ML17345A583: Difference between revisions

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{{#Wiki_filter:UNIT SHUTDOWNS AND POWER REDUCTIONS                                     ET NO   50-250 UNiT NAME    Turke     Point   Lt;l         f 03 DATE November       15,
{{#Wiki_filter:~COPRECTED COPY**
        ~COPRECTED COPY**
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORTMONTH October 1988 ET NO 50-250 UNiTNAME Turke Point Lt;l f 03 DATE November 15, 1988'OMPLETED By D 1
By D     1 Bonett     1988'OMPLETED 7
Bonett 7
REPORTMONTH      October  1988                                            407     694-4432 Method of
407 694-4432
> t3$
> o60 t3$
o60 Shutting      Ucen see                                      Causa a Corrective
Ã~N b3 3)O tlO OO
  Ã~                     Type'uration                 Down          Event    System  Component                      Actionto N          Date            (Hours)   Reason2   Reactor       Report¹   Code~     Codes                  Prevent Recurrence b3  No.
()V KQl OM VICO O~
3)O tlO OO    10    881001            723. 6                        250-88-024       CF     PNPXX I
Oh) oo~
During the monthly Residual Heat
min)Q OVl No.
() V KQl                                                                                                Removal Pump (RHR)     inservice test, OM                                                                                                seal leakage in the 3A RHR pump VICO O~                                                                                                resulted in the pump being declared oo~
10 Date 881001 Type'uration (Hours) 723. 6 Reason2 Method of Shutting Down Reactor Ucen see Event Report¹ System Code~
Oh)                                                                                              out of service.     The   unit   was shut min)Q OVl de   and the 3A   RHR pump     leaking seal ms replaced srith a spare shaft seal.
250-88-024 CF Component Codes PNPXX Causa a Corrective Actionto Prevent Recurrence I
The outage was   further extended to repair the pressurizer heaters and replace electrical generator rotor.
During the monthly Residual Heat Removal Pump (RHR) inservice test, seal leakage in the 3A RHR pump resulted in the pump being declared out of service.
3 F Forced             Reason                                            Method                          Exhlxt G-instructions S Scheduhd           A - Equipment FaRure(Explain)                     1 - Manual                      for Preparation of Data 8 - Maintenance or Test                            2 - Manual Scram                Entry Scheets Ucensee C - RefueRng                                       3- Automatic Scram              Event Report(LER) Re D - Reguhtory Restriction                         4- Continued                    (NUREG0161)
The unit was shut de and the 3A RHR pump leaking seal ms replaced srith a spare shaft seal.
E - Operator Training & Ucense Examination         5- LoadReduction F - Administrative                                 9 - Other(Exphin)
The outage was further extended to repair the pressurizer heaters and replace electrical generator rotor.
G - Operational Error (Exphin)                                                     ExNbit1-Same Source H - Other(Exphin)
F Forced S Scheduhd Reason A - Equipment FaRure(Explain) 8 - Maintenance orTest C - RefueRng D - Reguhtory Restriction E - Operator Training &Ucense Examination F - Administrative G - Operational Error (Exphin)
H - Other(Exphin) 3 Method 1 - Manual 2 - Manual Scram 3-Automatic Scram 4-Continued 5-LoadReduction 9 - Other(Exphin)
ExhlxtG-instructions forPreparation ofData EntryScheets Ucensee Event Report(LER) Re (NUREG0161)
ExNbit1-Same Source


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Latest revision as of 11:37, 7 January 2025

Corrected Monthly Operating Rept for Oct 1988 for Turkey Point Unit 3
ML17345A583
Person / Time
Site: Turkey Point, 05000000
Issue date: 10/31/1988
From: Bonett D
FLORIDA POWER & LIGHT CO.
To:
Shared Package
ML17345A581 List:
References
NUDOCS 8812200015
Download: ML17345A583 (2)


Text

~COPRECTED COPY**

UNIT SHUTDOWNS AND POWER REDUCTIONS REPORTMONTH October 1988 ET NO 50-250 UNiTNAME Turke Point Lt;l f 03 DATE November 15, 1988'OMPLETED By D 1

Bonett 7

407 694-4432

> o60 t3$

Ã~N b3 3)O tlO OO

()V KQl OM VICO O~

Oh) oo~

min)Q OVl No.

10 Date 881001 Type'uration (Hours) 723. 6 Reason2 Method of Shutting Down Reactor Ucen see Event Report¹ System Code~

250-88-024 CF Component Codes PNPXX Causa a Corrective Actionto Prevent Recurrence I

During the monthly Residual Heat Removal Pump (RHR) inservice test, seal leakage in the 3A RHR pump resulted in the pump being declared out of service.

The unit was shut de and the 3A RHR pump leaking seal ms replaced srith a spare shaft seal.

The outage was further extended to repair the pressurizer heaters and replace electrical generator rotor.

F Forced S Scheduhd Reason A - Equipment FaRure(Explain) 8 - Maintenance orTest C - RefueRng D - Reguhtory Restriction E - Operator Training &Ucense Examination F - Administrative G - Operational Error (Exphin)

H - Other(Exphin) 3 Method 1 - Manual 2 - Manual Scram 3-Automatic Scram 4-Continued 5-LoadReduction 9 - Other(Exphin)

ExhlxtG-instructions forPreparation ofData EntryScheets Ucensee Event Report(LER) Re (NUREG0161)

ExNbit1-Same Source

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