation (458/8566-02). The NRC inspector found one instance
numbers of thez remaining pa'ges changed after the TCN was approved. This
              (TCN 85-1550 to S0P-0035) where two pages of a TCH were removed and the
change was apparently accomplished without the knowledge of the originator
              numbers of thez remaining pa'ges changed after the TCN was approved. This
or any of the approving personnel. 'This is also an apparent violation
              change was apparently accomplished without the knowledge of the originator
(458/8566-03).
              or any of the approving personnel. 'This is also an apparent violation
.
                                                      .
No other violations or deviations were identified in this portion of the
              (458/8566-03).
inspection.
              No other violations or deviations were identified in this portion of the
6.
              inspection.
Exit Interview
              Exit Interview
~
                                                                          ~
            6.
!
!
              An exit interview was held on October 4, 1985, with the personnel denoted
An exit interview was held on October 4, 1985, with the personnel denoted
              in paragraph 1 of this report. The NRC senior resident inspector also
in paragraph 1 of this report. The NRC senior resident inspector also
              attended this meeting. At this meeting, the scope of the inspection and
attended this meeting. At this meeting, the scope of the inspection and
              the findings were summarized.
the findings were summarized.
,
,
}}
}}

Latest revision as of 02:30, 25 May 2025

Insp Rept 50-458/85-66 on 850930-1004.Violations Noted: Failure to Update Procedures After Issuance of Temporary Change Notices & Issuance of Temporary Change Notice After Final Approval
ML20137A279
Person / Time
Site: River Bend Entergy icon.png
Issue date: 11/13/1985
From: Bennett W, Jaudon J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20137A234 List:
References
50-458-85-66, IEB-82-03, IEB-82-3, NUDOCS 8511250453
Download: ML20137A279 (4)


See also: IR 05000458/1985066

Text

,

_

_

%-

.

.

.-

'g

'.

) -.

'

APPENDIX B

U.S. NUCLEAR REGULATORY C0f71ISSION

REGION IV

NRC Inspection Report: 50-458/85-66

License:

NPF-40

>

Docket: 50-458

'

,

Licensee:

-Gulf States Utilites

P.-0. Box 2951

Beaumont, Texas 77704

'

Facility Na'me: ' diver Bend Station -

'

'

' Inspection At: River Bend Site, St. Francisville, Louisiana

Inspection Conducted: September 30-October 4,1985

, Inspector:

A

M

/

WW./R. Aenn9(t, Project Engineer, Project

Date

,

,

Section A, Reactor Projects Branch

. Approved:

o2

h

a

O

.

J.p. /auc) tin, Chief, Project Section A

Date

,

LReac' tor [ Projects Branch

>

,

. Inspection Sumary

. Inspection Conducted September 30-October 4,1985 [ Report 50-458/8566)

>

x

Areas Inspected:

Routine, unan'nounced inspection of licensee identified'

deficiency reports, 10 CFR 50.55(e),

IE Bulletin followup,-and operating.

..

procedures. The inspection involved 37_ inspector-hours onsite by'one.NRC

>

inspector.

n

Results: Within the three areas inspected, three. violations were identified

,

,

(failure to update procedures after issuance of'three TCNs, issuance of a TCN

- after final approtal and failure to properly prepare TCNs, paragraph 5).

,

-

0511250h53 851114

-

PDR

ADOCK 05000458

O

PDR

-,.

.

2

DETAILS

1.

Personnel Contacted

  • T. L. Crouse, Manager - Quality Assurance (QA)

.

  • J. C. Deddens, Vice President
  • A.,O. Fredieu, Assistant Operations Supervisor
  • D. R. Gipson, Assistant Plant Manager
  • P. D. Graham, Assistant Plant Manager
  • B. E. Hey, . Engineer-Licensing

G. R. Kimmell, Supervisor, Operations QA

  • G. V. King, Plant Services Supervisor

J. Miller, Senior Nuclear Engineer, Nuclear Plant Engineering (NUPE)

  • J. E. Spivey, Operations QA Engineer
  • R. B. Stafford, Director Quality Services
  • P. F. Tomlinson, Director Operations QA

W. Trudell, Senior Reactor Operator

  • J. A. Wright, NUPE Supervisor

The~NRC inspector also contacted other site personnel including

administrative, clerical, operations, and testing personnel.

  • Denotes those attending the exit interview conducted on October 4, 1985.

2.

Licensee Action on Previous Inspection Findings

a.

(Closed) Violation (458/8542-01).

Control of Temporary Alterations.

Corrective action included deleting the option of not hanging

temporary alteration tags if they were required for less than one

work shift.

The NRC inspector reviewed the temporary alterations log

and determined that the procedure for temporary alterations is being

'

implemented properly.

-This item is considered closed,

b.

(Closed) Open Item (458/8542-02) Implementation of a Spare-Lead

Identification System.

All spare leads in panels in the main control' room have been wrapped

and tied back. Maintenance work requests have been initiated to wrap

and tie back spare leads in the rest of the plant.

This item is considered closed.

c.

(Closed) Open Item (458/8432-03) Filling ana Venting Procedures

The NRC inspector reviewed a sample of the syctem operating

procedures and determined that instructions fm filling and venting

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of systems related to safety.have been incorporated into,the system

operating procedures.

This item is considered closed.

3 .'

Licensee Identified Deficiency Reports (DRs), 10 CFR 50.55(e)

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The purpose of this portion of the inspection was to determine the

adequacy of corrective actions taken by the licensee on construction

deficiencies identified to the NRC pursuant to the requirements of

10 CFR'50.55(e).

The NRC inspector reviewed the following " Reportable" DR and it is

considered closed:

DR

SHORT TITLE

INITIAL

GSU FINAL

NUMBER

OR SUBJECT

NOTIFICATION

REPORT LETTER

280

Loss of Torque of

07/23/85

RBG 21683-07/24/85

Reliance Rotors in

Motor-0perated Valves

(MOVs)

The NRC inspector determined that the deficiency was properly determined

to be reportable and that all required reports were made within the

appropriate time and contained all required information.

The licensee

performed an evaluation of the deficiency.

Corrective action consisted of

making changes to emergency operating procedures relative to these MOVs.

These changes are specified in the operating license for River Bend as

License Condition 2.b of Attachment 1.

The NRC inspector reviewed the

changes to the emergency operating procedures and License Condition 2.b is

considered to be completed satisfactorily.

No violations or deviations were identified in this portion of the

inspection.

4.

IE Bulletin Followup

The purpose of this portion of the inspection was to determine the status

of IE Bulletins.

a.

IE Bulletin 82-03 and Revision 1 - Stress Corrosion Cracking in

Thick-Wall, Large Diameter, St.'.inless Steel, Recirculation System

Piping at BWR Plants.

Item - A plant reported. visually detectable leakage during

hydrostatic testing of recirculation system piping.

Visual

examination revealed pin-hole leaks and cracks in piping which had

been successfully ultrasonically tested 9 months previously.

A

modified ultrasonic test verified these defects and revealed

additional defects in that piping.

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Findings - The licensee identified that the only coolant pressure

boundary piping which does not conform to NUREG 0313 Revision 1 is

small diameter instrument piping. Analysis shows that the

nonconforming piping will not be exposed to temperatures above 200*F,

which is the threshold for intergranular stress corrosion cracking as

stated in Reg. Guide 1.44, for more than 1% of expected plant life.

This bulletin is considered closed.

5.

Operating Procedures

The objective of this portion of the inspection was to confirm that the

plant operating procedures are prepared to control safety-related

operations within the applicable regulatory requirements.

The NRC inspector sampled system operating procedures specifically to

determine if filling and venting instructions were incorporated in the

procedures. River Bend Procedure ADM-0003 requires that a procedure

revision be initiated when three TCNs are outstanding against a procedure.

Eight of the system operating procedures reviewed (50Ps-2, -16, -18, -41,

-42, -48, -53, and -90) had more than 3 TCNs, which required a permanent

procedure change, outstanding. S0P-90, " Reactor Water Cleanup System,"

Revision 1, dated May'13, 1985, had 12 outstanding TCNS. Six of the eight

S0Ps, were in various stages of procedure revision, however, the revision

to S0P-90 only. incorporated 6 of the 12 outstanding TCNs. This is an

apparent violation (458/8566-01). The NRC inspector found several

instances (50Ps-35, -42, -48,- and -49) wherein TCNs were issued which did

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not incorporate previously approved TCNs to the same pages. This resulted

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in two different approved changes to the same page. This is an apparent

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violation (458/8566-02). The NRC inspector found one instance

(TCN 85-1550 to S0P-0035) where two pages of a TCH were removed and the

numbers of thez remaining pa'ges changed after the TCN was approved. This

change was apparently accomplished without the knowledge of the originator

or any of the approving personnel. 'This is also an apparent violation

(458/8566-03).

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No other violations or deviations were identified in this portion of the

inspection.

6.

Exit Interview

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An exit interview was held on October 4, 1985, with the personnel denoted

in paragraph 1 of this report. The NRC senior resident inspector also

attended this meeting. At this meeting, the scope of the inspection and

the findings were summarized.

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