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{{#Wiki_filter:_ _ _ _ _ _ _ - _ - - _ ____-_ __ . _ _ _
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                                                                                                                            ,
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                                              O
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                                                                        U.S. NL' CLEAR REGULATORY C0m11SSION
U.S. NL' CLEAR REGULATORY C0m11SSION
                                                                                                                                  :
REGION III
                                                                                      REGION III                                 l
Report No. 50-341/85040(DRP)
                                                                                                                                  l
Docket No. 50-341
                                                Report No. 50-341/85040(DRP)
License No. NPF-43
                                                Docket No. 50-341                                         License No. NPF-43
.
Licensee: Detroit Edison Company
2000 Second Avenue
Detroit, MI 48226
i
facility Name: Femi 2
Inspection At: Femi Site, Newport, MI
Inspection Conducted: July 1 through October 15, 1985
'
Management Meetings At: Glen Ellyn, Illinois on July 23
i
and September 10, 1985
Inspectors:
P. M. Byron
]
M. E. Parker
D. C. Jones
'
!
i
)G. C. Wright, Chief
/lf/'/ff[
dG LO
Approved By:
Projects Section 2C;
Date
.
.
                                                Licensee: Detroit Edison Company                                                  ;
Inspection Summary
                                                            2000 Second Avenue                                                    !
Inspection on July 1 through October 15, 1985, and Management Meetings on
                                                            Detroit, MI 48226                                                    i
July 23 and September 10, 1985 (Report No. 50-341/85040(DRP))
                                                facility Name: Femi 2
Areas Inspected: Special, unannounced inspection by resident inspectors of
                                                Inspection At: Femi Site, Newport, MI
activities surrounding the out-of-sequence rod pull, the control room HVAC,
                                                Inspection Conducted: July 1 through October 15, 1985                             i
the RCIC/ core spray room cooler, the cooling tower bypass valve, the hydrogen
'
recombiner and the breach of primary containment integrity. The inspection
                                                Management Meetings At: Glen Ellyn, Illinois on July 23
,
i                                                                          and September 10, 1985
involved a total of 246 inspector-hours onsite by three inspectors including
                                                Inspectors:   P. M. Byron
]                                                              M. E. Parker
'
'
                                                              D. C. Jones                                                        i
77 hours onsite during off-shifts. The Management Meetings involved a total of
!                                                                                                                                I
153 hours by 26 NRC personnel.
i                                                                dG LO
Results: Twenty-sixviblations(includingexamples)wereidentified(seven-
                                                Approved By:  )G.  C. Wright, Chief
,
                                                                Projects Section 2C;
Limiting Condition for Operations and nineteen - Procedural).
                                                                                                                      /lf/'/ff[
j
                                                                                                                    Date        !
j
                                                                                                                                .
p"um mgb
                                                                                                                                  l
-
                                                Inspection Summary
- -
                                                                                                                                  I
-
                                                Inspection on July 1 through October 15, 1985, and Management Meetings on        i
                                                July 23 and September 10, 1985 (Report No. 50-341/85040(DRP))                    !
                                                Areas Inspected: Special, unannounced inspection by resident inspectors of
                                                activities surrounding the out-of-sequence rod pull, the control room HVAC,
                                                the RCIC/ core spray room cooler, the cooling tower bypass valve, the hydrogen    :
                                                recombiner and the breach of primary containment integrity. The inspection        ,
                                                involved a total of 246 inspector-hours onsite by three inspectors including      '
                                                77 hours onsite during off-shifts. The Management Meetings involved a total of
                                                153 hours by 26 NRC personnel.
                                                Results: Twenty-sixviblations(includingexamples)wereidentified(seven-             ,
                                                Limiting Condition for Operations and nineteen - Procedural).                     j
j                                                     p"um mgb                                                             -


                                                                          __ ____- _____ - _ _ _ _ ___ ____ -__ _ _
__ ____- _____ - _ _ _
f                   .,
_ ___ ____ -__ _ _
          '
f
                                                                                                                    l
.,
    .
'
                                                                                                                    l
.
                                                                                                                    1
1
i                                                 DETAILS
DETAILS
i
l
l
l
            1. Attendees
1.
Attendees
a.
Persons Attending Management Meeting on July 23, 1985
l
l
                a.    Persons Attending Management Meeting on July 23, 1985
~
l                                                                                                                  ~
                                                                                                                    1
'
'
                        Deco
Deco
                        C. M. Heidel President
C. M. Heidel President
                        W. H. Jens. Vice-President, Nuclear Operations
W. H. Jens. Vice-President, Nuclear Operations
                        R. S. Lenart, Assistant Manager, Nuclear Production
R. S. Lenart, Assistant Manager, Nuclear Production
                        A. Wegele, Compliance Engineer
A. Wegele, Compliance Engineer
                        D. A. Aniol. Nuclear Shift Supervisor
D. A. Aniol. Nuclear Shift Supervisor
                        G. R. Overbeck, Superintendent, Operations
G. R. Overbeck, Superintendent, Operations
                        P. A. Marquardt, General Attorney
P. A. Marquardt, General Attorney
                        L. C. Lessor, Advisor, Management Analysis Co.
L. C. Lessor, Advisor, Management Analysis Co.
                        Public
Public
!
!
  '
B. Campball, Reporter, Detroit Free Press
                        B. Campball, Reporter, Detroit Free Press
'
                        NRC HQ's
NRC HQ's
                        E. Jordon, Director, Division of EP
E. Jordon, Director, Division of EP
                        B. J. Youngblood, NRR Licensing Chief, Branch No. 1
B. J. Youngblood, NRR Licensing Chief, Branch No. 1
                        M. D. Lynch, NRR Licensing Project Manager
M. D. Lynch, NRR Licensing Project Manager
                        NRC RI!!
NRC RI!!
                        J. G. Keppler, Regional Administrator
J. G. Keppler, Regional Administrator
                        C. J. Paperiello, Director, Division of Reactor Safety
C. J. Paperiello, Director, Division of Reactor Safety
                        E. Greenman, Deputy Director, Division of Reactor Projects
E. Greenman, Deputy Director, Division of Reactor Projects
l                       N. J. Chrissotimos, Chief, Branch 2. DRP
l
                        L. A. Reyes, Chief, Operations Branch, DRS
N. J. Chrissotimos, Chief, Branch 2. DRP
'
'
l                       G. C. Wright, Chief. Section 2C, DRP
L. A. Reyes, Chief, Operations Branch, DRS
                        P. M. Byron, SRI Fermi 2
l
G. C. Wright, Chief. Section 2C, DRP
P. M. Byron, SRI Fermi 2
T. E. Lang, Operator Licensing
,
,
                        T. E. Lang, Operator Licensing
B. Stapleton, Enforcement Specialist
'
'
                        B. Stapleton, Enforcement Specialist
W. H. Schultz, Enforcement Coordinator
                        W. H. Schultz, Enforcement Coordinator
S. Stasek, Project Inspector, Femi
                        S. Stasek, Project Inspector, Femi
R. B. Landsman, Project Manager, Section 2C, DRP
                        R. B. Landsman, Project Manager, Section 2C, DRP
5. G. DuPont, Reactor Inspector
                        5. G. DuPont, Reactor Inspector
R. D. Lanksbury, Reactor Inspector
                        R. D. Lanksbury, Reactor Inspector
l
l
!
!
!
!
                                                      2
2
      ,*
,*
        ,
,


    . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                 _ _ ___ _ _ __ _ _ ____ __ - - ______   ._- __________ _
. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
  .
_ _ ___ _ _ __ _ _ ____ __ - - ______
._- __________ _
.
.
b.
Persons Attending Management Meeting on September 10, 1985
DECO
C. M. Heidel, President
W. H. Jens, Vice-President, Nuclear Operations
R. S. Lenart Assistant Manager, Nuclear Production
T. Randazzo Director, Regulatory Affairs
E. P. Griffing Assistant Manager, Regulatory Compliance
L. C. Lessor, Advisor, Management Analysis Co.
Wolverine Power Supply
C. Borr, Member, Services Coordinator
J. Gore, Consultant
Public
T. Lam, Reporter, Ann Arbor News
S. Benkelman, Reporter, The Detroit News
B. Campball, Reporter, Detroit Free Press
M. Johnston, Member, Safe Energy Coalition of Michigan
J. Puntennery, Director, Safe Energy Coalition of Michigan
F. Kuron, Monroe County Commissioner
J. Eckert. Director, Office of Civil Preparedness
NRC HQ's
H. D. Lynch, NRR Licensing Project Manager
L. P. Crocker, NRR Licensing Section Chief, Quality Branch
NRC RIII
J. G. Keppler, Regional Administrator
A. B. Davis, Deputy Regional Administrator
C. E. Norelius Director, Division of Reactor Projects
E. Greenman, Deputy Director, Division of Reactor Projects
G. C. Wright, Chief, Section 2C, DRP
P. H. Byron, SRI, Fermi 2
B. W. Stapleton, Enforcement Specialist
J. Strasma. Public Affairs Officer
R. Lickus, Chief. State of Government Affairs
J. A. Hind. Director, Division of Radiation Safety and Safeguards
W. D. Shafer Branch Chief Emergency Preparedness and Radiological
Protection
R. B. Landsman, Project Manager, Section 2C, DRP
C. H. Weil, Compliance Specialist
T. E. Long Operator Licensing
L. Dimmock, Operator Licensing
3
.
.
    b.                                     Persons Attending Management Meeting on September 10, 1985
. -
                                                      DECO
                                                      C. M. Heidel, President
                                                    W. H. Jens, Vice-President, Nuclear Operations
                                                      R. S. Lenart Assistant Manager, Nuclear Production
                                                    T. Randazzo Director, Regulatory Affairs
                                                      E. P. Griffing Assistant Manager, Regulatory Compliance
                                                    L. C. Lessor, Advisor, Management Analysis Co.
                                                    Wolverine Power Supply
                                                    C. Borr, Member, Services Coordinator
                                                    J. Gore, Consultant
                                                      Public
                                                    T. Lam, Reporter, Ann Arbor News
                                                    S. Benkelman, Reporter, The Detroit News
                                                    B. Campball, Reporter, Detroit Free Press
                                                    M. Johnston, Member, Safe Energy Coalition of Michigan
                                                    J. Puntennery, Director, Safe Energy Coalition of Michigan
                                                      F. Kuron, Monroe County Commissioner
                                                    J. Eckert. Director, Office of Civil Preparedness
                                                    NRC HQ's
                                                    H. D. Lynch, NRR Licensing Project Manager
                                                    L. P. Crocker, NRR Licensing Section Chief, Quality Branch
                                                    NRC RIII
                                                    J. G. Keppler, Regional Administrator
                                                    A. B. Davis, Deputy Regional Administrator
                                                    C. E. Norelius Director, Division of Reactor Projects
                                                    E. Greenman, Deputy Director, Division of Reactor Projects
                                                    G. C. Wright, Chief, Section 2C, DRP
                                                    P. H. Byron, SRI, Fermi 2
                                                    B. W. Stapleton, Enforcement Specialist
                                                    J. Strasma. Public Affairs Officer
                                                    R. Lickus, Chief. State of Government Affairs
                                                    J. A. Hind. Director, Division of Radiation Safety and Safeguards
                                                    W. D. Shafer Branch Chief Emergency Preparedness and Radiological
                                                                      Protection
                                                    R. B. Landsman, Project Manager, Section 2C, DRP
                                                    C. H. Weil, Compliance Specialist
                                                    T. E. Long Operator Licensing
                                                    L. Dimmock, Operator Licensing
                                                                                                                3


T
T
    .
.
  .
.
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i
      2. Out-of-Sequence Rod Pull
2.
        While withdrawing control rods to achieve criticality on July 1, 1985,
Out-of-Sequence Rod Pull
        the Nuclear Supervising Operator (NS0) pulled eleven control rods in       '
While withdrawing control rods to achieve criticality on July 1, 1985,
        Group 3 to position 48 rather than position 04 as required by the control
the Nuclear Supervising Operator (NS0) pulled eleven control rods in
        rod pull sheets.
'
Group 3 to position 48 rather than position 04 as required by the control
rod pull sheets.
l
The afternoon shift NSO had started pulling control rods around 10:21 p.m.
!
EDT on July 1, 1985, and completed pulling centrol rods through step 37
l
at 11:15 p.m. EDT.
The night shift NSO started to pull rods at step 38
one minute and eleven seconds later.
The night shift NSO had observed
l
the off going NSO for a period of time before taking the controls.
The
l
nightshift NSO utilized a Shift Technical Advisor in Training (STAIT) to
l
monitor the Source Range Monitor (SRM) instrumentation to facilitate the
l
rod pull rather than perform that function himself.
The NSO completed
pulling rods in Group 2 and then commenced pulling rods in Group 3
(step 46).
Starting with step 46 and for the next 10 steps the NSO
pulled each control rod to the full out position (48) rather than
position 04 as required by the procedure.
The NSO verified by his
initials, on the rod pull sheet, that each of the eleven control rods
was at position 04 when in fact they were at position 48.
While pulling the eleventh control rod in Group 3 (control rod 18-51),
the Short Period Alarm annunciated five times and the pen for the
Channel A SRM recorder failed to ink for about three minutes. When
l
l
        The afternoon shift NSO had started pulling control rods around 10:21 p.m.
the pen started inking again the NSO and STAIT observed that recorder
!        EDT on July 1, 1985, and completed pulling centrol rods through step 37
was reading approximately 5x103 counts per second and increasing.
l        at 11:15 p.m. EDT. The night shift NSO started to pull rods at step 38
The
        one minute and eleven seconds later. The night shift NSO had observed
;
l        the off going NSO for a period of time before taking the controls. The
Shif t Reactor Engineer (SRE) had predicted that criticality should occur
l        nightshift NSO utilized a Shift Technical Advisor in Training (STAIT) to
between steps 150 and 160, when the NSO observed the increasing count
l        monitor the Source Range Monitor (SRM) instrumentation to facilitate the
l        rod pull rather than perform that function himself.    The NSO completed
        pulling rods in Group 2 and then commenced pulling rods in Group 3
        (step 46). Starting with step 46 and for the next 10 steps the NSO
        pulled each control rod to the full out position (48) rather than
        position 04 as required by the procedure.    The NSO verified by his
        initials, on the rod pull sheet, that each of the eleven control rods
        was at position 04 when in fact they were at position 48.
        While pulling the eleventh control rod in Group 3 (control rod 18-51),
        the Short Period Alarm annunciated five times and the pen for the
        Channel A SRM recorder failed to ink for about three minutes. When
l        the pen started inking again the NSO and STAIT observed that recorder
        was reading approximately 5x103 counts per second and increasing. The
;       Shif t Reactor Engineer (SRE) had predicted that criticality should occur
'
'
        between steps 150 and 160, when the NSO observed the increasing count
l
l        rata he was only on step 56. The NSO instructed the STAIT to inform the
rata he was only on step 56.
        Nuclear Shif t Supervisor (NSS) of the situation and immediately started
The NSO instructed the STAIT to inform the
        to insert rod 18-51. It took 14 minutes and 41 seconds to insert all
Nuclear Shif t Supervisor (NSS) of the situation and immediately started
        eleven control rods to position 04. Thirty-five (35) seconds later
to insert rod 18-51.
        the NSO continued the startup by pulling rods from step 57 of
It took 14 minutes and 41 seconds to insert all
        the procedure.
eleven control rods to position 04.
        During the control rod pulls the NSS and the Nuclear Assistant Shift
Thirty-five (35) seconds later
        Supervisor (NASS) were in the NSS's office. The SRE was behind the panels
the NSO continued the startup by pulling rods from step 57 of
        and could not observe the rod pulls. The NSO in charge of the control
the procedure.
        room was at his desk facing the pan 11s and the Shift Technical Advisor
During the control rod pulls the NSS and the Nuclear Assistant Shift
        (STA) and the Shift Operations Advisor (50A) were by the NSO's desk,
Supervisor (NASS) were in the NSS's office.
        Neither the NSO in charge, the SOA, nor the STA were observing the rod
The SRE was behind the panels
        pull nor were they aware of the incident. The STAIT Informed the SRC
and could not observe the rod pulls.
        of the event who wrote in his log that the reactor may have been
The NSO in charge of the control
        critical.
room was at his desk facing the pan 11s and the Shift Technical Advisor
        The NSS reviewed the event with the NSO (at the controls) and the STAIT
(STA) and the Shift Operations Advisor (50A) were by the NSO's desk,
        and determined that the reactor had not gone critical. lhe NSS then
Neither the NSO in charge, the SOA, nor the STA were observing the rod
        directed that rod pulling recommence. The NSS apparently did not seek
pull nor were they aware of the incident.
        the advice or counsel of the SRE, the SOA, or the S1A, The SRE also ,
The STAIT Informed the SRC
        lined out in his log book the reference of the unit being critical.
of the event who wrote in his log that the reactor may have been
        Neither the NSS nor the NSO logs contained an entry regarding the
critical.
                                            4
The NSS reviewed the event with the NSO (at the controls) and the STAIT
and determined that the reactor had not gone critical.
lhe NSS then
directed that rod pulling recommence.
The NSS apparently did not seek
the advice or counsel of the SRE, the SOA, or the S1A,
The SRE also ,
lined out in his log book the reference of the unit being critical.
Neither the NSS nor the NSO logs contained an entry regarding the
4
-


    .
.
  .
.
      out-of-sequence rod pull. The NSS, however, did write a Deviation /
out-of-sequence rod pull.
      Event Report (DER) (No. NP-85-0334) describing the event and stated that
The NSS, however, did write a Deviation /
      the reactor had not gone critical.
Event Report (DER) (No. NP-85-0334) describing the event and stated that
      DER No. NP-85-0334 was reviewed by the licensee's Corrective Action
the reactor had not gone critical.
      Review Board (CARB) on July 2,1985, who concurred with the NSS's
DER No. NP-85-0334 was reviewed by the licensee's Corrective Action
      determination that the incident was not reportable under either 10 CFR
Review Board (CARB) on July 2,1985, who concurred with the NSS's
      50.72 or 50.73. It appeared that there was disagreement within the
determination that the incident was not reportable under either 10 CFR
      licensee's organization as to whether or not the reactor had been critical.
50.72 or 50.73.
      The licensee directed that additional engineering review be made. The
It appeared that there was disagreement within the
      licensee informed the Resident Inspector (RI) of the event on July 3,
licensee's organization as to whether or not the reactor had been critical.
      1985, and stated that the unit had not gone critical but that there was a
The licensee directed that additional engineering review be made.
      question among the staff and that Reactor Engineering was performing a
The
      technical review. The licensee stated that they would get back to the
licensee informed the Resident Inspector (RI) of the event on July 3,
      RI when the determination had been made. The RI informed RIII of his
1985, and stated that the unit had not gone critical but that there was a
      meeting.
question among the staff and that Reactor Engineering was performing a
      A SRE made the determination on July 4,195 that the reactor had been
technical review.
      critical on July 1, 1985, with a 114 second period and informed his
The licensee stated that they would get back to the
      management of the determination. Several licensee meetingr. were held on
RI when the determination had been made.
      July 5 and 6, 1985 to discuss this event and to initiate an investigation
The RI informed RIII of his
      into its cause.
meeting.
      The next discussion with the NRC resident staff, af ter July 3,1985,
A SRE made the determination on July 4,195 that the reactor had been
      was on July 15, 1985, when the Senior Resident Inspector (SRI)
critical on July 1, 1985, with a 114 second period and informed his
      was asked by licensee management if he was aware of the July 1, 1985
management of the determination.
      incident and that the reactor had been critical. The SRI was aware of
Several licensee meetingr. were held on
,
July 5 and 6, 1985 to discuss this event and to initiate an investigation
      the out-of-sequence rod pull but was not aware that the reactor had
into its cause.
      been critical. The SRI informed RIII of the meeting, and the new
The next discussion with the NRC resident staff, af ter July 3,1985,
      information on criticality.
was on July 15, 1985, when the Senior Resident Inspector (SRI)
      Region !!! Issued a Confirmatory Action Letter (CAL-RI!!-85-10) to the
was asked by licensee management if he was aware of the July 1, 1985
      licensee on July 16, 1985. The CAL detailed the corrective action
incident and that the reactor had been critical.
      the licensee was to take relating to the out-of-sequence rod pull. The
The SRI was aware of
      CAL is detailed in Inspection Report 50-341/85043(DRP).   The licensee
the out-of-sequence rod pull but was not aware that the reactor had
-      made a presentation in Region III on July 23, 1985, regarding their
,
      corrective action program and finu ngs related to the event which is
been critical.
      described in Paragraph 9 of this report. The licensee's presentation
The SRI informed RIII of the meeting, and the new
      is included as an attachment to their response to the CAL, Deco letter
information on criticality.
      RC-LG 85-0017 (Jens to Keppler) dated September 5, 1985.
Region !!! Issued a Confirmatory Action Letter (CAL-RI!!-85-10) to the
      During the inspection and review of the event, nine examples of apparent
licensee on July 16, 1985.
      violations of Technical Specification requirements were identified and are
The CAL detailed the corrective action
      as follows:
the licensee was to take relating to the out-of-sequence rod pull.
      Technical Specification 6.8.1.a requires that written procedures shall
The
      be estab11shed, implemented, and maintained covering the applicable
CAL is detailed in Inspection Report 50-341/85043(DRP).
      procedure recommendations of Appendix A of Regulatory Guide 1.33,
The licensee
      Revision 2, 1978. Appendix A of Regulatory Guide 1.33 lists the
made a presentation in Region III on July 23, 1985, regarding their
      following activities under Administrative procedures:
-
                                                                                  i
corrective action program and finu ngs related to the event which is
                                          5                                       :
described in Paragraph 9 of this report.
The licensee's presentation
is included as an attachment to their response to the CAL, Deco letter
RC-LG 85-0017 (Jens to Keppler) dated September 5, 1985.
During the inspection and review of the event, nine examples of apparent
violations of Technical Specification requirements were identified and are
as follows:
Technical Specification 6.8.1.a requires that written procedures shall
be estab11shed, implemented, and maintained covering the applicable
procedure recommendations of Appendix A of Regulatory Guide 1.33,
Revision 2, 1978.
Appendix A of Regulatory Guide 1.33 lists the
following activities under Administrative procedures:
i
5
:


                                                                                  _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _ _ _
      .
.
    .
.
                                                                            .
.
                -  Hot Standby to Minimum Load (Nuclear Startup)
Hot Standby to Minimum Load (Nuclear Startup)
                -   Authorities and Responsibilities for Safe Operation...
-
                -   Equipment Control
Authorities and Responsibilities for Safe Operation...
                -   Shift and Relief Turnovers
-
                -   Log Entries
Equipment Control
        Contrary to the above, the licensee failed to adhere to the provisions of
-
        Technical Specification 6.8.1.a covering the startup of the reactor on
Shift and Relief Turnovers
        July 1, 1985, as indicated below:
-
          a. P0M Procedure 51.000.08, " Control Rod Sequence and Movement
Log Entries
              Control," paragraph 3.1.1, requires that rod withdrawals in the
-
              region from 100% Rod Density to 20% Reactor Power must be
Contrary to the above, the licensee failed to adhere to the provisions of
              performed according to the rod pull sheet. The rod pull sheets
Technical Specification 6.8.1.a covering the startup of the reactor on
              in effect on July 1,1985, required the rods for Group 3 to be
July 1, 1985, as indicated below:
              pulled in notch control (00-04, 04-08, etc.). The licensee
a.
              pulle<* :leven control rods in Group 3 to the full out position
P0M Procedure 51.000.08, " Control Rod Sequence and Movement
              (48) rather than to the 04 position as required (341/85040-01a).
Control," paragraph 3.1.1, requires that rod withdrawals in the
          b. POM Procedure 51.000.08 Paragraph 3.1.4 states, in part, "Following
region from 100% Rod Density to 20% Reactor Power must be
              each rod move the Nuclear Supervising Operator (NS0) shall verify
performed according to the rod pull sheet. The rod pull sheets
              the control rod was lef t in the proper position indicated and shall
in effect on July 1,1985, required the rods for Group 3 to be
              document this verification by initialing the ' Final Position
pulled in notch control (00-04, 04-08, etc.). The licensee
-
pulle<* :leven control rods in Group 3 to the full out position
              Verified' block of Attachment 1." The NSO verified eleven rods to
(48) rather than to the 04 position as required (341/85040-01a).
              be at position 04, by initialinj the pull sheet, when in actuality
b.
              they were at position 48(341/85040-01b).
POM Procedure 51.000.08 Paragraph 3.1.4 states, in part, "Following
          c. POM Procedures 12.000.57, " Nuclear Production Organization" and
each rod move the Nuclear Supervising Operator (NS0) shall verify
              21.000.01, "Shif t Operation and Control Room" delineate the
the control rod was lef t in the proper position indicated and shall
              responsibilittee of the NSS to include supervision of all
document this verification by initialing the ' Final Position
              activities and observation and/or direction of major plant
Verified' block of Attachment 1."
              evolutions to ensure compliance with Technical Specificatiens,
The NSO verified eleven rods to
              procedures, and regulations.   The NSS did not appropriately
-
              discharge his duties on July 1 and 2,1985, in that Me neither
be at position 04, by initialinj the pull sheet, when in actuality
,
they were at position 48(341/85040-01b).
  ,
c.
              supervised, observed, nor directed the activities essociated                           ,
POM Procedures 12.000.57, " Nuclear Production Organization" and
              with the control rod pulls (a major plant evaluation) nor was
21.000.01, "Shif t Operation and Control Room" delineate the
              he in the proximity of the appropriate control panel and
responsibilittee of the NSS to include supervision of all
              associated nuclear instrumentation (341/85040-01c).
activities and observation and/or direction of major plant
          d. POM Procedur 21.000.01, Enclosure 1 Item 12, requires the Nuclear
evolutions to ensure compliance with Technical Specificatiens,
              Assistant Shif t Supervisor (NASS) to provide direct supervision of
procedures, and regulations.
              shift personnel. The NASS did not provide direct supervision of the
The NSS did not appropriately
              NSP manipulating the controls on July 1 and 2,1985 nor was he in
discharge his duties on July 1 and 2,1985, in that Me neither
              the proximity of the appropriate control panel and associated
supervised, observed, nor directed the activities essociated
,
,
,
with the control rod pulls (a major plant evaluation) nor was
he in the proximity of the appropriate control panel and
associated nuclear instrumentation (341/85040-01c).
d.
POM Procedur 21.000.01, Enclosure 1
Item 12, requires the Nuclear
Assistant Shif t Supervisor (NASS) to provide direct supervision of
shift personnel. The NASS did not provide direct supervision of the
NSP manipulating the controls on July 1 and 2,1985 nor was he in
the proximity of the appropriate control panel and associated
nuclear instrumentation (341/85040 01d).
'
'
              nuclear instrumentation (341/85040 01d).
e.
          e.  P0H Procedure 21.000.01, Enclosure 2, Item 5 requires the NSO
P0H Procedure 21.000.01, Enclosure 2, Item 5 requires the NSO
              to be responsible for the plant's main control room operation.
to be responsible for the plant's main control room operation.
              The control room NSO was unaware of the out-of-sequence rod
The control room NSO was unaware of the out-of-sequence rod
              pull and thus was not successfully discharging his duties
pull and thus was not successfully discharging his duties
              (341/85040-01e).
(341/85040-01e).
                  .
.
                                              6
6
-
-
-
-


                              _ _ _ _ _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _                   _ - _ _ _ ____
_ _ _ _ _ _ .
                                                                                                                      ,
. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _
  .
_ - _ _ _
____
,
.
.
f.
POM Procedure 21.000.01, Enclosure 6, Item 2, requires the Shift
Operations Advisor (SOA) observe actuation of annunciators to ensure
that they are being promptly and properly addressed with actions
taken. Five short period alarms were received in less than four
minutes while pulling rod 18-51 on July 1, 1985. The NSO at the
controls was allowed to continue pulling rods and the SOA did not
discharge his responsibilities by failing to become involved in the
resolution of the short period alarms (341/85040-01f).
g.
P0M Procedure 21.000.02, " Operating Logs and Records," Section
4.2.5.8, requires the NSS to record the occurrence of significant
events in the NSS log. The NSS log for July 1 and 2,1985,
contained no entries for the out-of-sequence rod pulls, a
significant event, which occurred between 11:40 and 11:59 p.m.
on July 1,1985(341/85040-01g).
h.
POM Procedure 21.000.01, " Shift Operation and Control Room," Section
6.3.8 states, " Reactor Engineering Administrative Procedure No.
51.000.10, ' Reactor Engineering Conduct of Operations,' details the
duties and responsibilities of on-shif t Reactor Engineering personnel."
Procedure 51.000.10 Section 1.0, states, "The purpose of this
procedure is to outline operational interfaces between Reactor
Engineering and Plant Operations and to clarify the overall responsi-
bilities of on-shif t Reactor Engineering personnel." Procedure 51.000.10
does not detail the duties and responsibilities of the on-shift
Reactor Engineer (341/85040-01h).
1.
POM Procedure 21.000.01, Section 6.8 addresses shift relief and
Section 6.8.4 specifically addresses the control room nuclear
supervisingoperator(NS0). The procedure defines the required
turnover for the NSO in charge of the control room but does not
define any turnuver requirements for the NSO assigned to duties in
the control room but not in charge of the control room (341/85040-011).
3.
Control Room HVAC
On July 11, 1985 PN-21 No. 286934 was issued to inspect the Division !!
Control Room HVAC condensate tray.
For personnel protection the Division !!
Control Room HVAC supply fan control switch was placed in the off position
at 8:35 a.m. on July 18, 1985 and the feeder break was opened and red
tagged at 8:50 a.m.
The Nuclear Supervising Operator (NS0) entered the
action in his log but did not list the Technical Specification appitcability.
The NSO also entered the action in the Control Room Information System
(CRIS) equipment status file and placed the applicable CRIS dot next to
the switch on the sanel. The NSO also advised the protection leader that
protection had to )e removed by 3:00 ).m. on July 25, 1985, however, the
NSO failed to notify the NSS of the c1ange in equipment status. Neither
the NSS log nor the out-of-specification log contain any entries on the
inoperable Division !! HVAC. The work was completed and the request to
7
j
.
.
.
        f.  POM Procedure 21.000.01, Enclosure 6, Item 2, requires the Shift
            Operations Advisor (SOA) observe actuation of annunciators to ensure
            that they are being promptly and properly addressed with actions
            taken. Five short period alarms were received in less than four
            minutes while pulling rod 18-51 on July 1, 1985. The NSO at the
            controls was allowed to continue pulling rods and the SOA did not
            discharge his responsibilities by failing to become involved in the
            resolution of the short period alarms (341/85040-01f).
        g.  P0M Procedure 21.000.02, " Operating Logs and Records," Section
            4.2.5.8, requires the NSS to record the occurrence of significant
            events in the NSS log. The NSS log for July 1 and 2,1985,
            contained no entries for the out-of-sequence rod pulls, a
            significant event, which occurred between 11:40 and 11:59 p.m.
            on July 1,1985(341/85040-01g).
        h.  POM Procedure 21.000.01, " Shift Operation and Control Room," Section
            6.3.8 states, " Reactor Engineering Administrative Procedure No.
            51.000.10, ' Reactor Engineering Conduct of Operations,' details the
            duties and responsibilities of on-shif t Reactor Engineering personnel."
            Procedure 51.000.10 Section 1.0, states, "The purpose of this
            procedure is to outline operational interfaces between Reactor
            Engineering and Plant Operations and to clarify the overall responsi-
            bilities of on-shif t Reactor Engineering personnel." Procedure 51.000.10
            does not detail the duties and responsibilities of the on-shift
            Reactor Engineer (341/85040-01h).
      1.    POM Procedure 21.000.01, Section 6.8 addresses shift relief and
            Section 6.8.4 specifically addresses the control room nuclear
            supervisingoperator(NS0). The procedure defines the required
            turnover for the NSO in charge of the control room but does not
            define any turnuver requirements for the NSO assigned to duties in
            the control room but not in charge of the control room (341/85040-011).
    3. Control Room HVAC
      On July 11, 1985 PN-21 No. 286934 was issued to inspect the Division !!
      Control Room HVAC condensate tray.                                                                    For personnel protection the Division !!
      Control Room HVAC supply fan control switch was placed in the off position
      at 8:35 a.m. on July 18, 1985 and the feeder break was opened and red
      tagged at 8:50 a.m. The Nuclear Supervising Operator (NS0) entered the
      action in his log but did not list the Technical Specification appitcability.
      The NSO also entered the action in the Control Room Information System
      (CRIS) equipment status file and placed the applicable CRIS dot next to
      the switch on the sanel. The NSO also advised the protection leader that
      protection had to )e removed by 3:00 ).m. on July 25, 1985, however, the
      NSO failed to notify the NSS of the c1ange in equipment status. Neither
      the NSS log nor the out-of-specification log contain any entries on the
      inoperable Division !! HVAC. The work was completed and the request to
                                                                                                            7                                          .
                                                                                                                                                        j


                                        _ _ _ _ - _ _ _ _ _
_ _ _ _ - _ _ _ _ _
  .
.
    removeprotectionwasmadeat1:20g.m.onJuly 18, 1985. However, the
removeprotectionwasmadeat1:20g.m.onJuly 18, 1985. However, the
    package was misfiled in the " active file rather thar, the " protection to
package was misfiled in the " active file rather thar, the " protection to
    be cleared" file.
be cleared" file.
    The out-of-specification condition went unnoticed for 27 shift turnovers
The out-of-specification condition went unnoticed for 27 shift turnovers
    by the oncoming NSS, NASS, and NS0's even though the switch was marked,
by the oncoming NSS, NASS, and NS0's even though the switch was marked,
    a log entry had been made, and it was entered in the CRIS equipment
a log entry had been made, and it was entered in the CRIS equipment
    status file.       It was not until July 27, 1985 that a nightshift NSS
status file.
    questioned the status of the Division II Control Room HVAC fan and
It was not until July 27, 1985 that a nightshift NSS
    had the fan returned to service at 5:38 a.m. on July 27, 1985.
questioned the status of the Division II Control Room HVAC fan and
    During the inspection and review of the event, two apparent violations
had the fan returned to service at 5:38 a.m. on July 27, 1985.
    of Technical Specification requirements were identified as follows:
During the inspection and review of the event, two apparent violations
l   a.   Technical Specification 3.7.2.C.1 requires that with the control
of Technical Specification requirements were identified as follows:
          center emergency filtration system supply fan inoperable, with the
l
          plant in cold shutdown, the fan be made operable in seven days or
a.
          initiate and maintain operation of the system in the recirculation
Technical Specification 3.7.2.C.1 requires that with the control
        mode of operation.
center emergency filtration system supply fan inoperable, with the
          Centrary to the above, the licensee failed to place the control
plant in cold shutdown, the fan be made operable in seven days or
          room emergency filtration system in the recirculation mode of
initiate and maintain operation of the system in the recirculation
mode of operation.
Centrary to the above, the licensee failed to place the control
room emergency filtration system in the recirculation mode of
l
operation on July 25, 1985; seven days after the system was
l
rendered inoperable on July 18, 1985. This condition existed
l
for aroroximately forty-five (45) hours (341/85040-02).
b.
Technicsl Specification 6.8.1.a requires that written prac#dures
shall be established, implemented, and maintained covering the
l
l
          operation on July 25, 1985; seven days after the system was
applicable procedure reconinendations of Appendix A of Regulatory
l          rendered inoperable on July 18, 1985. This condition existed
l          for aroroximately forty-five (45) hours (341/85040-02).
    b.    Technicsl Specification 6.8.1.a requires that written prac#dures
          shall be established, implemented, and maintained covering the
l        applicable procedure reconinendations of Appendix A of Regulatory
          Guide 1.33 Revision 2, 1978. Appendix A of Regulatory Guide 1.33
'
'
          lists the following activities under Administrative Procedures:
Guide 1.33 Revision 2, 1978. Appendix A of Regulatory Guide 1.33
            -  Authorities and Responsibilities for Safe Operation...
lists the following activities under Administrative Procedures:
            -   Equipnent Control
Authorities and Responsibilities for Safe Operation...
!            -   Shif t and helief Turnovers
-
            -   Log Entries...
Equipnent Control
          Contrary to the above, the licensee failed to adhere to the
-
          provisions of Technical Specification 6.8.1.a as follows:
Shif t and helief Turnovers
          (1) POM Procedure 21.000.01 "Shif t Operations and Control Room,"
!
                delineates the shift turnover responsibilities of the Nuclear
-
                Shif t Supervisor (NSS) the Nuclear Assistant Shift Supervisor
Log Entries...
                  (NAJS) and the Nuclear Station Operator (NS0). Included in the
-
                  responsibilities is a review of past log entries, and a review
Contrary to the above, the licensee failed to adhere to the
                of each Combination Operating Panel for off-normal conditions
provisions of Technical Specification 6.8.1.a as follows:
                or the addition of CRIS " dots." The NSS NASS, and NSO all
(1) POM Procedure 21.000.01 "Shif t Operations and Control Room,"
l                 failed to adequately perform the required activities as
delineates the shift turnover responsibilities of the Nuclear
                  indicatedbelow(341/85040-03a):
Shif t Supervisor (NSS) the Nuclear Assistant Shift Supervisor
                                                            8
(NAJS) and the Nuclear Station Operator (NS0).
        .
Included in the
responsibilities is a review of past log entries, and a review
of each Combination Operating Panel for off-normal conditions
or the addition of CRIS " dots." The NSS NASS, and NSO all
l
failed to adequately perform the required activities as
indicatedbelow(341/85040-03a):
8
.
-


    .
.
  .
.
                    (a) The Control Center Division II HVAC supply fan switch was
(a) The Control Center Division II HVAC supply fan switch was
                          placed in the off position on July 18, 1985, and not
placed in the off position on July 18, 1985, and not
                          observed to be out of position until July 27, 1985. The
observed to be out of position until July 27, 1985. The
                          out-of-specification switch position went unobserved for
out-of-specification switch position went unobserved for
                          27 shift turnovers.
27 shift turnovers.
                    (b) The NSO entered the switch position in the equipment
(b) The NSO entered the switch position in the equipment
                          status file and placed a CRIS " dot" by the switch on
status file and placed a CRIS " dot" by the switch on
                          July 18, 1985. The CRIS " dot" went unobserved for
July 18, 1985. The CRIS " dot" went unobserved for
                          27 shift turnovers.
27 shift turnovers.
                    (c) The NS0 had logged placing the Division II Control
(c) The NS0 had logged placing the Division II Control
                          Center HVAC supply fan in the off position at 8:35 a.m.
Center HVAC supply fan in the off position at 8:35 a.m.
                          on July 18, 1985. Subsequent reviews of the log either
on July 18, 1985. Subsequent reviews of the log either
                          failed to note the entry or failed to recognize its
failed to note the entry or failed to recognize its
                          significance. (6 NSS turnovers, 15 NASS turnovers,
significance.
                          and 27 NSO turnovers)
(6 NSS turnovers, 15 NASS turnovers,
              (2) P0H Procedure 21.000.01, Section 6.19.1.1 states, in part.
and 27 NSO turnovers)
                    " Evaluate the consequences of removing the system or component
(2) P0H Procedure 21.000.01, Section 6.19.1.1 states, in part.
                    from service considering such items as Technical Specifications
" Evaluate the consequences of removing the system or component
                    L.initing Condition for Operations which require an action
from service considering such items as Technical Specifications
!                   statement to be carried out...." The licensee failed to
L.initing Condition for Operations which require an action
I                   evaluate the consequences of removing cornponents from service
!
                    in that no acknowledgernent of any Technical Specification
statement to be carried out...."
                    applicability was made in either the NSO log of the Control
The licensee failed to
                    Room Information System (CRIS) when the Division !! Control
I
                    Center HVAC was removed from service (341/85040-03b).
evaluate the consequences of removing cornponents from service
l     4. RCIC/ Core Spray Room Cooler
in that no acknowledgernent of any Technical Specification
        The NSS observed whilt. reviewing the combination o)erating panels during
applicability was made in either the NSO log of the Control
        his turnover on July 24, 1985, at 6:30 p.m. that tie control switch for
Room Information System (CRIS) when the Division !! Control
        the Division ! Reactor Core Injection Cooling (RCIC)/ Core Spray Room
Center HVAC was removed from service (341/85040-03b).
        Cooler was in the off-reset position, this made both RCIC and Division !
l
4.
RCIC/ Core Spray Room Cooler
The NSS observed whilt. reviewing the combination o)erating panels during
his turnover on July 24, 1985, at 6:30 p.m. that tie control switch for
the Division ! Reactor Core Injection Cooling (RCIC)/ Core Spray Room
Cooler was in the off-reset position, this made both RCIC and Division !
I
I
        core spray inoperable. The NSS who discovered the out-of-position switch
core spray inoperable. The NSS who discovered the out-of-position switch
        stated that it was in the proper position at 3:30 p.m. on July 23, 1985.
stated that it was in the proper position at 3:30 p.m. on July 23, 1985.
        The Itcensee also determined that the Motor Control Center (MCC-728-3A
The Itcensee also determined that the Motor Control Center (MCC-728-3A
        Position 20) feeding the room cooler was found in the off position.
Position 20) feeding the room cooler was found in the off position.
        Subsequent investigation by the licensee did not reveal any reason for
Subsequent investigation by the licensee did not reveal any reason for
        the coolers status nor could any PN-215 be identified which would have
the coolers status nor could any PN-215 be identified which would have
        authorized de-energizing the MCC feeder breaker. The room cooler was
authorized de-energizing the MCC feeder breaker. The room cooler was
        returned to service and the licensee documented the incident in
returned to service and the licensee documented the incident in
        DER NP-85-0390.
DER NP-85-0390.
        Theunitwasinthestartupmodeofoperation(OperationalCondition2)
Theunitwasinthestartupmodeofoperation(OperationalCondition2)
        at the time the room cooler was taken out of service, but was in a
at the time the room cooler was taken out of service, but was in a
        planned shutdown due to the loss of the South Reactor Feed Pump when
planned shutdown due to the loss of the South Reactor Feed Pump when
        the cooler was found out of service. (Reactorpressurehadbeenreduced
the cooler was found out of service.
        to less than 150 psig at 7:30 a.m. on July 24,1985.) RCIC is not
(Reactorpressurehadbeenreduced
to less than 150 psig at 7:30 a.m. on July 24,1985.) RCIC is not
l
l
l
l
                                              9
9
.


                                                                      _.     -                                     .
_.
      -
-
.
!
!
,   .
-
,
.
I
I
l       required to be operational below 150 psig; however, the High Pressure                                         ;
l
required to be operational below 150 psig; however, the High Pressure
CoreInjection(HPCI)hadbeeninoperablesinceJuly 11, 1985 thus for
'
'
        CoreInjection(HPCI)hadbeeninoperablesinceJuly 11, 1985 thus for
!
!      approximately sixteen (16) hours the HPCI, RCIC and Division I core
approximately sixteen (16) hours the HPCI, RCIC and Division I core
        spray systems were all inoperable.
spray systems were all inoperable.
                                                                                                                      i
i
i
'
'
        During the inspection and review of the event, two apparent violations                                         l
During the inspection and review of the event, two apparent violations
l      of Technical Specification requirements were identified as follows:
l
of Technical Specification requirements were identified as follows:
!
!
a.
Technical Specification 3.5.1.C.1 requires that during the startup
l
!
!
        a.  Technical Specification 3.5.1.C.1 requires that during the startup                                        l
l
l            modeofoperation,theHighPressureCoreInjection(HPCI) system
modeofoperation,theHighPressureCoreInjection(HPCI) system
            may be inoperable provided that the Core Spray (CS) system, the
may be inoperable provided that the Core Spray (CS) system, the
            Low Pressure Coolant Injection (LPCI) system, the Automatic
Low Pressure Coolant Injection (LPCI) system, the Automatic
            Depressurization System (ADS), and the Reactor Core Isolation
Depressurization System (ADS), and the Reactor Core Isolation
            Cooling (RCIC)systemareoperable.
Cooling (RCIC)systemareoperable.
            Contrary to the above, the licensee failed to ensure that the                                             ;
Contrary to the above, the licensee failed to ensure that the
            RCIC and Division ! core spray systems were operable when they                                           i
RCIC and Division ! core spray systems were operable when they
            allowed the RCIC/CS room cooler to be removed from service at                                             j
allowed the RCIC/CS room cooler to be removed from service at
            3:30 p.m. on July 23, 1985 with the HPCI system already inoperable                                       ;
j
            as of 3:00 a.m. on July 11, 1985. This condition existed for
3:30 p.m. on July 23, 1985 with the HPCI system already inoperable
            approximately sixteen hours, with the reactor in the Startup
;
            condition (341/85040-04).
as of 3:00 a.m. on July 11, 1985. This condition existed for
        b.   Technical Specification 6.8.1.a requires that written procedures
approximately sixteen hours, with the reactor in the Startup
            shall be established, implemented, and maintained covering the
condition (341/85040-04).
            applicable procedure recomendations of Appendix A of Regulatory
b.
            Guide 1.33 Revision 2, 1978. Appendix A of Regulatory Guide 1.33
Technical Specification 6.8.1.a requires that written procedures
            lists the following activities under Administrative Procedures:
shall be established, implemented, and maintained covering the
              -  Authorities and Responsibilities for Safe Operation...
applicable procedure recomendations of Appendix A of Regulatory
l              -   Equipment Control
Guide 1.33 Revision 2, 1978. Appendix A of Regulatory Guide 1.33
l             -   Shift and Reitef Turnovers
lists the following activities under Administrative Procedures:
(             -  Log Entries...
Authorities and Responsibilities for Safe Operation...
            Contrary to the above the licensee failed to ad (n to the
-
Equipment Control
l
-
Shift and Reitef Turnovers
l
-
(
Log Entries...
-
Contrary to the above the licensee failed to ad (n to the
provisions of Technical Specification 6.8.1.a as voilows:
!
!
            provisions of Technical Specification 6.8.1.a as voilows:                                                i
(1) POM Procedure 12.000.15"PN-21jWorkOrder) Processing,"
              (1) POM Procedure 12.000.15"PN-21jWorkOrder) Processing,"
Section 7.2.1 states, in part, All work activities at
                  Section 7.2.1 states, in part, All work activities at
Fermi 2...sha11 be controlled by a PN-21 and Attachmeet 'A'
                  Fermi 2...sha11 be controlled by a PN-21 and Attachmeet 'A'                                         ,
,
,                  to the PN-21." The licensee failed to write a PN-21 to                                             !
to the PN-21." The licensee failed to write a PN-21 to
                  de-energize the feeder breaker (NCC-728-3A Position 20) for
,
                  the RCIC/ Core Spray room cooler fan on July 23 and 24,1965
de-energize the feeder breaker (NCC-728-3A Position 20) for
                    (341/8504005a).
the RCIC/ Core Spray room cooler fan on July 23 and 24,1965
              (2) POM Procedure 21.000.01, " Shift Operations and Control Room "                                       ,
(341/8504005a).
l                 delineates the shif t turnover responsibilities of the Nuclear                                     !
(2) POM Procedure 21.000.01, " Shift Operations and Control Room "
,
l
delineates the shif t turnover responsibilities of the Nuclear
Shif t Supervisor (NSS) the Nuclear Assistant Shif t Supervisor
l
l
                  Shif t Supervisor (NSS) the Nuclear Assistant Shif t Supervisor                                    !
(NASS) and the Nuclear Station Operator (NS0).
                    (NASS) and the Nuclear Station Operator (NS0). Included in the                                     !
Included in the
                    responsibilities is a review of past log entries, and a review                                     '
responsibilities is a review of past log entries, and a review
'
l
l
!
!
                                                                                                                      !
10
                                            10                                                                         l
.
                                                                                                                      l
.
                                                                                                                      1
-
  _                      _    ___    _.  . _ _ - _ _ _ - _ _ _ _ _    _ _ _ _ _ _ - _ _ _ - _ _ _ _ _ _ - _ _ _ -
-
-
-
-
-


    .
.
  O
O
                    of each Combination Operating Panel for off-normal conditions
of each Combination Operating Panel for off-normal conditions
                    or the addition of CRIS " dots." The NSS, NASS, and NSO all
or the addition of CRIS " dots." The NSS, NASS, and NSO all
                      failed to adequately perform the required activities as the
failed to adequately perform the required activities as the
                    RCIC/ Core Spray room cooler fan switch was in the "off-reset"
RCIC/ Core Spray room cooler fan switch was in the "off-reset"
l                   position for approximately 24 hours on July 23 and 24,1985. The
l
                      normal position for the switch is in the " Auto" position. The
position for approximately 24 hours on July 23 and 24,1985. The
'
'
                    out of position switch went unobserved for two shift turnovers
normal position for the switch is in the " Auto" position. The
                      (341/85040-05b).
out of position switch went unobserved for two shift turnovers
                (3) P0M Procedure 21.000.01, Section 6.19.1.1 states, in part.
(341/85040-05b).
l                     " Evaluate the consequences of removing the system or component
(3) P0M Procedure 21.000.01, Section 6.19.1.1 states, in part.
                      from service considering such items as Technical Specifications
l
" Evaluate the consequences of removing the system or component
from service considering such items as Technical Specifications
Limiting Condition for Operations which require an action
'
'
                    Limiting Condition for Operations which require an action
statement to be carried out...."
                    statement to be carried out...." The licensee failed to
The licensee failed to
                    evaluate the consequences of removing components from service
evaluate the consequences of removing components from service
!                   as he did not take into account the existing inoperability of
!
l                    the HPCI system prior to removing the RCIC/ Core Spray room
as he did not take into account the existing inoperability of
l                   cooler from service nor was the action entered into the NSO
the HPCI system prior to removing the RCIC/ Core Spray room
                      log or the CRIS equipment status file (341/85040-05c).
l
      5. Cooling Tower Bypass Valve
l
          On July 26, 1985, while performing surveillance testing on Division I,
cooler from service nor was the action entered into the NSO
l       Emergency Diesel Generator (EDG) #11, a Diesel Generator Service Water
log or the CRIS equipment status file (341/85040-05c).
l
5.
          (DGSW) Low Flow Alarm was received. The alarm indicated a lack of
Cooling Tower Bypass Valve
          cooling water for the EDG. The operator verified the low flow and
On July 26, 1985, while performing surveillance testing on Division I,
l
Emergency Diesel Generator (EDG) #11, a Diesel Generator Service Water
l
(DGSW) Low Flow Alarm was received. The alarm indicated a lack of
cooling water for the EDG. The operator verified the low flow and
l
l
          innediately shutdown the EOG. The licensee, upon further investigatibn.
innediately shutdown the EOG. The licensee, upon further investigatibn.
          determined that the mechanical draft cooling tower bypass valve
determined that the mechanical draft cooling tower bypass valve
          E1150-F603A was closed and de-energized. This valve is required by a
E1150-F603A was closed and de-energized. This valve is required by a
          condition of the license to be open and de-energized, or one of the
condition of the license to be open and de-energized, or one of the
          cooling tower shutoff valves E1150 F604A/F605A is to be open and
cooling tower shutoff valves E1150 F604A/F605A is to be open and
          de-energized to prevent spurious closure due to hot shorts in the event
de-energized to prevent spurious closure due to hot shorts in the event
          of a fire in the plant. The nomal position for this motor operated
of a fire in the plant. The nomal position for this motor operated
          va'te is de-energized and open per POM Procedure 23.208, Revision 8.
va'te is de-energized and open per POM Procedure 23.208, Revision 8.
          Thi . is an apparent violation of License Condition 2.C.(9)(d) (341/85010-06).
Thi . is an apparent violation of License Condition 2.C.(9)(d) (341/85010-06).
          Invtstigation into the rcason why the bypass valve was out of proper
Invtstigation into the rcason why the bypass valve was out of proper
          position, identified that the valve was last manipulated on July 23,
position, identified that the valve was last manipulated on July 23,
          1985, while running the Reactor Heat Removal Service Water (RHR$W)
1985, while running the Reactor Heat Removal Service Water (RHR$W)
          system. The valve had exhibited a tendency to trip either the thermal
system. The valve had exhibited a tendency to trip either the thermal
          overloads or the torque switches during stroking and an operator had been
overloads or the torque switches during stroking and an operator had been
          required to partially stroke the valve to the desired position as well as
required to partially stroke the valve to the desired position as well as
          reset the thermal overloads to allow continued stroking from the control
reset the thermal overloads to allow continued stroking from the control
          room. It appears that clear instructions were not given to the Reactor
room.
          Building Rounds Operator as he was not aware of the necessity of leaving
It appears that clear instructions were not given to the Reactor
          the Ell 50 F603A valve in the open de energized condition.
Building Rounds Operator as he was not aware of the necessity of leaving
          The E1.50 F603A valve is located in the discharge flow path to the
the Ell 50 F603A valve in the open de energized condition.
          coolin$ water reservoir and its closure affects multiple systems. With
The E1.50 F603A valve is located in the discharge flow path to the
          the valve closed, flow of Erwrgency Equipment Service Water (EESW),
coolin$ water reservoir and its closure affects multiple systems. With
                                              11
the valve closed, flow of Erwrgency Equipment Service Water (EESW),
11
.
-


                                                    . -                             -.
. -
    .
-.
  .
.
.
RHR$W, and DGSW is blocked. Besides affecting the Division I EDG's,
.
.
        RHR$W, and DGSW is blocked. Besides affecting the Division I EDG's,
with the bypass valve closed all Division I emergency core cooling
        with the bypass valve closed all Division I emergency core cooling
systems were inoperable including the core spray and residual heat
        systems were inoperable including the core spray and residual heat
removal systems.
        removal systems.
At the time the bypass valve was discovered in the closed position, the
        At the time the bypass valve was discovered in the closed position, the
reactor was in cold shutdown, Condition 4, with the reactor temperature
        reactor was in cold shutdown, Condition 4, with the reactor temperature
at approximately 130*F and atmospheric pressure.
        at approximately 130*F and atmospheric pressure. In cold shutdown the
In cold shutdown the
        plant is required to have one operable division of ECCS, and one operable
plant is required to have one operable division of ECCS, and one operable
        divisionofEDG's(twodiesels). This condition was satisfied, however,
divisionofEDG's(twodiesels). This condition was satisfied, however,
        the bypass valve E1150-F603A had been closed since about 1:19 p.m. on
the bypass valve E1150-F603A had been closed since about 1:19 p.m. on
        July 23, 1985. On July 23, 1985, theunitwasinCondition2(Startup)
July 23, 1985. On July 23, 1985, theunitwasinCondition2(Startup)
        which requires both divisions of ECCS and both divisions of the onsite
which requires both divisions of ECCS and both divisions of the onsite
        electrical power source (EDG's) to be operable. As a result of the
electrical power source (EDG's) to be operable. As a result of the
        bypass valve being closed, only one division was operable. The failure
bypass valve being closed, only one division was operable. The failure
        to take remedial action with one division of the EDG's inoperable is
to take remedial action with one division of the EDG's inoperable is
        an apparent violation of T.S. 3.8.1.1.b (341/85040-07).
an apparent violation of T.S. 3.8.1.1.b (341/85040-07).
        On July 23, 1985, the licensee connenced a reactor shutdown at about
On July 23, 1985, the licensee connenced a reactor shutdown at about
        1:15 p.m. as a result cf the failure of the South Reactor Feed Pums.
1:15 p.m. as a result cf the failure of the South Reactor Feed Pums.
        It was fortuitous that the licensee coemenced a recctor shutdown a>out
It was fortuitous that the licensee coemenced a recctor shutdown a>out
        the same time the cooling tower bypass valve was de-energized in 'le
the same time the cooling tower bypass valve was de-energized in 'le
        closed position, as the licensee was by chance co.. plying with the
closed position, as the licensee was by chance co.. plying with the
        Limiting Condition for Operation (LCO) action statements in reducing
Limiting Condition for Operation (LCO) action statements in reducing
        power and proceeding to cold shutdown. Without this action, the plant
power and proceeding to cold shutdown. Without this action, the plant
        would have been in further violation of technical specifications.
would have been in further violation of technical specifications.
      6. Hydrogen Recombiner
6.
        On June 20, 1985, the licensee completed maintenance on the Division !!
Hydrogen Recombiner
        hydrogen recombiner per Work Order PN-21269327 to replace a leaking
On June 20, 1985, the licensee completed maintenance on the Division !!
        blower seal. The work order stated that post maintenance testing was
hydrogen recombiner per Work Order PN-21269327 to replace a leaking
        required, and identified Plant Operations Manual (POM) Procedures
blower seal. The work order stated that post maintenance testing was
        43.409.01, " Post LOCA Thermal Recombiner System Test," and 24.409.01
required, and identified Plant Operations Manual (POM) Procedures
        " Post LOCA Thermal Recombiner Functional Test." These procedures were
43.409.01, " Post LOCA Thermal Recombiner System Test," and 24.409.01
        required to demonstrate leak tight integrity and operability,
" Post LOCA Thermal Recombiner Functional Test." These procedures were
        respectively. The work order was stoned off as completed by the Nuclear       !
required to demonstrate leak tight integrity and operability,
        Shif t Supervisor on June 20,1985, w' thout the leakage test having been
respectively. The work order was stoned off as completed by the Nuclear
        perforned per P0M Procedure 43.409.01. This is an apparent violation of
Shif t Supervisor on June 20,1985, w' thout the leakage test having been
        TechnicalSpecifications(T.S.)6.8.1.aand6.8.4.ainthatthelicensee
perforned per P0M Procedure 43.409.01. This is an apparent violation of
        failed to follow estabitshed procedures and comply with the leakage
TechnicalSpecifications(T.S.)6.8.1.aand6.8.4.ainthatthelicensee
        reduction program (341/85040 08).                                             i
failed to follow estabitshed procedures and comply with the leakage
        On August 26 1985, the licensee initiated a Deviation / Event Report
reduction program (341/85040 08).
        LNo. I'P-85-0I55) to document the failure to perform the post maintenance
i
        leak rate testing on the Olvision !! hydrogen recombiner. After               i
On August 26 1985, the licensee initiated a Deviation / Event Report
        determining the failure to                    the licensee had sufficient   l
LNo. I'P-85-0I55) to document the failure to perform the post maintenance
                                        wrfom testing}ner
leak rate testing on the Olvision !! hydrogen recombiner. After
        infomation to declare the aydrogen   recomb     inoperable, as a result      j
the licensee had sufficient
        of exceeding the 30 day LCO limit, and the licensee did not take action
determining the failure to wrfom testing}ner inoperable, as a result
        per technical specification 3.0.3. to place the unit in hot shutdown
infomation to declare the aydrogen recomb
                                                                                      ,
j
                                            12
of exceeding the 30 day LCO limit, and the licensee did not take action
                                                                      .__---_-___a
per technical specification 3.0.3. to place the unit in hot shutdown
,
12
.
--- -
a


                                              _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ .       _ _ _ _ _ _ . _
_ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ .
                                            .
_ _ _ _ _ _ . _
                                                                                                                                      l
.
  *                                                                                                                                   l
l
        within six hours. The licensee proceeded to determine the leakage rate
*
        and on August 28, 1985, declared the Division II hydrogen recombiner
within six hours. The licensee proceeded to determine the leakage rate
        innperable as a result of the initial leakage rate testing. Subsequently
and on August 28, 1985, declared the Division II hydrogen recombiner
        on August 29, 1985, at 2:46 p.m. the licensee determined that the leakage
innperable as a result of the initial leakage rate testing. Subsequently
        rate was in excess of the allowable containment leakage. This is an
on August 29, 1985, at 2:46 p.m. the licensee determined that the leakage
        apparent violation of T.S. 3.6.6.1, and 3.0.3 in that the licensee failed
rate was in excess of the allowable containment leakage. This is an
        to comply with the LCO action statements (341/85040-09).
apparent violation of T.S. 3.6.6.1, and 3.0.3 in that the licensee failed
        At 6:00 p.m., on August 29, 1985, the licensee cummenced preparations
to comply with the LCO action statements (341/85040-09).
        to proceed to hot shutdown. The hydrcgen recombiner was repaired, leak
At 6:00 p.m., on August 29, 1985, the licensee cummenced preparations
        tested, and declared operable on August 29, 1985, at 9:00 p.m. The plant
to proceed to hot shutdown. The hydrcgen recombiner was repaired, leak
        was returned to the startup mode with pressure at 950 psig and 3.8% power
tested, and declared operable on August 29, 1985, at 9:00 p.m.
        for HPCI and SCRAM time testing at 10:40 p.m.
The plant
was returned to the startup mode with pressure at 950 psig and 3.8% power
for HPCI and SCRAM time testing at 10:40 p.m.
,
,
        During the time period from June 21 to July 21, 1985, the plant entered
During the time period from June 21 to July 21, 1985, the plant entered
l       Operational condition (Startup) on five (5) occasions including initial
l
        criticality (June 21, 1985, June 29, 1985, July 2, 1985, July 6, 1985,
Operational condition (Startup) on five (5) occasions including initial
criticality (June 21, 1985, June 29, 1985, July 2, 1985, July 6, 1985,
and July 10,1985) without both divisions of hydrogen recombiners
,
,
        and July 10,1985) without both divisions of hydrogen recombiners
l
l      operable. This is an apparent violation of T.S. 3.0.4(341/85040-10).
operable. This is an apparent violation of T.S. 3.0.4(341/85040-10).
    7. Breach of Primary Containment Integrity
7.
l       ThelicenseediscoveredaContainmentMonitoringSystemValve(T50-071A)
Breach of Primary Containment Integrity
!       which is a primary containment boundary, in the open position and uncapped
l
I     on September 2, 1985. The valve was shut upon discovery. The Nuclear
ThelicenseediscoveredaContainmentMonitoringSystemValve(T50-071A)
l       Shif t Supervisor (NSS) was informed of the event on September 4,1985,
!
l       approximately 39 hours af ter discovery. ADeviation/EventReport(DER)
which is a primary containment boundary, in the open position and uncapped
l       (No.NP-85-0469) was written to document the open valve.
I
        Valve T50-071A was installed under Engineering Design Package (EDP)
on September 2, 1985. The valve was shut upon discovery. The Nuclear
        No. 1970 dated March 25, 1985. The EDP included the installation of four
l
        test connection cutoff valves in the primary containment monitoring
Shif t Supervisor (NSS) was informed of the event on September 4,1985,
        system. Valves T50-068A and B were installed in piping from the bottom
l
        of the torus while valves T50-071A and B were installed in piping from
approximately 39 hours af ter discovery. ADeviation/EventReport(DER)
        the top of the torus. PN-21(WorkOrder)No. 814949 was written to
l
        install the "A" valves in Division I and PN-21 No. 814948 was written to
(No.NP-85-0469) was written to document the open valve.
        install the "8" valves in Olvision !!. Both PN-21s were signed off as
Valve T50-071A was installed under Engineering Design Package (EDP)
        " Order Completed" on June 20, 1985.                                       It should be noted that neither EDP
No. 1970 dated March 25, 1985. The EDP included the installation of four
        1970 nor the four PN-21s associated with it were closed out as of
test connection cutoff valves in the primary containment monitoring
        September 10, 1985.
system. Valves T50-068A and B were installed in piping from the bottom
        Doth PN-21s for the primary containment monitoring system required Local
of the torus while valves T50-071A and B were installed in piping from
        Leak Rate Tests (LLRTs) plus Plant Operations Manual Procedure
the top of the torus. PN-21(WorkOrder)No. 814949 was written to
        24.000.05, " Monthly Continuity Light and Channel Check Test," Section 4
install the "A" valves in Division I and PN-21 No. 814948 was written to
        " Precautions and Limitations" to be completed. The NSS signed the
install the "8" valves in Olvision !!. Both PN-21s were signed off as
        PN-21s as order complete on June 20, 1985. The licensee reviewed EDP
" Order Completed" on June 20, 1985.
        1970 and detemined that the LLRTs for the primary containment monitoring
It should be noted that neither EDP
        system modifications had not been performed. DER No. NP-85-471 dated
1970 nor the four PN-21s associated with it were closed out as of
        September 5, 1985, was written to document this discrepancy. The licensee
September 10, 1985.
        subsequently performed the missed LLRTs and three of the four LLRTs met
Doth PN-21s for the primary containment monitoring system required Local
                                            13
Leak Rate Tests (LLRTs) plus Plant Operations Manual Procedure
24.000.05, " Monthly Continuity Light and Channel Check Test," Section 4
" Precautions and Limitations" to be completed. The NSS signed the
PN-21s as order complete on June 20, 1985. The licensee reviewed EDP
1970 and detemined that the LLRTs for the primary containment monitoring
system modifications had not been performed. DER No. NP-85-471 dated
September 5, 1985, was written to document this discrepancy. The licensee
subsequently performed the missed LLRTs and three of the four LLRTs met
13


                .
.
        .
.
!                           procedural criteria. The LLRT for Penetration.X203A.(P0M Procedure
!
                            43.401.386) which contains valve T50-071A did not meet the leakage
procedural criteria. The LLRT for Penetration.X203A.(P0M Procedure
                            criteria. Two of the three boundary valves were repaired and the
43.401.386) which contains valve T50-071A did not meet the leakage
                            penetration subsequently met the test criteria,
criteria. Two of the three boundary valves were repaired and the
p                           During the inspection and review of the event, three apparent violations
penetration subsequently met the test criteria,
p
During the inspection and review of the event, three apparent violations
were identified as follows:
,
,
                            were identified as follows:
i
i                            a.     Technical Specification 3.6.1.1 requires that PRIMARY CONTAINMENT
a.
                                      INTEGRITY shall be maintained in Operational Conditions 1, 2,-and 3.
Technical Specification 3.6.1.1 requires that PRIMARY CONTAINMENT
e                                    Without PRIMARY CONTAINMENT INTEGRITY restore PRIMARY CONTAINMENT.
INTEGRITY shall be maintained in Operational Conditions 1, 2,-and 3.
Without PRIMARY CONTAINMENT INTEGRITY restore PRIMARY CONTAINMENT.
e
INTEGRITY within one hour or be in at least HOT SHUTDOWN within the
*
*
                                      INTEGRITY within one hour or be in at least HOT SHUTDOWN within the
[
[                                    next 12 hours and in COLD SHUTDOWN within the following 24 hours.
next 12 hours and in COLD SHUTDOWN within the following 24 hours.
,
,
4                                    Contrary to the above, the licensee failed to maintain containment
Contrary to the above, the licensee failed to maintain containment
i                                     integrity from June 21 to September 2,1985, in that primary
4
                                    containmentmonitoringsystemvalve(T50-F071-A)wasintheopen
i
                                    position and the line downstream of the' valve was uncapped which
integrity from June 21 to September 2,1985, in that primary
4                                    resulted in an open pathway from the primary containment to the.
containmentmonitoringsystemvalve(T50-F071-A)wasintheopen
L                                   reactor building. Primary containment integrity was required during
position and the line downstream of the' valve was uncapped which
l                                   this time frame except for 6.25 days of the interval-(341/85040-11).
resulted in an open pathway from the primary containment to the.
!                           b.     Technical Specification 6.8.1.a requires that written procedures
4
                                    shall be established, implemented, and maintained covering the-
L
                                    applicable procedure recommendations of Appendix A of-Regulatory-
reactor building. Primary containment integrity was required during
l
this time frame except for 6.25 days of the interval-(341/85040-11).
!
b.
Technical Specification 6.8.1.a requires that written procedures
shall be established, implemented, and maintained covering the-
applicable procedure recommendations of Appendix A of-Regulatory-
.
.
                                    Guide 1.33 Revision 2, 1978. Appendix- A of Regulatory Guide'1.33.
Guide 1.33 Revision 2, 1978. Appendix- A of Regulatory Guide'1.33.
l                                   lists the following activities under Administrative Procedures:
l
lists the following activities under Administrative Procedures:
!
(1) Equipment Control
(2) Log Entries...
i
Contrary to the above, the licensee failed to adhere to the
provisions of Technical Specification 6.8.1.a as follows:
1
!
!
                                          (1) Equipment Control
P0M Procedure 12.000.15, "PN-21 (Work Order) Processing," Revision 11,
                                          (2) Log Entries...
August 20, 1985, paragraph 7.3.16 states:
i                                    Contrary to the above, the licensee failed to adhere to the
"Upon completion of all-
1
                                    provisions of Technical Specification 6.8.1.a as follows:
!                                    P0M Procedure 12.000.15, "PN-21 (Work Order) Processing," Revision 11,
*
*
                                    August 20, 1985, paragraph 7.3.16 states: "Upon completion of all-
maintenance, testing, STR or EPC and after_the ' Accepted for Service-
;                                    maintenance, testing, STR or EPC and after_the ' Accepted for Service-
;
By' slot has been signed, the pink copy-of PN-21 is forwarded to the
'
'
                                    By' slot has been signed, the pink copy-of PN-21 is forwarded to the
Nuclear Shift Supervisor who will review the order and sign ' Order
                                    Nuclear Shift Supervisor who will review the order and sign ' Order
~
                                                                                      ~
i
i                                   Completed.'" Contrary to the above, the licensee failed to adhere -                     ' ,
Completed.'" Contrary to the above, the licensee failed to adhere -
to the requirements of POM Procedure 12.000.15. in that Work Order-
' ,
i
,
i
i
                                    to the requirements of POM Procedure 12.000.15. in that Work Order-                          ,
PN-21 No. 814945 (covering the addition of leak rate test conriection.
i                                    PN-21 No. 814945 (covering the addition of leak rate test conriection.                         '
'
:                                    valve T50-F071A) was signed " order completed" on June 20, 1985,
valve T50-F071A) was signed " order completed" on June 20, 1985,
;                                   without the post installation leak rate testing being performed as.                           ;
:
;                                   specified.onthework-order-(341/85040-12)..
;
without the post installation leak rate testing being performed as.
;
;
specified.onthework-order-(341/85040-12)..
i
i
                                                                .
.
                                                                          .
.
                                                                                            ..             ..
..
                                                                                                                                    ;
..
;
i
i
                          . c.     10 CFR 50, Appendix B, Criterion VI,; states, in part,a" Measure. shall:                       !
. c.
:                                   be established to control the issuance of documents, such as                                   *
10 CFR 50, Appendix B, Criterion VI,; states, in part,a" Measure. shall:
                                    instructions, procedures,'and drawings,. including changes'thereto,
!
                                    which prescribe all activities affecting quality. These measures
:
;                                    shall assure that documents including changes are reviewed for                                 '
be established to control the issuance of documents, such as
                                    adequacy...."                                             '
*
                                                                                                                                ,3
instructions, procedures,'and drawings,. including changes'thereto,
                                                                                                          %           '
which prescribe all activities affecting quality. These measures
                                                                                                                                    .
shall assure that documents including changes are reviewed for
                                                                                                          yi                       :
'
                                                                                                    9 ,l,m
;
                                                                                                      '
adequacy...."
                                                                  .14~
'
                                                                                                                                    ,
,3
  _ . . _ . _ . _ . . _ _ _ _ . . _                                        -
%
                                                                                                  ,3 -
'
                                                                                                        .a   . . ...   . _
.
yi
:
,m
9
,l
.14~
'
,
. .
.
.
. .
. .
-
,3
-
.a
. . ...
.


          .       -             . .. -                   -                         - .       . -         .         . .. . - - . -
.
              .
-
                                                                                                                                                          *
. .. -
;
-
      .
- .
. -
.
. .. . - - . -
.
;
*
.
i
i
I
I
                                        POM Procedure' 12.000.64, "EDP1 Implementation Procedure,": Revision 2,                                         ..;
POM Procedure' 12.000.64, "EDP1 Implementation Procedure,": Revision 2,
                                        dated March 5, 1985, Section 6.5.1; states, in part, "The responsible                                             !
..;
                                        PSE shall identify the plant documents requiring revision when the -                                           4
dated March 5, 1985, Section 6.5.1; states, in part, "The responsible
!
PSE shall identify the plant documents requiring revision when the -
4
package is prepared."
*
*
                                        package is prepared."
Contrary to the above, the EDP. Implementation Procedure for EDP'
                                        Contrary to the above, the EDP. Implementation Procedure for EDP'
:
:                                       No.1970, covering.the installation of the containment sample system .                                             '
No.1970, covering.the installation of the containment sample system .
!-                                       leak rate test connection valve T50-f CIA, did not. identify.all                                                   -
'
I                                       the plant documents requiring revision in that it did not identify.                                             .l
! -
                                        POM Procedures 24.425.01, " Primary Containment Integrity                                                         i
leak rate test connection valve T50-f CIA, did not. identify.all
l                                       Verification for Valves Outside Containment," or 47.000.77, " Test                                                 *
-
                                        Vent and Drain (TVD) Cap:and Plug Verification." The failure to                                                   :
I
the plant documents requiring revision in that it did not identify.
.l
POM Procedures 24.425.01, " Primary Containment Integrity
i
l
Verification for Valves Outside Containment," or 47.000.77, " Test
*
Vent and Drain (TVD) Cap:and Plug Verification." The failure to
:
identify these documents resulted in valve T50-F071A (an_d seven-.
:
,
,
                                        identify these documents resulted in valve T50-F071A (an_d seven-.                                                :
;
;                                        other valves) not being incorporated into the procedures used to                                                     .
other valves) not being incorporated into the procedures used to
;                                       verify containment integrity (341/85040-13).                                                                         !
.
                    8. 'Sumary                                                                                                                         ];
;
1                                                                                                                                                       ;
verify containment integrity (341/85040-13).
                                                                                    -     .                           .
!
                                                                                                                                                          3
];
8. 'Sumary
1
;
-
.
.
3
Twenty-six -violations (including multiple examples) of NRC requirements
j
-
-
                            Twenty-six -violations (including multiple examples) of NRC requirements                                                    j
are identified in this report. The majority of these fall into the
                            are identified in this report. The majority of these fall into the
i
                                                                                            .                                                               i
.
;                           category of failure to follow procedures._ This represents a-breakdown                                                       j
;
i                             in the licensee's ability to operate the plant in accordance with.                                                           !
category of failure to follow procedures._ This represents a-breakdown
                            prescribed procedures as required by the Technical Specifications.                                                         lj
j
                                                                                                                                                          :
i
in the licensee's ability to operate the plant in accordance with.
!
prescribed procedures as required by the Technical Specifications.
lj
:
The licensee's Operational Assurance (0A) organization has a program
!
;
;
called. Procedure Compliance Module (PCM) which monitors, on a monthly :
!
'
'
                            The licensee's Operational Assurance (0A) organization has a program                                                          !
bases, procedural compliance by various organizations. The results'of
                            called. Procedure Compliance Module (PCM) which monitors, on a monthly :                                                      !
!
~
-
six monthly surveillances (January-June 1985) clearly' revealed that the
;
operations section had had problems in following procedures. (Procedural
i
;
compliance ran from 74% to 100% and there was no trend--the results were
-
-
                            bases, procedural compliance by various organizations. The results'of
erratic. The six-month average was 87% with 99% compliance as a goal.
                                                                                                                ~
[
                                                                                                                                                            !
*
                            six monthly surveillances (January-June 1985) clearly' revealed that the
It should be noted that the findings of-the PCM program are not absolute
;                            operations section had had problems in following procedures. (Procedural                                                      i
;                            compliance ran from 74% to 100% and there was no trend--the results were                                                      -
                      *
                            erratic. The six-month average was 87% with 99% compliance as a goal.                                                         ['
:
:
'
'
                            It should be noted that the findings of-the PCM program are not absolute
'
          -
-
                            but are excellent indicators of potential-problem areas. The'results,                                                       l
but are excellent indicators of potential-problem areas. The'results,
;                           both current and cumulative, are issued monthly. Theslicensee had                                                           1
l
(                           sufficient knowledge of procedural compliance problems to initiate                                                             !
;
j,                          corrective actions rather than wait for a larger' data base.                                                                  !
both current and cumulative, are issued monthly. Theslicensee had
1
(
sufficient knowledge of procedural compliance problems to initiate
!
!
                            Seven of the violations were failures to meet Technical Specification
j,
corrective actions rather than wait for a larger' data base.
!
Seven of the violations were failures to meet Technical Specification
!
.
LimitingConditionforOperations(LC0's).1 Each of these were serious and
!
[
collectively represented a breakdown in the licensee's administrative and
i
management controls design to safely operate the plant. The safety;
!
significance!of the violations was. mitigated considerably by two' items-
. i
i
the plant had only operated for 20 days at an average power of,2 percent;
.
.
                            LimitingConditionforOperations(LC0's).1 Each of these were serious and                                                        !
!
[                            collectively represented a breakdown in the licensee's administrative and                                                    i
and the failure of the South Reactor Feed Pump turbine which resulted in-
                            management controls design to safely operate the plant. The safety;                                                            !
j
                            significance!of the violations was. mitigated considerably by two' items-                                                    i
the licensee shutting the reactor down. The inspectors consider the
.                            the plant had only operated for 20 days at an average power of,2 percent;                                                  .i
'
!                          and the failure of the South Reactor Feed Pump turbine which resulted in-                                                     j
;
>
<
<
          >
4
                            the licensee shutting the reactor down. The inspectors consider the                                                .        !
second item to be fortuitous.in-that the: reactor was removed from an
                            second item to be fortuitous.in-that the: reactor was removed from an
.
                                                                                                                                                '
!
4                                                                                                                                                          ;
i
operating condition which required certain equipment to be operable or
'
ractions to'be taken when the licensee wasLunaware that the actions or..
,
J
equipment were. required..
"
]
;.
.
[
'N
!
:.
.:
i
i
                            operating condition which required certain equipment to be operable or                                                        '
s
                          "ractions to'be taken when the licensee wasLunaware that the actions or..
.
                                                                                                                                                          ,
_
                    J      equipment were. required..
1
;.                                                                                                                                                      ] .
[          'N                                                                                                                                            !
:.                                                                                                                                                      .:
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                                                                                                                                                          .
+
+
                                      _
.
                                                                                  .
-15
                                                                                                                                                        1
.
.
,
,
                                                                              -15
.
                                                .
.
                                                                                                                                                            .
3
3
                                                                                                                                                      '
'
                ..
..
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;,.s
                                                                                                                                                          *
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    .,
.,
  .
.
          Twenty-six violations, many of them repetitive, have been identified-
Twenty-six violations, many of them repetitive, have been identified-
          in this. report.- Operating history mitigated their safety significance;
in this. report.- Operating history mitigated their safety significance;
          however, they demonstrated a major breakdown in the licensee's
however, they demonstrated a major breakdown in the licensee's
          administrative controls to safely operate the plant.
administrative controls to safely operate the plant.
      9. Management Meetings
9.
          a.   OutJof-Sequence Rod Pull
Management Meetings
                DECO management.(denoted in Paragraph 1) met with RIII management.
a.
                in' Glen Ellyn, Illinois,-on July 23, 1985', to' discuss the sequence of
OutJof-Sequence Rod Pull
                events surrounding the out-of-sequence rod pull which occurred on
DECO management.(denoted in Paragraph 1) met with RIII management.
                July 1 and 2,.1985, and their subsequent actions. This meeting was,
in' Glen Ellyn, Illinois,-on July 23, 1985', to' discuss the sequence of
                attended by the public.
events surrounding the out-of-sequence rod pull which occurred on
                The . licensee's presentation included a' detailed sequence.'of events
July 1 and 2,.1985, and their subsequent actions. This meeting was,
                imediately preceding and following the event, the rod pull _ sheets,
attended by the public.
                and the Source Range Monitor (SRM) strip chart which. corresponded to-
The . licensee's presentation included a' detailed sequence.'of events
                the time of the incident. .The licensee also presented a layout of
imediately preceding and following the event, the rod pull _ sheets,
                the control room and the relative location in the control room of
and the Source Range Monitor (SRM) strip chart which. corresponded to-
                those on shift at the time of the event. A great deal of discussion
the time of the incident. .The licensee also presented a layout of
                was focused on the events and licensee' actions subsequent.to the
the control room and the relative location in the control room of
                incident. The adequacy of the onshift review was discussed; RIII's
those on shift at the time of the event. A great deal of discussion
                position was that the onshift review was insufficient. Considerable
was focused on the events and licensee' actions subsequent.to the
                discussion was focused around the adequacy, completeness, and
incident. The adequacy of the onshift review was discussed; RIII's
                timeliness of the reporting of the incident to the NRC. The
position was that the onshift review was insufficient. Considerable
                licensee did not consider the event to he reportable under 10 CFRs
discussion was focused around the adequacy, completeness, and
                50.72 or 50.73. Region III concurred that the incident was.not
timeliness of the reporting of the incident to the NRC. The
                reportable under 10 CFR 50.72 or 50.73, but given;the proximity of
licensee did not consider the event to he reportable under 10 CFRs
r               the Comission's full-power briefing, Deco should have been more-
50.72 or 50.73. Region III concurred that the incident was.not
reportable under 10 CFR 50.72 or 50.73, but given;the proximity of
r
the Comission's full-power briefing, Deco should have been more-
'
'
                sensitive to the importance of keeping.the NRC informed.- The
sensitive to the importance of keeping.the NRC informed.- The
                Regional Administrator informed the licensee that he had requested
Regional Administrator informed the licensee that he had requested
[               the Office of Investigations (OI) to. investigate the event.
[
                The licensee also discussed their actions pertaining to whether or
the Office of Investigations (OI) to. investigate the event.
                                                    ~
The licensee also discussed their actions pertaining to whether or
                not the unit had been critical, as a ' result of the out-of-sequence .
~
                rod pull, and their corrective action. program. The licensee was
not the unit had been critical, as a ' result of the out-of-sequence .
                informed that Region III would send an inspection team to Femi.2 -
rod pull, and their corrective action. program. The licensee was
                to assess control room operations and the effectiveness of. the -
informed that Region III would send an inspection team to Femi.2 -
                corrective action program.                                       -
to assess control room operations and the effectiveness of. the -
                The licensee's presentation is included as-an-attachment to DECO
corrective action program.
                letter No. RC-LG-85-0017~ (Jens to Keppler) dated September 5, .1985.
-
          b.   Corrective Action Program
The licensee's presentation is included as-an-attachment to DECO
                DECO management (denoted in Paragraph 1) net with Region III-
letter No. RC-LG-85-0017~ (Jens to Keppler) dated September 5, .1985.
                management in Glen Ellyn,' Illinois, on September 10, 1985, to discuss
b.
                their corrective action program to preclude the repetition of the ~
Corrective Action Program
                events which were reported to the NRC during July and. August 1985'and
DECO management (denoted in Paragraph 1) net with Region III-
                documented elsewhere in this report. -The meeting was attended by
management in Glen Ellyn,' Illinois, on September 10, 1985, to discuss
                                                        .
their corrective action program to preclude the repetition of the ~
                representatives of the. Monroe County. Government and the public.
events which were reported to the NRC during July and. August 1985'and
documented elsewhere in this report. -The meeting was attended by
.
representatives of the. Monroe County. Government and the public.
!
!
i
i
!                                             16'
!
16'


    .
.
  .
.
                The licensee proposed a corrective action program based on
The licensee proposed a corrective action program based on
                observations and recommendations made by the Institute of Nuclear
observations and recommendations made by the Institute of Nuclear
                Power Operations (INP0) assistance inspection team, findings of two
Power Operations (INP0) assistance inspection team, findings of two
                recent NRC team inspections, conditions of the Confimatory Action
recent NRC team inspections, conditions of the Confimatory Action
                Letter (CAL-RIII-85-10) dated July 16, 1985, findings by the
Letter (CAL-RIII-85-10) dated July 16, 1985, findings by the
                resident NRC inspectors, and recommendations made by Management
resident NRC inspectors, and recommendations made by Management
                AnalysisCorporation(MAC). The program was divided into short
AnalysisCorporation(MAC). The program was divided into short
                and long term actions. Short term actions were to be completed
and long term actions. Short term actions were to be completed
                prior to power escalation above five percent. Long term actions
prior to power escalation above five percent. Long term actions
                addressed programmatic areas with the licensee indicating a phased
addressed programmatic areas with the licensee indicating a phased
                implementation to minimize pertubations to plant operations.
implementation to minimize pertubations to plant operations.
                Long term actions were to be initiated prior to exceeding five
Long term actions were to be initiated prior to exceeding five
                percent power but not to be completed until some later date with
percent power but not to be completed until some later date with
                the longest date of December 1, 1986.
the longest date of December 1, 1986.
                Deco requested that the five percent power restriction be lifted but
Deco requested that the five percent power restriction be lifted but
                that they would commit to not exceeding twenty percent power until
that they would commit to not exceeding twenty percent power until
                after the forthcoming outage which is scheduled to start during
after the forthcoming outage which is scheduled to start during
                October 1985. The request was denied.
October 1985. The request was denied.
                Region III requested that the licensee docket the corrective action
Region III requested that the licensee docket the corrective action
                program which had been presented and include methods of monitoring
program which had been presented and include methods of monitoring
                the effectiveness of the corrective actions. The licensee
the effectiveness of the corrective actions. The licensee
                subsequently submitted their " Reactor Operations Improvement
subsequently submitted their " Reactor Operations Improvement
                Plan" in a letter from Jens to Keppler (DECO No. VP-85-0198)
Plan" in a letter from Jens to Keppler (DECO No. VP-85-0198)
                dated October 10, 1985 (copy attached).
dated October 10, 1985 (copy attached).
                The licensee was also informed that another inspection team would
The licensee was also informed that another inspection team would
                be sent to Femi 2 to observe operations and review the corrective
be sent to Femi 2 to observe operations and review the corrective
                action program and its effectiveness before .the five percent
action program and its effectiveness before .the five percent
                restriction could be lifted. This action was predicated upon
restriction could be lifted. This action was predicated upon
                a satisfactory resolution of the 01 investigation.
a satisfactory resolution of the 01 investigation.
      10. Enforcement Conference
10. Enforcement Conference
          The NRC staff met with licensee representatives (denoted in Paragraph 1)
The NRC staff met with licensee representatives (denoted in Paragraph 1)
          during the management meetings and at various times during the inspection
during the management meetings and at various times during the inspection
          and reviewed the issues discussed in this report.
and reviewed the issues discussed in this report.
          The staff also discussed the likely informational content of the
The staff also discussed the likely informational content of the
          inspection report with regard to documents or processes review by the
inspection report with regard to documents or processes review by the
          inspectors during the inspection. The licensee did not identify any
inspectors during the inspection. The licensee did not identify any
          such documents / processes as proprietary.
such documents / processes as proprietary.
I
I
!
!
!
!
!
!
                                              17
17
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[
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Latest revision as of 02:17, 25 May 2025

Insp Rept 50-341/85-40 on 850701-1015.Violation Noted: Failure to Adhere to Tech Spec 6.8.1.2 Re Startup of Reactor on 850701 & Failure to Place Control Room Emergency Filtration Sys in Recirculation Mode of Operation
ML20137C726
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 11/14/1985
From: Wright G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20137C718 List:
References
50-341-85-40, NUDOCS 8601160395
Download: ML20137C726 (17)


See also: IR 05000341/1985040

Text

_ _ _ _ _ _ _ - _ - - _ ____-_ __ . _ _ _

,

O

O

U.S. NL' CLEAR REGULATORY C0m11SSION

REGION III

Report No. 50-341/85040(DRP)

Docket No. 50-341

License No. NPF-43

.

Licensee: Detroit Edison Company

2000 Second Avenue

Detroit, MI 48226

i

facility Name: Femi 2

Inspection At: Femi Site, Newport, MI

Inspection Conducted: July 1 through October 15, 1985

'

Management Meetings At: Glen Ellyn, Illinois on July 23

i

and September 10, 1985

Inspectors:

P. M. Byron

]

M. E. Parker

D. C. Jones

'

!

i

)G. C. Wright, Chief

/lf/'/ff[

dG LO

Approved By:

Projects Section 2C;

Date

.

Inspection Summary

Inspection on July 1 through October 15, 1985, and Management Meetings on

July 23 and September 10, 1985 (Report No. 50-341/85040(DRP))

Areas Inspected: Special, unannounced inspection by resident inspectors of

activities surrounding the out-of-sequence rod pull, the control room HVAC,

the RCIC/ core spray room cooler, the cooling tower bypass valve, the hydrogen

recombiner and the breach of primary containment integrity. The inspection

,

involved a total of 246 inspector-hours onsite by three inspectors including

'

77 hours8.912037e-4 days <br />0.0214 hours <br />1.273148e-4 weeks <br />2.92985e-5 months <br /> onsite during off-shifts. The Management Meetings involved a total of

153 hours0.00177 days <br />0.0425 hours <br />2.529762e-4 weeks <br />5.82165e-5 months <br /> by 26 NRC personnel.

Results: Twenty-sixviblations(includingexamples)wereidentified(seven-

,

Limiting Condition for Operations and nineteen - Procedural).

j

j

p"um mgb

-

- -

-

__ ____- _____ - _ _ _

_ ___ ____ -__ _ _

f

.,

'

.

1

DETAILS

i

l

l

1.

Attendees

a.

Persons Attending Management Meeting on July 23, 1985

l

~

'

Deco

C. M. Heidel President

W. H. Jens. Vice-President, Nuclear Operations

R. S. Lenart, Assistant Manager, Nuclear Production

A. Wegele, Compliance Engineer

D. A. Aniol. Nuclear Shift Supervisor

G. R. Overbeck, Superintendent, Operations

P. A. Marquardt, General Attorney

L. C. Lessor, Advisor, Management Analysis Co.

Public

!

B. Campball, Reporter, Detroit Free Press

'

NRC HQ's

E. Jordon, Director, Division of EP

B. J. Youngblood, NRR Licensing Chief, Branch No. 1

M. D. Lynch, NRR Licensing Project Manager

NRC RI!!

J. G. Keppler, Regional Administrator

C. J. Paperiello, Director, Division of Reactor Safety

E. Greenman, Deputy Director, Division of Reactor Projects

l

N. J. Chrissotimos, Chief, Branch 2. DRP

'

L. A. Reyes, Chief, Operations Branch, DRS

l

G. C. Wright, Chief. Section 2C, DRP

P. M. Byron, SRI Fermi 2

T. E. Lang, Operator Licensing

,

B. Stapleton, Enforcement Specialist

'

W. H. Schultz, Enforcement Coordinator

S. Stasek, Project Inspector, Femi

R. B. Landsman, Project Manager, Section 2C, DRP

5. G. DuPont, Reactor Inspector

R. D. Lanksbury, Reactor Inspector

l

!

!

2

,*

,

. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ ___ _ _ __ _ _ ____ __ - - ______

._- __________ _

.

.

b.

Persons Attending Management Meeting on September 10, 1985

DECO

C. M. Heidel, President

W. H. Jens, Vice-President, Nuclear Operations

R. S. Lenart Assistant Manager, Nuclear Production

T. Randazzo Director, Regulatory Affairs

E. P. Griffing Assistant Manager, Regulatory Compliance

L. C. Lessor, Advisor, Management Analysis Co.

Wolverine Power Supply

C. Borr, Member, Services Coordinator

J. Gore, Consultant

Public

T. Lam, Reporter, Ann Arbor News

S. Benkelman, Reporter, The Detroit News

B. Campball, Reporter, Detroit Free Press

M. Johnston, Member, Safe Energy Coalition of Michigan

J. Puntennery, Director, Safe Energy Coalition of Michigan

F. Kuron, Monroe County Commissioner

J. Eckert. Director, Office of Civil Preparedness

NRC HQ's

H. D. Lynch, NRR Licensing Project Manager

L. P. Crocker, NRR Licensing Section Chief, Quality Branch

NRC RIII

J. G. Keppler, Regional Administrator

A. B. Davis, Deputy Regional Administrator

C. E. Norelius Director, Division of Reactor Projects

E. Greenman, Deputy Director, Division of Reactor Projects

G. C. Wright, Chief, Section 2C, DRP

P. H. Byron, SRI, Fermi 2

B. W. Stapleton, Enforcement Specialist

J. Strasma. Public Affairs Officer

R. Lickus, Chief. State of Government Affairs

J. A. Hind. Director, Division of Radiation Safety and Safeguards

W. D. Shafer Branch Chief Emergency Preparedness and Radiological

Protection

R. B. Landsman, Project Manager, Section 2C, DRP

C. H. Weil, Compliance Specialist

T. E. Long Operator Licensing

L. Dimmock, Operator Licensing

3

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2.

Out-of-Sequence Rod Pull

While withdrawing control rods to achieve criticality on July 1, 1985,

the Nuclear Supervising Operator (NS0) pulled eleven control rods in

'

Group 3 to position 48 rather than position 04 as required by the control

rod pull sheets.

l

The afternoon shift NSO had started pulling control rods around 10:21 p.m.

!

EDT on July 1, 1985, and completed pulling centrol rods through step 37

l

at 11:15 p.m. EDT.

The night shift NSO started to pull rods at step 38

one minute and eleven seconds later.

The night shift NSO had observed

l

the off going NSO for a period of time before taking the controls.

The

l

nightshift NSO utilized a Shift Technical Advisor in Training (STAIT) to

l

monitor the Source Range Monitor (SRM) instrumentation to facilitate the

l

rod pull rather than perform that function himself.

The NSO completed

pulling rods in Group 2 and then commenced pulling rods in Group 3

(step 46).

Starting with step 46 and for the next 10 steps the NSO

pulled each control rod to the full out position (48) rather than

position 04 as required by the procedure.

The NSO verified by his

initials, on the rod pull sheet, that each of the eleven control rods

was at position 04 when in fact they were at position 48.

While pulling the eleventh control rod in Group 3 (control rod 18-51),

the Short Period Alarm annunciated five times and the pen for the

Channel A SRM recorder failed to ink for about three minutes. When

l

the pen started inking again the NSO and STAIT observed that recorder

was reading approximately 5x103 counts per second and increasing.

The

Shif t Reactor Engineer (SRE) had predicted that criticality should occur

between steps 150 and 160, when the NSO observed the increasing count

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rata he was only on step 56.

The NSO instructed the STAIT to inform the

Nuclear Shif t Supervisor (NSS) of the situation and immediately started

to insert rod 18-51.

It took 14 minutes and 41 seconds to insert all

eleven control rods to position 04.

Thirty-five (35) seconds later

the NSO continued the startup by pulling rods from step 57 of

the procedure.

During the control rod pulls the NSS and the Nuclear Assistant Shift

Supervisor (NASS) were in the NSS's office.

The SRE was behind the panels

and could not observe the rod pulls.

The NSO in charge of the control

room was at his desk facing the pan 11s and the Shift Technical Advisor

(STA) and the Shift Operations Advisor (50A) were by the NSO's desk,

Neither the NSO in charge, the SOA, nor the STA were observing the rod

pull nor were they aware of the incident.

The STAIT Informed the SRC

of the event who wrote in his log that the reactor may have been

critical.

The NSS reviewed the event with the NSO (at the controls) and the STAIT

and determined that the reactor had not gone critical.

lhe NSS then

directed that rod pulling recommence.

The NSS apparently did not seek

the advice or counsel of the SRE, the SOA, or the S1A,

The SRE also ,

lined out in his log book the reference of the unit being critical.

Neither the NSS nor the NSO logs contained an entry regarding the

4

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.

out-of-sequence rod pull.

The NSS, however, did write a Deviation /

Event Report (DER) (No. NP-85-0334) describing the event and stated that

the reactor had not gone critical.

DER No. NP-85-0334 was reviewed by the licensee's Corrective Action

Review Board (CARB) on July 2,1985, who concurred with the NSS's

determination that the incident was not reportable under either 10 CFR 50.72 or 50.73.

It appeared that there was disagreement within the

licensee's organization as to whether or not the reactor had been critical.

The licensee directed that additional engineering review be made.

The

licensee informed the Resident Inspector (RI) of the event on July 3,

1985, and stated that the unit had not gone critical but that there was a

question among the staff and that Reactor Engineering was performing a

technical review.

The licensee stated that they would get back to the

RI when the determination had been made.

The RI informed RIII of his

meeting.

A SRE made the determination on July 4,195 that the reactor had been

critical on July 1, 1985, with a 114 second period and informed his

management of the determination.

Several licensee meetingr. were held on

July 5 and 6, 1985 to discuss this event and to initiate an investigation

into its cause.

The next discussion with the NRC resident staff, af ter July 3,1985,

was on July 15, 1985, when the Senior Resident Inspector (SRI)

was asked by licensee management if he was aware of the July 1, 1985

incident and that the reactor had been critical.

The SRI was aware of

the out-of-sequence rod pull but was not aware that the reactor had

,

been critical.

The SRI informed RIII of the meeting, and the new

information on criticality.

Region !!! Issued a Confirmatory Action Letter (CAL-RI!!-85-10) to the

licensee on July 16, 1985.

The CAL detailed the corrective action

the licensee was to take relating to the out-of-sequence rod pull.

The

CAL is detailed in Inspection Report 50-341/85043(DRP).

The licensee

made a presentation in Region III on July 23, 1985, regarding their

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corrective action program and finu ngs related to the event which is

described in Paragraph 9 of this report.

The licensee's presentation

is included as an attachment to their response to the CAL, Deco letter

RC-LG 85-0017 (Jens to Keppler) dated September 5, 1985.

During the inspection and review of the event, nine examples of apparent

violations of Technical Specification requirements were identified and are

as follows:

Technical Specification 6.8.1.a requires that written procedures shall

be estab11shed, implemented, and maintained covering the applicable

procedure recommendations of Appendix A of Regulatory Guide 1.33,

Revision 2, 1978.

Appendix A of Regulatory Guide 1.33 lists the

following activities under Administrative procedures:

i

5

_ _ _ _ _ _ _ _ _

.

.

.

Hot Standby to Minimum Load (Nuclear Startup)

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Authorities and Responsibilities for Safe Operation...

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Equipment Control

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Shift and Relief Turnovers

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Log Entries

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Contrary to the above, the licensee failed to adhere to the provisions of

Technical Specification 6.8.1.a covering the startup of the reactor on

July 1, 1985, as indicated below:

a.

P0M Procedure 51.000.08, " Control Rod Sequence and Movement

Control," paragraph 3.1.1, requires that rod withdrawals in the

region from 100% Rod Density to 20% Reactor Power must be

performed according to the rod pull sheet. The rod pull sheets

in effect on July 1,1985, required the rods for Group 3 to be

pulled in notch control (00-04, 04-08, etc.). The licensee

pulle<* :leven control rods in Group 3 to the full out position

(48) rather than to the 04 position as required (341/85040-01a).

b.

POM Procedure 51.000.08 Paragraph 3.1.4 states, in part, "Following

each rod move the Nuclear Supervising Operator (NS0) shall verify

the control rod was lef t in the proper position indicated and shall

document this verification by initialing the ' Final Position

Verified' block of Attachment 1."

The NSO verified eleven rods to

-

be at position 04, by initialinj the pull sheet, when in actuality

they were at position 48(341/85040-01b).

c.

POM Procedures 12.000.57, " Nuclear Production Organization" and

21.000.01, "Shif t Operation and Control Room" delineate the

responsibilittee of the NSS to include supervision of all

activities and observation and/or direction of major plant

evolutions to ensure compliance with Technical Specificatiens,

procedures, and regulations.

The NSS did not appropriately

discharge his duties on July 1 and 2,1985, in that Me neither

supervised, observed, nor directed the activities essociated

,

,

,

with the control rod pulls (a major plant evaluation) nor was

he in the proximity of the appropriate control panel and

associated nuclear instrumentation (341/85040-01c).

d.

POM Procedur 21.000.01, Enclosure 1

Item 12, requires the Nuclear

Assistant Shif t Supervisor (NASS) to provide direct supervision of

shift personnel. The NASS did not provide direct supervision of the

NSP manipulating the controls on July 1 and 2,1985 nor was he in

the proximity of the appropriate control panel and associated

nuclear instrumentation (341/85040 01d).

'

e.

P0H Procedure 21.000.01, Enclosure 2, Item 5 requires the NSO

to be responsible for the plant's main control room operation.

The control room NSO was unaware of the out-of-sequence rod

pull and thus was not successfully discharging his duties

(341/85040-01e).

.

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. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _

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f.

POM Procedure 21.000.01, Enclosure 6, Item 2, requires the Shift

Operations Advisor (SOA) observe actuation of annunciators to ensure

that they are being promptly and properly addressed with actions

taken. Five short period alarms were received in less than four

minutes while pulling rod 18-51 on July 1, 1985. The NSO at the

controls was allowed to continue pulling rods and the SOA did not

discharge his responsibilities by failing to become involved in the

resolution of the short period alarms (341/85040-01f).

g.

P0M Procedure 21.000.02, " Operating Logs and Records," Section

4.2.5.8, requires the NSS to record the occurrence of significant

events in the NSS log. The NSS log for July 1 and 2,1985,

contained no entries for the out-of-sequence rod pulls, a

significant event, which occurred between 11:40 and 11:59 p.m.

on July 1,1985(341/85040-01g).

h.

POM Procedure 21.000.01, " Shift Operation and Control Room," Section

6.3.8 states, " Reactor Engineering Administrative Procedure No.

51.000.10, ' Reactor Engineering Conduct of Operations,' details the

duties and responsibilities of on-shif t Reactor Engineering personnel."

Procedure 51.000.10 Section 1.0, states, "The purpose of this

procedure is to outline operational interfaces between Reactor

Engineering and Plant Operations and to clarify the overall responsi-

bilities of on-shif t Reactor Engineering personnel." Procedure 51.000.10

does not detail the duties and responsibilities of the on-shift

Reactor Engineer (341/85040-01h).

1.

POM Procedure 21.000.01, Section 6.8 addresses shift relief and

Section 6.8.4 specifically addresses the control room nuclear

supervisingoperator(NS0). The procedure defines the required

turnover for the NSO in charge of the control room but does not

define any turnuver requirements for the NSO assigned to duties in

the control room but not in charge of the control room (341/85040-011).

3.

Control Room HVAC

On July 11, 1985 PN-21 No. 286934 was issued to inspect the Division !!

Control Room HVAC condensate tray.

For personnel protection the Division !!

Control Room HVAC supply fan control switch was placed in the off position

at 8:35 a.m. on July 18, 1985 and the feeder break was opened and red

tagged at 8:50 a.m.

The Nuclear Supervising Operator (NS0) entered the

action in his log but did not list the Technical Specification appitcability.

The NSO also entered the action in the Control Room Information System

(CRIS) equipment status file and placed the applicable CRIS dot next to

the switch on the sanel. The NSO also advised the protection leader that

protection had to )e removed by 3:00 ).m. on July 25, 1985, however, the

NSO failed to notify the NSS of the c1ange in equipment status. Neither

the NSS log nor the out-of-specification log contain any entries on the

inoperable Division !! HVAC. The work was completed and the request to

7

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_ _ _ _ - _ _ _ _ _

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removeprotectionwasmadeat1:20g.m.onJuly 18, 1985. However, the

package was misfiled in the " active file rather thar, the " protection to

be cleared" file.

The out-of-specification condition went unnoticed for 27 shift turnovers

by the oncoming NSS, NASS, and NS0's even though the switch was marked,

a log entry had been made, and it was entered in the CRIS equipment

status file.

It was not until July 27, 1985 that a nightshift NSS

questioned the status of the Division II Control Room HVAC fan and

had the fan returned to service at 5:38 a.m. on July 27, 1985.

During the inspection and review of the event, two apparent violations

of Technical Specification requirements were identified as follows:

l

a.

Technical Specification 3.7.2.C.1 requires that with the control

center emergency filtration system supply fan inoperable, with the

plant in cold shutdown, the fan be made operable in seven days or

initiate and maintain operation of the system in the recirculation

mode of operation.

Centrary to the above, the licensee failed to place the control

room emergency filtration system in the recirculation mode of

l

operation on July 25, 1985; seven days after the system was

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rendered inoperable on July 18, 1985. This condition existed

l

for aroroximately forty-five (45) hours (341/85040-02).

b.

Technicsl Specification 6.8.1.a requires that written prac#dures

shall be established, implemented, and maintained covering the

l

applicable procedure reconinendations of Appendix A of Regulatory

'

Guide 1.33 Revision 2, 1978. Appendix A of Regulatory Guide 1.33

lists the following activities under Administrative Procedures:

Authorities and Responsibilities for Safe Operation...

-

Equipnent Control

-

Shif t and helief Turnovers

!

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Log Entries...

-

Contrary to the above, the licensee failed to adhere to the

provisions of Technical Specification 6.8.1.a as follows:

(1) POM Procedure 21.000.01 "Shif t Operations and Control Room,"

delineates the shift turnover responsibilities of the Nuclear

Shif t Supervisor (NSS) the Nuclear Assistant Shift Supervisor

(NAJS) and the Nuclear Station Operator (NS0).

Included in the

responsibilities is a review of past log entries, and a review

of each Combination Operating Panel for off-normal conditions

or the addition of CRIS " dots." The NSS NASS, and NSO all

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failed to adequately perform the required activities as

indicatedbelow(341/85040-03a):

8

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(a) The Control Center Division II HVAC supply fan switch was

placed in the off position on July 18, 1985, and not

observed to be out of position until July 27, 1985. The

out-of-specification switch position went unobserved for

27 shift turnovers.

(b) The NSO entered the switch position in the equipment

status file and placed a CRIS " dot" by the switch on

July 18, 1985. The CRIS " dot" went unobserved for

27 shift turnovers.

(c) The NS0 had logged placing the Division II Control

Center HVAC supply fan in the off position at 8:35 a.m.

on July 18, 1985. Subsequent reviews of the log either

failed to note the entry or failed to recognize its

significance.

(6 NSS turnovers, 15 NASS turnovers,

and 27 NSO turnovers)

(2) P0H Procedure 21.000.01, Section 6.19.1.1 states, in part.

" Evaluate the consequences of removing the system or component

from service considering such items as Technical Specifications

L.initing Condition for Operations which require an action

!

statement to be carried out...."

The licensee failed to

I

evaluate the consequences of removing cornponents from service

in that no acknowledgernent of any Technical Specification

applicability was made in either the NSO log of the Control

Room Information System (CRIS) when the Division !! Control

Center HVAC was removed from service (341/85040-03b).

l

4.

RCIC/ Core Spray Room Cooler

The NSS observed whilt. reviewing the combination o)erating panels during

his turnover on July 24, 1985, at 6:30 p.m. that tie control switch for

the Division ! Reactor Core Injection Cooling (RCIC)/ Core Spray Room

Cooler was in the off-reset position, this made both RCIC and Division !

I

core spray inoperable. The NSS who discovered the out-of-position switch

stated that it was in the proper position at 3:30 p.m. on July 23, 1985.

The Itcensee also determined that the Motor Control Center (MCC-728-3A

Position 20) feeding the room cooler was found in the off position.

Subsequent investigation by the licensee did not reveal any reason for

the coolers status nor could any PN-215 be identified which would have

authorized de-energizing the MCC feeder breaker. The room cooler was

returned to service and the licensee documented the incident in

DER NP-85-0390.

Theunitwasinthestartupmodeofoperation(OperationalCondition2)

at the time the room cooler was taken out of service, but was in a

planned shutdown due to the loss of the South Reactor Feed Pump when

the cooler was found out of service.

(Reactorpressurehadbeenreduced

to less than 150 psig at 7:30 a.m. on July 24,1985.) RCIC is not

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required to be operational below 150 psig; however, the High Pressure

CoreInjection(HPCI)hadbeeninoperablesinceJuly 11, 1985 thus for

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approximately sixteen (16) hours the HPCI, RCIC and Division I core

spray systems were all inoperable.

i

i

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During the inspection and review of the event, two apparent violations

l

of Technical Specification requirements were identified as follows:

!

a.

Technical Specification 3.5.1.C.1 requires that during the startup

l

!

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modeofoperation,theHighPressureCoreInjection(HPCI) system

may be inoperable provided that the Core Spray (CS) system, the

Low Pressure Coolant Injection (LPCI) system, the Automatic

Depressurization System (ADS), and the Reactor Core Isolation

Cooling (RCIC)systemareoperable.

Contrary to the above, the licensee failed to ensure that the

RCIC and Division ! core spray systems were operable when they

allowed the RCIC/CS room cooler to be removed from service at

j

3:30 p.m. on July 23, 1985 with the HPCI system already inoperable

as of 3:00 a.m. on July 11, 1985. This condition existed for

approximately sixteen hours, with the reactor in the Startup

condition (341/85040-04).

b.

Technical Specification 6.8.1.a requires that written procedures

shall be established, implemented, and maintained covering the

applicable procedure recomendations of Appendix A of Regulatory

Guide 1.33 Revision 2, 1978. Appendix A of Regulatory Guide 1.33

lists the following activities under Administrative Procedures:

Authorities and Responsibilities for Safe Operation...

-

Equipment Control

l

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Shift and Reitef Turnovers

l

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(

Log Entries...

-

Contrary to the above the licensee failed to ad (n to the

provisions of Technical Specification 6.8.1.a as voilows:

!

(1) POM Procedure 12.000.15"PN-21jWorkOrder) Processing,"

Section 7.2.1 states, in part, All work activities at

Fermi 2...sha11 be controlled by a PN-21 and Attachmeet 'A'

,

to the PN-21." The licensee failed to write a PN-21 to

,

de-energize the feeder breaker (NCC-728-3A Position 20) for

the RCIC/ Core Spray room cooler fan on July 23 and 24,1965

(341/8504005a).

(2) POM Procedure 21.000.01, " Shift Operations and Control Room "

,

l

delineates the shif t turnover responsibilities of the Nuclear

Shif t Supervisor (NSS) the Nuclear Assistant Shif t Supervisor

l

(NASS) and the Nuclear Station Operator (NS0).

Included in the

responsibilities is a review of past log entries, and a review

'

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O

of each Combination Operating Panel for off-normal conditions

or the addition of CRIS " dots." The NSS, NASS, and NSO all

failed to adequately perform the required activities as the

RCIC/ Core Spray room cooler fan switch was in the "off-reset"

l

position for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> on July 23 and 24,1985. The

'

normal position for the switch is in the " Auto" position. The

out of position switch went unobserved for two shift turnovers

(341/85040-05b).

(3) P0M Procedure 21.000.01, Section 6.19.1.1 states, in part.

l

" Evaluate the consequences of removing the system or component

from service considering such items as Technical Specifications

Limiting Condition for Operations which require an action

'

statement to be carried out...."

The licensee failed to

evaluate the consequences of removing components from service

!

as he did not take into account the existing inoperability of

the HPCI system prior to removing the RCIC/ Core Spray room

l

l

cooler from service nor was the action entered into the NSO

log or the CRIS equipment status file (341/85040-05c).

5.

Cooling Tower Bypass Valve

On July 26, 1985, while performing surveillance testing on Division I,

l

Emergency Diesel Generator (EDG) #11, a Diesel Generator Service Water

l

(DGSW) Low Flow Alarm was received. The alarm indicated a lack of

cooling water for the EDG. The operator verified the low flow and

l

innediately shutdown the EOG. The licensee, upon further investigatibn.

determined that the mechanical draft cooling tower bypass valve

E1150-F603A was closed and de-energized. This valve is required by a

condition of the license to be open and de-energized, or one of the

cooling tower shutoff valves E1150 F604A/F605A is to be open and

de-energized to prevent spurious closure due to hot shorts in the event

of a fire in the plant. The nomal position for this motor operated

va'te is de-energized and open per POM Procedure 23.208, Revision 8.

Thi . is an apparent violation of License Condition 2.C.(9)(d) (341/85010-06).

Invtstigation into the rcason why the bypass valve was out of proper

position, identified that the valve was last manipulated on July 23,

1985, while running the Reactor Heat Removal Service Water (RHR$W)

system. The valve had exhibited a tendency to trip either the thermal

overloads or the torque switches during stroking and an operator had been

required to partially stroke the valve to the desired position as well as

reset the thermal overloads to allow continued stroking from the control

room.

It appears that clear instructions were not given to the Reactor

Building Rounds Operator as he was not aware of the necessity of leaving

the Ell 50 F603A valve in the open de energized condition.

The E1.50 F603A valve is located in the discharge flow path to the

coolin$ water reservoir and its closure affects multiple systems. With

the valve closed, flow of Erwrgency Equipment Service Water (EESW),

11

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RHR$W, and DGSW is blocked. Besides affecting the Division I EDG's,

.

with the bypass valve closed all Division I emergency core cooling

systems were inoperable including the core spray and residual heat

removal systems.

At the time the bypass valve was discovered in the closed position, the

reactor was in cold shutdown, Condition 4, with the reactor temperature

at approximately 130*F and atmospheric pressure.

In cold shutdown the

plant is required to have one operable division of ECCS, and one operable

divisionofEDG's(twodiesels). This condition was satisfied, however,

the bypass valve E1150-F603A had been closed since about 1:19 p.m. on

July 23, 1985. On July 23, 1985, theunitwasinCondition2(Startup)

which requires both divisions of ECCS and both divisions of the onsite

electrical power source (EDG's) to be operable. As a result of the

bypass valve being closed, only one division was operable. The failure

to take remedial action with one division of the EDG's inoperable is

an apparent violation of T.S. 3.8.1.1.b (341/85040-07).

On July 23, 1985, the licensee connenced a reactor shutdown at about

1:15 p.m. as a result cf the failure of the South Reactor Feed Pums.

It was fortuitous that the licensee coemenced a recctor shutdown a>out

the same time the cooling tower bypass valve was de-energized in 'le

closed position, as the licensee was by chance co.. plying with the

Limiting Condition for Operation (LCO) action statements in reducing

power and proceeding to cold shutdown. Without this action, the plant

would have been in further violation of technical specifications.

6.

Hydrogen Recombiner

On June 20, 1985, the licensee completed maintenance on the Division !!

hydrogen recombiner per Work Order PN-21269327 to replace a leaking

blower seal. The work order stated that post maintenance testing was

required, and identified Plant Operations Manual (POM) Procedures

43.409.01, " Post LOCA Thermal Recombiner System Test," and 24.409.01

" Post LOCA Thermal Recombiner Functional Test." These procedures were

required to demonstrate leak tight integrity and operability,

respectively. The work order was stoned off as completed by the Nuclear

Shif t Supervisor on June 20,1985, w' thout the leakage test having been

perforned per P0M Procedure 43.409.01. This is an apparent violation of

TechnicalSpecifications(T.S.)6.8.1.aand6.8.4.ainthatthelicensee

failed to follow estabitshed procedures and comply with the leakage

reduction program (341/85040 08).

i

On August 26 1985, the licensee initiated a Deviation / Event Report

LNo. I'P-85-0I55) to document the failure to perform the post maintenance

leak rate testing on the Olvision !! hydrogen recombiner. After

the licensee had sufficient

determining the failure to wrfom testing}ner inoperable, as a result

infomation to declare the aydrogen recomb

j

of exceeding the 30 day LCO limit, and the licensee did not take action

per technical specification 3.0.3. to place the unit in hot shutdown

,

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_ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ .

_ _ _ _ _ _ . _

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l

within six hours. The licensee proceeded to determine the leakage rate

and on August 28, 1985, declared the Division II hydrogen recombiner

innperable as a result of the initial leakage rate testing. Subsequently

on August 29, 1985, at 2:46 p.m. the licensee determined that the leakage

rate was in excess of the allowable containment leakage. This is an

apparent violation of T.S. 3.6.6.1, and 3.0.3 in that the licensee failed

to comply with the LCO action statements (341/85040-09).

At 6:00 p.m., on August 29, 1985, the licensee cummenced preparations

to proceed to hot shutdown. The hydrcgen recombiner was repaired, leak

tested, and declared operable on August 29, 1985, at 9:00 p.m.

The plant

was returned to the startup mode with pressure at 950 psig and 3.8% power

for HPCI and SCRAM time testing at 10:40 p.m.

,

During the time period from June 21 to July 21, 1985, the plant entered

l

Operational condition (Startup) on five (5) occasions including initial

criticality (June 21, 1985, June 29, 1985, July 2, 1985, July 6, 1985,

and July 10,1985) without both divisions of hydrogen recombiners

,

l

operable. This is an apparent violation of T.S. 3.0.4(341/85040-10).

7.

Breach of Primary Containment Integrity

l

ThelicenseediscoveredaContainmentMonitoringSystemValve(T50-071A)

!

which is a primary containment boundary, in the open position and uncapped

I

on September 2, 1985. The valve was shut upon discovery. The Nuclear

l

Shif t Supervisor (NSS) was informed of the event on September 4,1985,

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approximately 39 hours4.513889e-4 days <br />0.0108 hours <br />6.448413e-5 weeks <br />1.48395e-5 months <br /> af ter discovery. ADeviation/EventReport(DER)

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(No.NP-85-0469) was written to document the open valve.

Valve T50-071A was installed under Engineering Design Package (EDP)

No. 1970 dated March 25, 1985. The EDP included the installation of four

test connection cutoff valves in the primary containment monitoring

system. Valves T50-068A and B were installed in piping from the bottom

of the torus while valves T50-071A and B were installed in piping from

the top of the torus. PN-21(WorkOrder)No. 814949 was written to

install the "A" valves in Division I and PN-21 No. 814948 was written to

install the "8" valves in Olvision !!. Both PN-21s were signed off as

" Order Completed" on June 20, 1985.

It should be noted that neither EDP

1970 nor the four PN-21s associated with it were closed out as of

September 10, 1985.

Doth PN-21s for the primary containment monitoring system required Local

Leak Rate Tests (LLRTs) plus Plant Operations Manual Procedure

24.000.05, " Monthly Continuity Light and Channel Check Test," Section 4

" Precautions and Limitations" to be completed. The NSS signed the

PN-21s as order complete on June 20, 1985. The licensee reviewed EDP

1970 and detemined that the LLRTs for the primary containment monitoring

system modifications had not been performed. DER No. NP-85-471 dated

September 5, 1985, was written to document this discrepancy. The licensee

subsequently performed the missed LLRTs and three of the four LLRTs met

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procedural criteria. The LLRT for Penetration.X203A.(P0M Procedure

43.401.386) which contains valve T50-071A did not meet the leakage

criteria. Two of the three boundary valves were repaired and the

penetration subsequently met the test criteria,

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During the inspection and review of the event, three apparent violations

were identified as follows:

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a.

Technical Specification 3.6.1.1 requires that PRIMARY CONTAINMENT

INTEGRITY shall be maintained in Operational Conditions 1, 2,-and 3.

Without PRIMARY CONTAINMENT INTEGRITY restore PRIMARY CONTAINMENT.

e

INTEGRITY within one hour or be in at least HOT SHUTDOWN within the

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next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in COLD SHUTDOWN within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

,

Contrary to the above, the licensee failed to maintain containment

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integrity from June 21 to September 2,1985, in that primary

containmentmonitoringsystemvalve(T50-F071-A)wasintheopen

position and the line downstream of the' valve was uncapped which

resulted in an open pathway from the primary containment to the.

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reactor building. Primary containment integrity was required during

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this time frame except for 6.25 days of the interval-(341/85040-11).

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b.

Technical Specification 6.8.1.a requires that written procedures

shall be established, implemented, and maintained covering the-

applicable procedure recommendations of Appendix A of-Regulatory-

.

Guide 1.33 Revision 2, 1978. Appendix- A of Regulatory Guide'1.33.

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lists the following activities under Administrative Procedures:

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(1) Equipment Control

(2) Log Entries...

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Contrary to the above, the licensee failed to adhere to the

provisions of Technical Specification 6.8.1.a as follows:

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P0M Procedure 12.000.15, "PN-21 (Work Order) Processing," Revision 11,

August 20, 1985, paragraph 7.3.16 states:

"Upon completion of all-

maintenance, testing, STR or EPC and after_the ' Accepted for Service-

By' slot has been signed, the pink copy-of PN-21 is forwarded to the

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Nuclear Shift Supervisor who will review the order and sign ' Order

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Completed.'" Contrary to the above, the licensee failed to adhere -

to the requirements of POM Procedure 12.000.15. in that Work Order-

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PN-21 No. 814945 (covering the addition of leak rate test conriection.

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valve T50-F071A) was signed " order completed" on June 20, 1985,

without the post installation leak rate testing being performed as.

specified.onthework-order-(341/85040-12)..

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. c.

10 CFR 50, Appendix B, Criterion VI,; states, in part,a" Measure. shall:

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be established to control the issuance of documents, such as

instructions, procedures,'and drawings,. including changes'thereto,

which prescribe all activities affecting quality. These measures

shall assure that documents including changes are reviewed for

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adequacy...."

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POM Procedure' 12.000.64, "EDP1 Implementation Procedure,": Revision 2,

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dated March 5, 1985, Section 6.5.1; states, in part, "The responsible

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PSE shall identify the plant documents requiring revision when the -

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package is prepared."

Contrary to the above, the EDP. Implementation Procedure for EDP'

No.1970, covering.the installation of the containment sample system .

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leak rate test connection valve T50-f CIA, did not. identify.all

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the plant documents requiring revision in that it did not identify.

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POM Procedures 24.425.01, " Primary Containment Integrity

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Verification for Valves Outside Containment," or 47.000.77, " Test

Vent and Drain (TVD) Cap:and Plug Verification." The failure to

identify these documents resulted in valve T50-F071A (an_d seven-.

,

other valves) not being incorporated into the procedures used to

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verify containment integrity (341/85040-13).

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8. 'Sumary

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3

Twenty-six -violations (including multiple examples) of NRC requirements

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are identified in this report. The majority of these fall into the

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category of failure to follow procedures._ This represents a-breakdown

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in the licensee's ability to operate the plant in accordance with.

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prescribed procedures as required by the Technical Specifications.

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The licensee's Operational Assurance (0A) organization has a program

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called. Procedure Compliance Module (PCM) which monitors, on a monthly :

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bases, procedural compliance by various organizations. The results'of

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six monthly surveillances (January-June 1985) clearly' revealed that the

operations section had had problems in following procedures. (Procedural

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compliance ran from 74% to 100% and there was no trend--the results were

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erratic. The six-month average was 87% with 99% compliance as a goal.

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It should be noted that the findings of-the PCM program are not absolute

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but are excellent indicators of potential-problem areas. The'results,

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both current and cumulative, are issued monthly. Theslicensee had

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sufficient knowledge of procedural compliance problems to initiate

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corrective actions rather than wait for a larger' data base.

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Seven of the violations were failures to meet Technical Specification

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LimitingConditionforOperations(LC0's).1 Each of these were serious and

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collectively represented a breakdown in the licensee's administrative and

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management controls design to safely operate the plant. The safety;

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significance!of the violations was. mitigated considerably by two' items-

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the plant had only operated for 20 days at an average power of,2 percent;

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and the failure of the South Reactor Feed Pump turbine which resulted in-

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the licensee shutting the reactor down. The inspectors consider the

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second item to be fortuitous.in-that the: reactor was removed from an

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operating condition which required certain equipment to be operable or

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ractions to'be taken when the licensee wasLunaware that the actions or..

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equipment were. required..

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Twenty-six violations, many of them repetitive, have been identified-

in this. report.- Operating history mitigated their safety significance;

however, they demonstrated a major breakdown in the licensee's

administrative controls to safely operate the plant.

9.

Management Meetings

a.

OutJof-Sequence Rod Pull

DECO management.(denoted in Paragraph 1) met with RIII management.

in' Glen Ellyn, Illinois,-on July 23, 1985', to' discuss the sequence of

events surrounding the out-of-sequence rod pull which occurred on

July 1 and 2,.1985, and their subsequent actions. This meeting was,

attended by the public.

The . licensee's presentation included a' detailed sequence.'of events

imediately preceding and following the event, the rod pull _ sheets,

and the Source Range Monitor (SRM) strip chart which. corresponded to-

the time of the incident. .The licensee also presented a layout of

the control room and the relative location in the control room of

those on shift at the time of the event. A great deal of discussion

was focused on the events and licensee' actions subsequent.to the

incident. The adequacy of the onshift review was discussed; RIII's

position was that the onshift review was insufficient. Considerable

discussion was focused around the adequacy, completeness, and

timeliness of the reporting of the incident to the NRC. The

licensee did not consider the event to he reportable under 10 CFRs

50.72 or 50.73. Region III concurred that the incident was.not

reportable under 10 CFR 50.72 or 50.73, but given;the proximity of

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the Comission's full-power briefing, Deco should have been more-

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sensitive to the importance of keeping.the NRC informed.- The

Regional Administrator informed the licensee that he had requested

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the Office of Investigations (OI) to. investigate the event.

The licensee also discussed their actions pertaining to whether or

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not the unit had been critical, as a ' result of the out-of-sequence .

rod pull, and their corrective action. program. The licensee was

informed that Region III would send an inspection team to Femi.2 -

to assess control room operations and the effectiveness of. the -

corrective action program.

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The licensee's presentation is included as-an-attachment to DECO

letter No. RC-LG-85-0017~ (Jens to Keppler) dated September 5, .1985.

b.

Corrective Action Program

DECO management (denoted in Paragraph 1) net with Region III-

management in Glen Ellyn,' Illinois, on September 10, 1985, to discuss

their corrective action program to preclude the repetition of the ~

events which were reported to the NRC during July and. August 1985'and

documented elsewhere in this report. -The meeting was attended by

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representatives of the. Monroe County. Government and the public.

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The licensee proposed a corrective action program based on

observations and recommendations made by the Institute of Nuclear

Power Operations (INP0) assistance inspection team, findings of two

recent NRC team inspections, conditions of the Confimatory Action

Letter (CAL-RIII-85-10) dated July 16, 1985, findings by the

resident NRC inspectors, and recommendations made by Management

AnalysisCorporation(MAC). The program was divided into short

and long term actions. Short term actions were to be completed

prior to power escalation above five percent. Long term actions

addressed programmatic areas with the licensee indicating a phased

implementation to minimize pertubations to plant operations.

Long term actions were to be initiated prior to exceeding five

percent power but not to be completed until some later date with

the longest date of December 1, 1986.

Deco requested that the five percent power restriction be lifted but

that they would commit to not exceeding twenty percent power until

after the forthcoming outage which is scheduled to start during

October 1985. The request was denied.

Region III requested that the licensee docket the corrective action

program which had been presented and include methods of monitoring

the effectiveness of the corrective actions. The licensee

subsequently submitted their " Reactor Operations Improvement

Plan" in a letter from Jens to Keppler (DECO No. VP-85-0198)

dated October 10, 1985 (copy attached).

The licensee was also informed that another inspection team would

be sent to Femi 2 to observe operations and review the corrective

action program and its effectiveness before .the five percent

restriction could be lifted. This action was predicated upon

a satisfactory resolution of the 01 investigation.

10. Enforcement Conference

The NRC staff met with licensee representatives (denoted in Paragraph 1)

during the management meetings and at various times during the inspection

and reviewed the issues discussed in this report.

The staff also discussed the likely informational content of the

inspection report with regard to documents or processes review by the

inspectors during the inspection. The licensee did not identify any

such documents / processes as proprietary.

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