ML19268C169: Difference between revisions

From kanterella
Jump to navigation Jump to search
Created page by program invented by StriderTol
 
StriderTol Bot change
 
(One intermediate revision by the same user not shown)
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = NUDOCS 8001030516
| document report number = NUDOCS 8001030516
| document type = REPORTABLE OCCURRENCE REPORT (SEE ALSO AO,LER), TEXT-SAFETY REPORT
| document type = REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER), TEXT-SAFETY REPORT
| page count = 1
| page count = 1
}}
}}


=Text=
=Text=
{{#Wiki_filter:._____._.-.-                -      -
{{#Wiki_filter:. _ _ _ _ _. _. -. -
Virginia Electric and Fcher Capany 1ortn Anns P:'ar   a  Staticn, Unit 91 NFF-4
Virginia Electric and Fcher Capany 1ortn Anns P:'ar Staticn, Unit 91 NFF-4 a
    ,'                  Decket b. EO-330 24 Mcur Reportable Event f                    licitten Follt.w-Up
Decket b. EO-330 f
[1 h
24 Mcur Reportable Event
3                     Event:       Iccorrect f aisnic Respensa spectru Cur.e Used d
[1 licitten Follt.w-Up h
3 Event:
Iccorrect f aisnic Respensa spectru Cur.e Used d
in a Pips Stress Analysis LER/60 79-15)/01T-0
in a Pips Stress Analysis LER/60 79-15)/01T-0
  $
$i During 'the revi(w of valve keights in cen[urcticn with the as-tuilt' reviu of IE Eulletin 79-14, it was discovered that an incorrect geisnic respcase i
i During 'the revi(w of valve keights in cen[urcticn with the as-tuilt' reviu of IE Eulletin 79-14, it was discovered that an incorrect geisnic respcase i                     specteta curva nxd been used in a pipe strass analysis. Review of the selmic i                     input to other stress prcblic.s ra,realed that sc a othar seis,.ic curve:; had ust.d
specteta curva nxd been used in a pipe strass analysis.
    '
Review of the selmic i
the wrcng input for:.at.
input to other stress prcblic.s ra,realed that sc a othar seis,.ic curve:; had ust.d the wrcng input for:.at.
  '
.The cause of this discrepancy is r.ot knc n at this tiu.
                                  .The cause of this discrepancy is r.ot knc n at this tiu.
An investigstion of tre extent of tta problen is in prcgrass.
:
This in w -
* An investigstion of tre extent of tta problen is in prcgrass.         This in w -
tigaticn has sit. n that sc a of the strass analyses for ec Eccur.t ccaling. suc...
tigaticn has sit. n that sc a of the strass analyses for ec Eccur.t ccaling. suc. ..
kater, ar.d other safety related systa. s used incorrect seistiic f nput whicn eculd have yieldad ir.ccnservative pipa stresses pipe support loads, ar.d equip. ant im Ncne cf the deficier.cias founo were 1ccated in the contaire, ant tu11dico n.n e
    .                    kater, ar.d other safety related systa. s used incorrect seistiic f nput whicn eculd
kere any a part of the reactor ecolant pressure tcundsry.
'.                      have yieldad ir.ccnservative pipa stresses pipe support loads, ar.d equip . ant im e                            Ncne cf the deficier.cias founo were 1ccated in the contaire, ant tu11dico n.n kere any a part of the reactor ecolant pressure tcundsry. Cr.e of the strets analyses in tt:e Auxiliary Euildir.g has tun run with the correct seliale curva
Cr.e of the strets analyses in tt:e Auxiliary Euildir.g has tun run with the correct seliale curva and resultad in a calculated pipe stress atove the allcatie stated in the FDn.
    -                    and resultad in a calculated pipe stress atove the allcatie stated in the FDn.
The unit is presently in a refueling shutdt,wn r.cds.
      -                            The unit is presently in a refueling shutdt,wn r.cds.
I U
I                                                                                               U     Cc
Cc O
        .
Ii2 a s,P.01g uY C *g Ao cn a g, g. UP#GW
O      Ii2
: t. _
                                      '
3,9.CHEMDES O
a s,P.01g uY
. s, a, **
                                                                                          '
T d
                                                                                                        $      C *g
i i
          ,
& k WG g, putMff t, suTMM
                                                                  '#                                    cn     Ao
'U i
          !
g f,, -
a g, g. UP#GW                               t. _
ll E Y C
          ;                                                          3,9.CHEMDES                               O i
cr:
                                                                  . s, a, **                             T     d
s J
                                                                                                              "'
0 q
i                                                          & k WG g, putMff                   ..
r 6
i    t, suTMM                               'U
' " ~ ~ ~
            ,                                                                                          g
d'
            '                                                                      C                  cr:  f,, -
~-
s                                                        ll E Y
8001030 C/6 3
            '
.}}
                  ,
                  -
J                             .
:
:
                    .
0
    .                                                _
                                                                '
                                                                                                .
q r 6
                                                                                      ' " ~ ~ ~
                ' -    _ _ _ _ _          _              d' ~-
                                                                                .
8001030 C/6
                                                                                          . 3}}

Latest revision as of 07:04, 3 January 2025

RO-79-151/01T-0:during Review of Valve Weights in Conjunction W/Ie Bulletin 79-14,discovered That Incorrect Seismic Response Spectrum Was Used in Pipe Stress Analysis. Cause Not Known.Investigation in Progress
ML19268C169
Person / Time
Site: North Anna 
Issue date: 11/06/1979
From:
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
References
NUDOCS 8001030516
Download: ML19268C169 (1)


Text

. _ _ _ _ _. _. -. -

Virginia Electric and Fcher Capany 1ortn Anns P:'ar Staticn, Unit 91 NFF-4 a

Decket b. EO-330 f

24 Mcur Reportable Event

[1 licitten Follt.w-Up h

3 Event:

Iccorrect f aisnic Respensa spectru Cur.e Used d

in a Pips Stress Analysis LER/60 79-15)/01T-0

$i During 'the revi(w of valve keights in cen[urcticn with the as-tuilt' reviu of IE Eulletin 79-14, it was discovered that an incorrect geisnic respcase i

specteta curva nxd been used in a pipe strass analysis.

Review of the selmic i

input to other stress prcblic.s ra,realed that sc a othar seis,.ic curve:; had ust.d the wrcng input for:.at.

.The cause of this discrepancy is r.ot knc n at this tiu.

An investigstion of tre extent of tta problen is in prcgrass.

This in w -

tigaticn has sit. n that sc a of the strass analyses for ec Eccur.t ccaling. suc...

kater, ar.d other safety related systa. s used incorrect seistiic f nput whicn eculd have yieldad ir.ccnservative pipa stresses pipe support loads, ar.d equip. ant im Ncne cf the deficier.cias founo were 1ccated in the contaire, ant tu11dico n.n e

kere any a part of the reactor ecolant pressure tcundsry.

Cr.e of the strets analyses in tt:e Auxiliary Euildir.g has tun run with the correct seliale curva and resultad in a calculated pipe stress atove the allcatie stated in the FDn.

The unit is presently in a refueling shutdt,wn r.cds.

I U

Cc O

Ii2 a s,P.01g uY C *g Ao cn a g, g. UP#GW

t. _

3,9.CHEMDES O

. s, a, **

T d

i i

& k WG g, putMff t, suTMM

'U i

g f,, -

ll E Y C

cr:

s J

0 q

r 6

' " ~ ~ ~

d'

~-

8001030 C/6 3

.