ML17345A583: Difference between revisions
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{{#Wiki_filter:UNIT SHUTDOWNS AND POWER REDUCTIONS | {{#Wiki_filter:~COPRECTED COPY** | ||
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORTMONTH October 1988 ET NO 50-250 UNiTNAME Turke Point Lt;l f 03 DATE November 15, 1988'OMPLETED By D 1 | |||
By D | Bonett 7 | ||
407 694-4432 | |||
> t3$ | > o60 t3$ | ||
Ã~N b3 3)O tlO OO | |||
()V KQl OM VICO O~ | |||
Oh) oo~ | |||
During the monthly Residual Heat | min)Q OVl No. | ||
10 Date 881001 Type'uration (Hours) 723. 6 Reason2 Method of Shutting Down Reactor Ucen see Event Report¹ System Code~ | |||
250-88-024 CF Component Codes PNPXX Causa a Corrective Actionto Prevent Recurrence I | |||
The outage was | During the monthly Residual Heat Removal Pump (RHR) inservice test, seal leakage in the 3A RHR pump resulted in the pump being declared out of service. | ||
The unit was shut de and the 3A RHR pump leaking seal ms replaced srith a spare shaft seal. | |||
E - Operator Training & Ucense Examination | The outage was further extended to repair the pressurizer heaters and replace electrical generator rotor. | ||
F Forced S Scheduhd Reason A - Equipment FaRure(Explain) 8 - Maintenance orTest C - RefueRng D - Reguhtory Restriction E - Operator Training &Ucense Examination F - Administrative G - Operational Error (Exphin) | |||
H - Other(Exphin) 3 Method 1 - Manual 2 - Manual Scram 3-Automatic Scram 4-Continued 5-LoadReduction 9 - Other(Exphin) | |||
ExhlxtG-instructions forPreparation ofData EntryScheets Ucensee Event Report(LER) Re (NUREG0161) | |||
ExNbit1-Same Source | |||
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h}} | h}} | ||
Latest revision as of 11:37, 7 January 2025
| ML17345A583 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point, 05000000 |
| Issue date: | 10/31/1988 |
| From: | Bonett D FLORIDA POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML17345A581 | List: |
| References | |
| NUDOCS 8812200015 | |
| Download: ML17345A583 (2) | |
Text
~COPRECTED COPY**
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORTMONTH October 1988 ET NO 50-250 UNiTNAME Turke Point Lt;l f 03 DATE November 15, 1988'OMPLETED By D 1
Bonett 7
407 694-4432
> o60 t3$
Ã~N b3 3)O tlO OO
()V KQl OM VICO O~
Oh) oo~
min)Q OVl No.
10 Date 881001 Type'uration (Hours) 723. 6 Reason2 Method of Shutting Down Reactor Ucen see Event Report¹ System Code~
250-88-024 CF Component Codes PNPXX Causa a Corrective Actionto Prevent Recurrence I
During the monthly Residual Heat Removal Pump (RHR) inservice test, seal leakage in the 3A RHR pump resulted in the pump being declared out of service.
The unit was shut de and the 3A RHR pump leaking seal ms replaced srith a spare shaft seal.
The outage was further extended to repair the pressurizer heaters and replace electrical generator rotor.
F Forced S Scheduhd Reason A - Equipment FaRure(Explain) 8 - Maintenance orTest C - RefueRng D - Reguhtory Restriction E - Operator Training &Ucense Examination F - Administrative G - Operational Error (Exphin)
H - Other(Exphin) 3 Method 1 - Manual 2 - Manual Scram 3-Automatic Scram 4-Continued 5-LoadReduction 9 - Other(Exphin)
ExhlxtG-instructions forPreparation ofData EntryScheets Ucensee Event Report(LER) Re (NUREG0161)
ExNbit1-Same Source
~r li
~
g L
h