ENS 57506: Difference between revisions
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Revision as of 10:45, 24 January 2025
ENS Event | |
|---|---|
22:05 Dec 5, 2024 | |
| Title | 60-DAY Notification of Invalid Actuation of Emergency Diesel Generator |
| Event Description | The following information was provided by the licensee via phone and email:
This 60-day optional telephone notification is being made in lieu of a licensee event report submittal as allowed by 10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of one of the systems listed in 10 CFR 50.73(a)(2)(iv)(B). At approximately 1705 EST on December 5, 2024, an invalid actuation of emergency diesel generator (EDG) '2' occurred. It was determined that the run timing relay failed causing energization of the starting air solenoid valves ultimately resulting in EDG '2' spuriously starting and running with no demand and no auto-start signals. The actuation was not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the system. Therefore, this event has been determined to be an invalid actuation. During this event, the actuation of EDG '2' was complete. Initiation of attendant instrumentation/controls and supporting auxiliary equipment was as expected for the actuation being outside normal EDG start logic. Emergency bus 'E2' remained energized from offsite power and EDG '2' did not tie to bus 'E2'. This event did not result in any adverse impact to the health and safety of the public. The NRC Resident Inspector has been notified. |
| Where | |
|---|---|
| Unswick North Carolina (NRC Region 2) | |
| Reporting | |
| 10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
| Time - Person (Reporting Time:+1163.92 h48.497 days <br />6.928 weeks <br />1.594 months <br />) | |
| Opened: | Quintin Holley 10:00 Jan 23, 2025 |
| NRC Officer: | Josue Ramirez |
| Last Updated: | Jan 23, 2025 |
| 57506 - NRC Website | |
Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | No |
| Before | Power Operation (100 %) |
| After | Power Operation (100 %) |
Unit 2 | |
|---|---|
| Reactor critical | Critical |
| Scram | No |
| Before | Power Operation (100 %) |
| After | Power Operation (95 %) |
WEEKMONTHYEARENS 575062024-12-05T22:05:0005 December 2024 22:05:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-DAY Notification of Invalid Actuation of Emergency Diesel Generator ENS 573872024-09-10T17:42:00010 September 2024 17:42:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Optional Telephonic Notification of Invalid Actuation of Containment Isolation Valves ENS 569882023-12-28T13:15:00028 December 2023 13:15:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generators ENS 562872022-11-09T14:06:0009 November 2022 14:06:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 561382022-08-06T10:28:0006 August 2022 10:28:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Optional Telephonic Notification of Invalid Actuation of Containment Isolation Valves ENS 558592022-03-07T04:40:0007 March 2022 04:40:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation 60-DAY Telephone Notification ENS 557562022-01-04T18:16:0004 January 2022 18:16:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Optional Telephonic Notification for Invalid Actuation of Containment Isolation Valves ENS 551912021-02-17T19:07:00017 February 2021 19:07:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 546752020-03-05T14:25:0005 March 2020 14:25:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Telephonic Notification of an Invalid Specified System Actuation ENS 541442019-05-10T00:00:00010 May 2019 00:00:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Notification Due to Actuation of an Emergency Diesel Generator ENS 527782017-04-06T16:12:0006 April 2017 16:12:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generators ENS 520512016-05-09T10:26:0009 May 2016 10:26:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Primary Containment Isolation Valves (Pcivs) ENS 517392016-01-09T14:46:0009 January 2016 14:46:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generator ENS 515052015-09-10T01:03:00010 September 2015 01:03:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of a General Containment Isolation Signal Affecting More than One System ENS 498002013-12-11T13:18:00011 December 2013 13:18:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Primary Containment Isolation System (Pcis) Valves During I&C Maintenance ENS 491682013-05-08T01:14:0008 May 2013 01:14:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generators ENS 489722013-03-04T13:04:0004 March 2013 13:04:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generators ENS 442132008-03-15T20:35:00015 March 2008 20:35:00 10 CFR 50.73(a)(1), Submit an LER Invalid Primary Containment Isolation System (Pcis) Actuation ENS 437912007-09-21T18:10:00021 September 2007 18:10:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generators ENS 416922005-05-12T08:11:00012 May 2005 08:11:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.73(a)(1), Submit an LER Technical Specification Required Shutdown Due to Loss of Emergency Bus E1 ENS 413572004-12-13T21:15:00013 December 2004 21:15:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 405412004-01-11T11:37:00011 January 2004 11:37:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 404962003-12-22T03:04:00022 December 2003 03:04:00 10 CFR 50.73(a)(1), Submit an LER Invalid Reactor Building Exhaust Radiation Monitor Signal Resulting in Pcis Isolations 2024-09-10T17:42:00 | |