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    NN s ..                     >-    .                                       ~ APPENDIX                                   ..
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                                                          -
.
                                                              U.S. NUCLEAR REGULATORY COMMISSION
-
      71                         ,
v
                                    ,
.
                                                                                REGION IV
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                                                '
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                '
~ APPENDIX
                            sNRC Insp'ection Report:             50-458/86-14                 License /CP: NPF-47
>-
                              Do'cket: .;501458
..
      '                '
U.S. NUCLEAR REGULATORY COMMISSION
                              Licensee:               Gulf States Utilities Company (GSU)
'
                  i
-
                                                      P. O. Box 2951
~
                                                      Beaumont, Texas       77704
71
                              Facility Name: River Bend Station (RBS)
REGION IV
                              Inspection At: River Bend Station, St. Francisville, Louisiana
,
                            . Inspection' Conducted: March 17-20, 1986
,
                          .
^
                              Inspector:             4             .        w   t   t                     3-25 8(3
+
                                                    . D. Du Chamberlain, Ser.ior Resident Inspector           Date
.
                                                    -(pars. 1, 2, and 3)
I
                                                                                        /
'
                              Approved:
sNRC Insp'ection Report:
                                                                uoon
50-458/86-14
                                                                        41 6         M
License /CP:
                                                                        hief, Pr& Ject Section A,
NPF-47
                                                                                                              3 27 b
'
                                                                                                              Date
Do'cket: .;501458
                                                                                                                  '
Licensee:
  '
Gulf States Utilities Company (GSU)
                                                          ac rP         ects Branch
'
                              Inspection Summary
'
                              Inspection Conducted March 17-20, 1986 (Report 50-458/86-14)
i
                    '
P. O. Box 2951
                            Areas Inspected: This inspection was a special, unannounced inspection
Beaumont, Texas
                            . conducted to review the conditions and actions which led to a Division II
77704
                            diesel generator operability failure on March 17, 1986, and to review the
Facility Name: River Bend Station (RBS)
Inspection At: River Bend Station, St. Francisville, Louisiana
. Inspection' Conducted: March 17-20, 1986
.
3-25 8(3
Inspector:
4
w
t
t
.
. D. Du Chamberlain, Ser.ior Resident Inspector
Date
-(pars. 1, 2, and 3)
/
Approved:
41 6
M
3 27
b
uoon
hief, Pr& Ject Section A,
Date
'
'
ac rP
ects Branch
Inspection Summary
Inspection Conducted March 17-20, 1986 (Report 50-458/86-14)
Areas Inspected: This inspection was a special, unannounced inspection
. conducted to review the conditions and actions which led to a Division II
'
diesel generator operability failure on March 17, 1986, and to review the
planned corrective actions.
;
;
                              planned corrective actions.
Results: Within the areas inspected, three violations were identified
                              Results: Within the areas inspected, three violations were identified
-(inadequate corrective action, failure to perform maintenance in accordance
                            -(inadequate corrective action, failure to perform maintenance in accordance
with procedures and inoperable Division !! diesel generator, paragraph 2).
                            with procedures and inoperable Division !! diesel generator, paragraph 2).
_
    _                                                                                                                             ,
,
1
1
:                                           O
:
O
,
,
I
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                      -
-
                                                                                                                          ,
,


    .
.
  .
.
                                            -2-
-2-
                                          DETAILS
DETAILS
    1. Persons Contacted
1.
        Principal Licensee Employee
Persons Contacted
      *R. E. Bailey, Supervisor, Quality Control (QC)
Principal Licensee Employee
      *W. H. Cahill, Jr., Senior Vice President, River Bend Nuclear Group
*R. E. Bailey, Supervisor, Quality Control (QC)
      *E. M. Cargill, Supervisor, Radiation Programs
*W. H. Cahill, Jr., Senior Vice President, River Bend Nuclear Group
      *T. C. Crouse, Manager, Quality Assurance (QA)
*E. M. Cargill, Supervisor, Radiation Programs
      *J. C. Deddens, Vice President, River Bend Nuclear Group
*T. C. Crouse, Manager, Quality Assurance (QA)
      *D. C. Davenport, Supervisor, Security
*J. C. Deddens, Vice President, River Bend Nuclear Group
      *J. W. Evans, Stenographer, GSU
*D. C. Davenport, Supervisor, Security
      *D. R. Gipson, Assistant Plant Manager, Operations
*J. W. Evans, Stenographer, GSU
      *E. R. Grant, Supervisor, Nuclear Licensing
*D. R. Gipson, Assistant Plant Manager, Operations
      *R. Helmick, Director of Projects
*E. R. Grant, Supervisor, Nuclear Licensing
      *R. Jackson, Shift Supervisor, Operations
*R. Helmick, Director of Projects
      *R. J. King, Licensing Er.gineer
*R. Jackson, Shift Supervisor, Operations
      *A. D. Kowalczuk, Assistant Plant Manager, Maintenance
*R. J. King, Licensing Er.gineer
        R. Mayeux, Reactor Operator
*A. D. Kowalczuk, Assistant Plant Manager, Maintenance
      *J. H. McQuirter, Licensing Engineer
R. Mayeux, Reactor Operator
      *W. H. Odell, Manager, Administrative
*J. H. McQuirter, Licensing Engineer
      *T. F. Plunkett, Plant Manager
*W. H. Odell, Manager, Administrative
      *S. R. Radebaugh, Assistant Plant Manager, Services
*T. F. Plunkett, Plant Manager
      *D. Reynerson, Director, Nuclear Plant Engineering
*S. R. Radebaugh, Assistant Plant Manager, Services
      *R. R. Smith, Licensing Engineer
*D. Reynerson, Director, Nuclear Plant Engineering
      *P. F. Tomlinson, Director, Quality Services
*R. R. Smith, Licensing Engineer
        D. Williamson, Operations Supervisor
*P. F. Tomlinson, Director, Quality Services
        The NRC senior resident inspector (SRI) also interviewed additional
D. Williamson, Operations Supervisor
        licensee personnel during the inspection period.
The NRC senior resident inspector (SRI) also interviewed additional
      * Denotes those persons that attended the exit interview conducted on
licensee personnel during the inspection period.
        March 20, 1986. NRC resident inspector (RI), W. B. Jones, also attended
* Denotes those persons that attended the exit interview conducted on
        the exit interview.
March 20, 1986. NRC resident inspector (RI), W. B. Jones, also attended
    2. Division II Diesel Generator Operability Failure Review
the exit interview.
        This inspection was conducted by the SRI to review the conditions and
2.
        actions which led to a Division II diesel generator operability failure on
Division II Diesel Generator Operability Failure Review
        March 17, 1986, and to review the planned corrective actions. During
This inspection was conducted by the SRI to review the conditions and
l       performance of Surveillance Test STP-309-0202, " Division II Diesel
actions which led to a Division II diesel generator operability failure on
        Operability Test," on March 17, 1986, the diesel started and came up to
March 17, 1986, and to review the planned corrective actions. During
        speed, frequency, and voltage within the required time, but about one
l
        minute later it began to coast down and stopped because of loss of fuel
performance of Surveillance Test STP-309-0202, " Division II Diesel
Operability Test," on March 17, 1986, the diesel started and came up to
speed, frequency, and voltage within the required time, but about one
minute later it began to coast down and stopped because of loss of fuel
oil flow. River Bend Technical Specifications requires the diesel to
;
;
        oil flow. River Bend Technical Specifications requires the diesel to
operate loaded for at least 60 minutes for demonstration of operability
        operate loaded for at least 60 minutes for demonstration of operability
l
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                                                                                __
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      ,
,
    .
.
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                                            -3-
-3-
        and requires three separate and independent diesel generators (1A,1B, and
and requires three separate and independent diesel generators (1A,1B, and
        IC) to be "0PERABLE" in "0PERATIONAL CONDITIONS 1, 2, and 3." The plant
IC) to be "0PERABLE" in "0PERATIONAL CONDITIONS 1, 2, and 3."
        was in operational Condition 1 on March 17, 1986. The licensee
The plant
        immediately initiated a condition report (86-0311) for investigation,
was in operational Condition 1 on March 17, 1986.
        analysis and corrective action on the ailed operability test.
The licensee
        The SRI review of the licensee's investigation of this incident revealed
immediately initiated a condition report (86-0311) for investigation,
        the following:
analysis and corrective action on the ailed operability test.
        a.   Inadequate Corrective Action: A similar event occurred on February
The SRI review of the licensee's investigation of this incident revealed
              14, 1986, when the Division I diesel generator (1A) failed the
the following:
              surveillance operability test. The condition report (86-0179)
a.
              investigation for this failure revealed that the fuel oil strainer
Inadequate Corrective Action: A similar event occurred on February
              valve handle was missing and that the strainer valve was misaligned
14, 1986, when the Division I diesel generator (1A) failed the
              causing a loss of fuel oil flow to the diesel generator. The Nuclear
surveillance operability test. The condition report (86-0179)
              Plant Engineering (HUPE) documented corrective action on February 15,
investigation for this failure revealed that the fuel oil strainer
              1986, only required that the fuel oil strainer valve be realigned and
valve handle was missing and that the strainer valve was misaligned
              that successful operation of the diesel be demonstrated. No ger.eric
causing a loss of fuel oil flow to the diesel generator. The Nuclear
              action to prevent recurrence was documented, and no remedial or
Plant Engineering (HUPE) documented corrective action on February 15,
              generic corrective action was specified to be implemented by any.
1986, only required that the fuel oil strainer valve be realigned and
              Other section or department. No reason was determined for the
that successful operation of the diesel be demonstrated. No ger.eric
              missing handle or for the misalignment of the fuel strainer. Also,
action to prevent recurrence was documented, and no remedial or
              the investigation did not determine the duration of time that the
generic corrective action was specified to be implemented by any.
              fuel strainer had been misaligned. The analysis and understanding of
Other section or department. No reason was determined for the
              the adverse condition does not appear to have been thorough enough to
missing handle or for the misalignment of the fuel strainer. Also,
              identify and correct the root cause of the problem. This is
the investigation did not determine the duration of time that the
              evidenced by a reoccurrent.e of the fuel strainer misalignment problem
fuel strainer had been misaligned. The analysis and understanding of
              on the Division II diesel generator, which resulted in the Division
the adverse condition does not appear to have been thorough enough to
              II diesel generator operability failure on March 17, 1986. This
identify and correct the root cause of the problem. This is
              inadequate corrective action for the diesel generator operability
evidenced by a reoccurrent.e of the fuel strainer misalignment problem
              failure on February 14, 1986, was identified by the SRI as an
on the Division II diesel generator, which resulted in the Division
              apparent violation (458/8614-01).
II diesel generator operability failure on March 17, 1986. This
        b.   Performance of Maintenance: As a result of the February 14, 1986,
inadequate corrective action for the diesel generator operability
              Division I diesel generator operability failure, the fuel oil
failure on February 14, 1986, was identified by the SRI as an
              strainer valve handle was removed from the Division II diesel and
apparent violation (458/8614-01).
              installed on the Division I diesel. It was also used as a pattern
b.
              for the maintenance shop to fabricate a new handle for the Division
Performance of Maintenance: As a result of the February 14, 1986,
              II diesel.
Division I diesel generator operability failure, the fuel oil
              This new handle was apparently fabricated through use of a shop work
strainer valve handle was removed from the Division II diesel and
              order (SWO), but the maintenance department could not locate the SWO.
installed on the Division I diesel.
              The new handle was installed February 17, 1986, on the Division II
It was also used as a pattern
              diesel generator fuel oil strainer, but no maintenance work request
for the maintenance shop to fabricate a new handle for the Division
              (MWR) was initiated to provide documentation of work performance or
II diesel.
              to provide for retesting as appropriate. A SWO should not be used to
This new handle was apparently fabricated through use of a shop work
              work on permanent plant equipment by licensee procedure. This
order (SWO), but the maintenance department could not locate the SWO.
              failure to initiate a HWR for performance of maintenance on permanent
The new handle was installed February 17, 1986, on the Division II
              plant equipment was identified by the SRI as an apparent violation
diesel generator fuel oil strainer, but no maintenance work request
              (458/8614-02).
(MWR) was initiated to provide documentation of work performance or
to provide for retesting as appropriate. A SWO should not be used to
work on permanent plant equipment by licensee procedure. This
failure to initiate a HWR for performance of maintenance on permanent
plant equipment was identified by the SRI as an apparent violation
(458/8614-02).


                      _----___               -
_----___
                                                                                                                                      .
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                                        c.-           Inoperable Division II Diesel Generator: 'The Division II diesel           '
=.4
                                      ,
.
                                              - generator was proved operable on February 15, 1986, by surveillance
<
e,                                                 ,test, and the new fuel oil strainer valve handle was apparently
J i
.                                                    installed on February 17, 1986. No testing was performed af ter the
*
        >
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              m
,
                  '
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                                                  ' handle was~ installed until the March ~17, 1986, surveillance test,             ,
k h~m ^
        J _                                           which failed because of the' improper alignment of the fuel oil
- generator was proved operable on February 15, 1986, by surveillance
              -
%'
                                                      strainer valve. On March 17, 1986, the valve handle was found to be
~
                                                      improperly posi_tioned on the fuel oil strainer, and the valve was
.
                                                      misaligned, causing a loss of fuel oil flow to the diesel. There was
c.-
                                                      no evidence found of any other maintenance work on the fuel oil
Inoperable Division II Diesel Generator: 'The Division II diesel
                                                      strainer between February 17, 1986, and March 17, 1986. Also, there
*
                                                  ,  was no' evidence ~ found of operational realignment of the fuel oil
'
                                                      strainer.
e,
                                                  - With the_ plant in Operational Condition I on March 17, 1986, the
,
                                                      Division II diesel was discovered to be inoperable during
,tes , and the new fuel oil strainer valve handle was apparently
                                                      surveillance testing. .The diesel had apparently been inoperable for
t
        -
installed on February 17, 1986. No testing was performed af ter the
                                                      an undetermined length of time between February 15, 1986, and March
.
                                                      17, 1986. This failure to have three separate and independent diesel
'
                                                      generators "0PERABLE" in "0PERATIONAL CONDITION 1" was identified by
' handle was~ installed until the March ~17, 1986, surveillance test,
                                                      the SRI as-an apparent Technical Specification violation
>
                                                      (458/8614-03).
m
                                        d.           Licensee Investigation and Corrective Actions
,
                                                      The SRI found that the licensee was continuing his investigation of
J _
                                                      this occurrence, and the following corrective actions were being
which failed because of the' improper alignment of the fuel oil
                                                      implemented:
strainer valve. On March 17, 1986, the valve handle was found to be
                                                      .      .The licensee has scribed all three diesel generator fuel oil
-
                                                              strainer valves so that proper valve positioning is identified
improperly posi_tioned on the fuel oil strainer, and the valve was
                                                              with or without the handle being installed. Diesel operabi.11ty
misaligned, causing a loss of fuel oil flow to the diesel. There was
                                                              has been verified for three diesels.
no evidence found of any other maintenance work on the fuel oil
                                                      .      Maintenance personnel have been instructed on the proper
strainer between February 17, 1986, and March 17, 1986. Also, there
                                                              alignment of the fuel oil strainer handle and valve.
was no' evidence ~ found of operational realignment of the fuel oil
                                                      .      The plant operators are verifying proper position of the fuel oil
, strainer.
                                                              strainers during normal rounds (at least once per shift).
- With the_ plant in Operational Condition I on March 17, 1986, the
                                                      .      The plant manager has added a compliance inspector analyst to
Division II diesel was discovered to be inoperable during
                                                              his staff to assure procedure adherence for conduct of
surveillance testing. .The diesel had apparently been inoperable for
                                                              maintenance.   This person is charged with the responsibility
an undetermined length of time between February 15, 1986, and March
                                          ,
-
                                                              for. compliance to procedures within the maintenance department.
17, 1986. This failure to have three separate and independent diesel
                                        .
generators "0PERABLE" in "0PERATIONAL CONDITION 1" was identified by
                                                      .      The use of shop work orders has been eliminated.
the SRI as-an apparent Technical Specification violation
i
(458/8614-03).
            :
d.
                                        The SRI will c.ontinue to nonitor licensee actions in this area.
Licensee Investigation and Corrective Actions
                                                    .
The SRI found that the licensee was continuing his investigation of
      s
this occurrence, and the following corrective actions were being
                                  -
implemented:
    ,
.The licensee has scribed all three diesel generator fuel oil
                ,
.
                                          0
strainer valves so that proper valve positioning is identified
    3
with or without the handle being installed. Diesel operabi.11ty
                                                                4
has been verified for three diesels.
Maintenance personnel have been instructed on the proper
.
alignment of the fuel oil strainer handle and valve.
The plant operators are verifying proper position of the fuel oil
.
strainers during normal rounds (at least once per shift).
The plant manager has added a compliance inspector analyst to
.
his staff to assure procedure adherence for conduct of
maintenance.
This person is charged with the responsibility
for. compliance to procedures within the maintenance department.
,
.
The use of shop work orders has been eliminated.
.
i
:
The SRI will c.ontinue to nonitor licensee actions in this area.
.
s
-
,
,
0
3
4


    . __.           .       _ _ _   _ _ _ _ _ _ _ _ _ - _ _ . _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ - _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
. __.
                                                                                                                                                              . _ _ _ _ _ _ _ - __ _ ,
.
            ..
_ _ _
          ..
_ _ _ _ _ _ _ _ _ - _ _ .
                                  .
_ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ - _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                                                -5-
. _ _ _ _ _ _ _ - __ _ ,
              3. Exit and Inspection Interviews
..
                An exit interview was conducted on March 20, 1986, with licensee
..
.
-5-
3.
Exit and Inspection Interviews
An exit interview was conducted on March 20, 1986, with licensee
representatives (identified in paragraph 1). During this interview, the
,
,
                representatives (identified in paragraph 1). During this interview, the
SRI reviewed the scope and findings of the inspection,
'
'
                SRI reviewed the scope and findings of the inspection,
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Latest revision as of 20:52, 24 May 2025

Insp Rept 50-458/86-14 on 860317-20.Violations Noted: Inadequate Corrective Action,Failure to Perform Maint Per Procedures & Inoperable Div II Diesel Generator
ML20140H699
Person / Time
Site: River Bend 
Issue date: 03/27/1986
From: Chamberlain D, Jaudon J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20140H677 List:
References
50-458-86-14, NUDOCS 8604040170
Download: ML20140H699 (5)


See also: IR 05000458/1986014

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~ APPENDIX

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION IV

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sNRC Insp'ection Report:

50-458/86-14

License /CP:

NPF-47

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Do'cket: .;501458

Licensee:

Gulf States Utilities Company (GSU)

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P. O. Box 2951

Beaumont, Texas

77704

Facility Name: River Bend Station (RBS)

Inspection At: River Bend Station, St. Francisville, Louisiana

. Inspection' Conducted: March 17-20, 1986

.

3-25 8(3

Inspector:

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. D. Du Chamberlain, Ser.ior Resident Inspector

Date

-(pars. 1, 2, and 3)

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Approved:

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hief, Pr& Ject Section A,

Date

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ects Branch

Inspection Summary

Inspection Conducted March 17-20, 1986 (Report 50-458/86-14)

Areas Inspected: This inspection was a special, unannounced inspection

. conducted to review the conditions and actions which led to a Division II

'

diesel generator operability failure on March 17, 1986, and to review the

planned corrective actions.

Results: Within the areas inspected, three violations were identified

-(inadequate corrective action, failure to perform maintenance in accordance

with procedures and inoperable Division !! diesel generator, paragraph 2).

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DETAILS

1.

Persons Contacted

Principal Licensee Employee

  • R. E. Bailey, Supervisor, Quality Control (QC)
  • W. H. Cahill, Jr., Senior Vice President, River Bend Nuclear Group
  • E. M. Cargill, Supervisor, Radiation Programs
  • T. C. Crouse, Manager, Quality Assurance (QA)
  • J. C. Deddens, Vice President, River Bend Nuclear Group
  • D. C. Davenport, Supervisor, Security
  • J. W. Evans, Stenographer, GSU
  • D. R. Gipson, Assistant Plant Manager, Operations
  • E. R. Grant, Supervisor, Nuclear Licensing
  • R. Helmick, Director of Projects
  • R. Jackson, Shift Supervisor, Operations
  • R. J. King, Licensing Er.gineer
  • A. D. Kowalczuk, Assistant Plant Manager, Maintenance

R. Mayeux, Reactor Operator

  • J. H. McQuirter, Licensing Engineer
  • W. H. Odell, Manager, Administrative
  • T. F. Plunkett, Plant Manager
  • S. R. Radebaugh, Assistant Plant Manager, Services
  • D. Reynerson, Director, Nuclear Plant Engineering
  • R. R. Smith, Licensing Engineer
  • P. F. Tomlinson, Director, Quality Services

D. Williamson, Operations Supervisor

The NRC senior resident inspector (SRI) also interviewed additional

licensee personnel during the inspection period.

  • Denotes those persons that attended the exit interview conducted on

March 20, 1986. NRC resident inspector (RI), W. B. Jones, also attended

the exit interview.

2.

Division II Diesel Generator Operability Failure Review

This inspection was conducted by the SRI to review the conditions and

actions which led to a Division II diesel generator operability failure on

March 17, 1986, and to review the planned corrective actions. During

l

performance of Surveillance Test STP-309-0202, " Division II Diesel

Operability Test," on March 17, 1986, the diesel started and came up to

speed, frequency, and voltage within the required time, but about one

minute later it began to coast down and stopped because of loss of fuel

oil flow. River Bend Technical Specifications requires the diesel to

operate loaded for at least 60 minutes for demonstration of operability

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and requires three separate and independent diesel generators (1A,1B, and

IC) to be "0PERABLE" in "0PERATIONAL CONDITIONS 1, 2, and 3."

The plant

was in operational Condition 1 on March 17, 1986.

The licensee

immediately initiated a condition report (86-0311) for investigation,

analysis and corrective action on the ailed operability test.

The SRI review of the licensee's investigation of this incident revealed

the following:

a.

Inadequate Corrective Action: A similar event occurred on February

14, 1986, when the Division I diesel generator (1A) failed the

surveillance operability test. The condition report (86-0179)

investigation for this failure revealed that the fuel oil strainer

valve handle was missing and that the strainer valve was misaligned

causing a loss of fuel oil flow to the diesel generator. The Nuclear

Plant Engineering (HUPE) documented corrective action on February 15,

1986, only required that the fuel oil strainer valve be realigned and

that successful operation of the diesel be demonstrated. No ger.eric

action to prevent recurrence was documented, and no remedial or

generic corrective action was specified to be implemented by any.

Other section or department. No reason was determined for the

missing handle or for the misalignment of the fuel strainer. Also,

the investigation did not determine the duration of time that the

fuel strainer had been misaligned. The analysis and understanding of

the adverse condition does not appear to have been thorough enough to

identify and correct the root cause of the problem. This is

evidenced by a reoccurrent.e of the fuel strainer misalignment problem

on the Division II diesel generator, which resulted in the Division

II diesel generator operability failure on March 17, 1986. This

inadequate corrective action for the diesel generator operability

failure on February 14, 1986, was identified by the SRI as an

apparent violation (458/8614-01).

b.

Performance of Maintenance: As a result of the February 14, 1986,

Division I diesel generator operability failure, the fuel oil

strainer valve handle was removed from the Division II diesel and

installed on the Division I diesel.

It was also used as a pattern

for the maintenance shop to fabricate a new handle for the Division

II diesel.

This new handle was apparently fabricated through use of a shop work

order (SWO), but the maintenance department could not locate the SWO.

The new handle was installed February 17, 1986, on the Division II

diesel generator fuel oil strainer, but no maintenance work request

(MWR) was initiated to provide documentation of work performance or

to provide for retesting as appropriate. A SWO should not be used to

work on permanent plant equipment by licensee procedure. This

failure to initiate a HWR for performance of maintenance on permanent

plant equipment was identified by the SRI as an apparent violation

(458/8614-02).

_----___

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- generator was proved operable on February 15, 1986, by surveillance

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c.-

Inoperable Division II Diesel Generator: 'The Division II diesel

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,tes , and the new fuel oil strainer valve handle was apparently

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installed on February 17, 1986. No testing was performed af ter the

.

'

' handle was~ installed until the March ~17, 1986, surveillance test,

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which failed because of the' improper alignment of the fuel oil

strainer valve. On March 17, 1986, the valve handle was found to be

-

improperly posi_tioned on the fuel oil strainer, and the valve was

misaligned, causing a loss of fuel oil flow to the diesel. There was

no evidence found of any other maintenance work on the fuel oil

strainer between February 17, 1986, and March 17, 1986. Also, there

was no' evidence ~ found of operational realignment of the fuel oil

, strainer.

- With the_ plant in Operational Condition I on March 17, 1986, the

Division II diesel was discovered to be inoperable during

surveillance testing. .The diesel had apparently been inoperable for

an undetermined length of time between February 15, 1986, and March

-

17, 1986. This failure to have three separate and independent diesel

generators "0PERABLE" in "0PERATIONAL CONDITION 1" was identified by

the SRI as-an apparent Technical Specification violation

(458/8614-03).

d.

Licensee Investigation and Corrective Actions

The SRI found that the licensee was continuing his investigation of

this occurrence, and the following corrective actions were being

implemented:

.The licensee has scribed all three diesel generator fuel oil

.

strainer valves so that proper valve positioning is identified

with or without the handle being installed. Diesel operabi.11ty

has been verified for three diesels.

Maintenance personnel have been instructed on the proper

.

alignment of the fuel oil strainer handle and valve.

The plant operators are verifying proper position of the fuel oil

.

strainers during normal rounds (at least once per shift).

The plant manager has added a compliance inspector analyst to

.

his staff to assure procedure adherence for conduct of

maintenance.

This person is charged with the responsibility

for. compliance to procedures within the maintenance department.

,

.

The use of shop work orders has been eliminated.

.

i

The SRI will c.ontinue to nonitor licensee actions in this area.

.

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,

0

3

4

. __.

.

_ _ _

_ _ _ _ _ _ _ _ _ - _ _ .

_ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ - _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

. _ _ _ _ _ _ _ - __ _ ,

..

..

.

-5-

3.

Exit and Inspection Interviews

An exit interview was conducted on March 20, 1986, with licensee

representatives (identified in paragraph 1). During this interview, the

,

SRI reviewed the scope and findings of the inspection,

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