ENS 49168
ENS Event | |
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01:14 May 8, 2013 | |
Title | Invalid Actuation of Emergency Diesel Generators |
Event Description | This 60-day telephone notification is provided in accordance with 10 CFR 50.73(a)(1) to report an invalid actuation of the Emergency Diesel Generators (EDGs) reportable under 10 CFR 50.73(a)(2)(iv)(A). Due to the shared configuration of the onsite AC Electrical Distribution System, this event is applicable to both Units 1 and 2.
On May 7, 2013, at approximately 2114 hours0.0245 days <br />0.587 hours <br />0.0035 weeks <br />8.04377e-4 months <br /> Eastern Daylight Time (EDT), while Operations personnel were making preparations for Unit 2 main turbine generator synchronization to the grid, a Main Generator Reverse Power Trip occurred. Main Generator Reverse Power Trip was actuated after adjusting the Manual Voltage Regulator on the Main Generator. The reverse power relay operates the Generator Primary Lockout which initiates a turbine trip and start of all four EDGs. These features functioned as designed. The main generator breaker was open at the time of the event; as such, electrical power was not lost to the emergency busses. All four EDGs started and operated as expected. Because electrical power was never lost to the emergency busses and none of the EDGs loaded to their respective emergency busses, the actuations were considered to be partial. The EDGs were returned to their standby line-up by 2229 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.481345e-4 months <br /> on May 7, 2013. Since no actual bus under voltage condition existed which required the EDGs to start and the start was not in response to actual plant conditions satisfying the requirements for initiation, this event has been classified as an invalid actuation. This event did not result in any adverse impact to the health and safety of the public. The licensee has notified the NRC Resident Inspector. |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1328.93 h55.372 days <br />7.91 weeks <br />1.82 months <br />) | |
Opened: | Mark Turkal 10:10 Jul 2, 2013 |
NRC Officer: | Dong Park |
Last Updated: | Jul 2, 2013 |
49168 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (24 %) |
After | Power Operation (24 %) |
WEEKMONTHYEARENS 573872024-09-10T17:42:00010 September 2024 17:42:00
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