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t JOSEPH M. FARLEY NUCLEAR PLANT | t JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1 NARRATIVE | ||
==SUMMARY== | ==SUMMARY== | ||
OF OPERATIONS DECEMBER, 1982 In the month of December there was one unit shutdown. | OF OPERATIONS DECEMBER, 1982 In the month of December there was one unit shutdown. | ||
The following safety-related maintenance was performed in the month of December: | The following safety-related maintenance was performed in the month of December: | ||
1. | |||
Performed miscellaneous maintenance on diesel generators. | |||
2. | |||
Repacked #4 River Water pump. | |||
4 i | 4 i | ||
n | n P301240041 830114 PDR ADOCK 05000348 R | ||
P301240041 830114 PDR ADOCK 05000348 R | PDR | ||
t OPERATING DATA REPORT DOCKET NO. 50-348 DATE 1/06/83 COMPLETED BY W.G.Hairston,Ill TELEPilONE (205)899-5156 OPERATING STATUS | t OPERATING DATA REPORT DOCKET NO. 50-348 DATE 1/06/83 COMPLETED BY W.G.Hairston,Ill TELEPilONE (205)899-5156 OPERATING STATUS | ||
: 1. Unit Name: | : 1. Unit Name: | ||
: 2. Reporting Period: | J seph M. Farley - Unit 1 Notes | ||
: 2. Reporting Period: | |||
December, 1982 | |||
: 1) Cumulative data since | |||
: 3. Licensed Thermal Power (MWt): | : 3. Licensed Thermal Power (MWt): | ||
: 4. Nameplate Rating (Gross MWe): | 2652 12/01/77, date" of | ||
: 5. Design Electrical Rating (Net MWe): | : 4. Nameplate Rating (Gross MWe): | ||
: 6. Maximum Dependable Capacity (Gross MWe): | 860 commercial operation. | ||
: 7. Maximum Dependable Capacity (Net MWe): | : 5. Design Electrical Rating (Net MWe): | ||
829 | |||
: 6. Maximum Dependable Capacity (Gross MWe): | |||
844.6 | |||
: 7. Maximum Dependable Capacity (Net MWe): | |||
803.6 | |||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | : 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | ||
N/A | N/A | ||
: 9. Power Level To Which Restricted,If Any (Net MWe): | : 9. Power Level To Which Restricted,If Any (Net MWe): | ||
: 10. Reasons For Restrictions.If Any: | N/A | ||
: 11. Hours In Reporting Period | : 10. Reasons For Restrictions.If Any: | ||
: 12. Number Of flours Reactor Was Critical | N/A This Month Yr..to.Date Curimlatise | ||
: 14. Hours Generator On-Line | : 11. Hours In Reporting Period 744 8,760 44,568 | ||
: 15. Unit Reserve Shutdown Hours | : 12. Number Of flours Reactor Was Critical 736.5 7,165.7 28,147.5 | ||
: 16. Gross Thermal Energy Generated (MWH) | : 13. Reactor Reserve Shutdown Hours 0 | ||
: 17. Gross Electrical Energy Generated (MWH) | 122.5 3,614.5 t | ||
l | |||
: 18. Net Electrical Energy Generated (MWH) | : 14. Hours Generator On-Line 731.2 6,938.5 27,268.2 | ||
: 19. Unit Service Factor | : 15. Unit Reserve Shutdown Hours 0 | ||
0 0- | |||
: 23. Unit Forced Outage Rate | : 16. Gross Thermal Energy Generated (MWH) i As6 457 17.545.138 68.490.049 | ||
: 17. Gross Electrical Energy Generated (MWH) 590.llft_,_. | |||
5.536.596 21.773,548 t | |||
: 18. Net Electrical Energy Generated (MWH) 559.140 5,216,496 20,440,220 l | |||
: 19. Unit Service Factor 98.3 79.2 61.2 | |||
: 20. Unit Availability Factor 98.3 79.2 61.2 l | |||
: 21. Unit Capacity Factor IUsing MDC Net) 93.5 74.1 57.1 l | |||
: 22. Unit Capacity FactoriUsing DER Net) 90.7 | |||
.71.8 55.3 | |||
: 23. Unit Forced Outage Rate 1.7 20.6 18.2 | |||
: 24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and Duration of Each): | : 24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and Duration of Each): | ||
Refuelinc Outane. January 15, 1983, Approximately 11 weeks | Refuelinc Outane. January 15, 1983, Approximately 11 weeks | ||
: 25. If Shut Down At End Of Report Period. Estimated Date of Startup: | : 25. If Shut Down At End Of Report Period. Estimated Date of Startup: | ||
: 26. Units in Test Status tPrior to Commercial Operation): | N/A | ||
: 26. Units in Test Status tPrior to Commercial Operation): | |||
Forecast Achiesed INITI A L CRITICALITY 8/06/77 8/09/77 INITIA L ELECTRICITY 8/20/77 8/18/77 COMMERCI AL OPER ATION 12 /n 1/ 7.7 12/01/77 (4/77) | |||
L: | L: | ||
..n.. | |||
.a | |||
a | .n.... | ||
..,.;.-~.~.... | |||
DOCKET NO. | a DOCKET NO. | ||
50-348 | |||
~ | |||
UNIT | ~ | ||
UNIT 1 | |||
DAY | ~ | ||
260 | DAE 1/06/83 CO5!PLETED BY W.G.Hairston, III | ||
587 | . TELEPl!ONE (205)899-5156 December MONTl! | ||
DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (AlWe Net) | |||
7 | (51We Net) g, g7 810 796 2 | ||
663 33 812 3 | |||
77 g9 808 807 260 2g 4 | |||
587 807 3 | |||
21 799 805 6 | |||
22 7 | |||
809 23 803 809 797 g | |||
24 9 | |||
809 25-797 10 808 26 809 800 801 27 gg 12 806 23 797 801 13 812 | |||
;9 810 800 g4 30 IS 803 33 795 16 808 INSTRUCDONS On this fonnst. list the svenge daily unit power levelin MWe-Net for esch d:y in the reporting inonth. Compute to | |||
, the neare:t whole ne;swait. | |||
(9p7) | (9p7) | ||
O | O g | ||
~ | |||
.. ~, | |||
6 | a 6 | ||
UNIT SilUTDOWNS AND POWER REDUCI10NS | UNIT SilUTDOWNS AND POWER REDUCI10NS DOCKET NO. 50-34o UNIT NAME J.M_FARLEY-UNIT 1 DATE 1/06/R7 COMPLETED BY W C nairston,III REPORT MONTil Decomho v-TELEPilONE (2051 899-5156 w. | ||
E E | |||
.! E | |||
* | } | ||
mU | j E5 Licensee h | ||
011 | h Cause & Corrective No. | ||
failure of a control driver card for lA feed regulating valve power supply. A subsequent reactor trip occurred due to Lo-Lo S/G level caused by operator error. | Date g | ||
gg 2g5 Event g | |||
jE 5 | |||
j5g Repori | |||
* g{ | |||
Action to H | |||
mU Prevent Recurrence 6 | |||
011 821202 F | |||
12.8 A | |||
3 NA CH INSTRU Unit tripped due to the failure of a control driver card for lA feed regulating valve power supply. | |||
A subsequent reactor trip occurred due to Lo-Lo S/G level caused by operator error. | |||
r l | |||
5 l | |||
t l | t l | ||
I | I 2 | ||
3 4 | |||
F: Forced Reason: | |||
C Refueling | Method: | ||
i E Operator Training & IJcense Examination | Exhibit G. instructions i | ||
S; Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram. | |||
G-Opes.;tional Litor (Explain) | Entry Sheets for I.icensee C Refueling 3 Automatic Scram. | ||
Event ReporI (1.ER) File (NUREG-l l | |||
D Regulatosy Restriction 4 Other (Explain) 0161) i E Operator Training & IJcense Examination l | |||
F-Administ rative 5 | |||
G-Opes.;tional Litor (Explain) | |||
Exhibit 1 Same Source (9/77) ll Othes (Explain) | |||
U}} | U}} | ||
Latest revision as of 05:53, 15 December 2024
| ML20072A495 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 01/05/1983 |
| From: | Hairston W ALABAMA POWER CO. |
| To: | |
| Shared Package | |
| ML20072A470 | List: |
| References | |
| NUDOCS 8301240041 | |
| Download: ML20072A495 (4) | |
Text
-
t JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1 NARRATIVE
SUMMARY
OF OPERATIONS DECEMBER, 1982 In the month of December there was one unit shutdown.
The following safety-related maintenance was performed in the month of December:
1.
Performed miscellaneous maintenance on diesel generators.
2.
Repacked #4 River Water pump.
4 i
n P301240041 830114 PDR ADOCK 05000348 R
t OPERATING DATA REPORT DOCKET NO. 50-348 DATE 1/06/83 COMPLETED BY W.G.Hairston,Ill TELEPilONE (205)899-5156 OPERATING STATUS
- 1. Unit Name:
J seph M. Farley - Unit 1 Notes
- 2. Reporting Period:
December, 1982
- 1) Cumulative data since
- 3. Licensed Thermal Power (MWt):
2652 12/01/77, date" of
- 4. Nameplate Rating (Gross MWe):
860 commercial operation.
- 5. Design Electrical Rating (Net MWe):
829
- 6. Maximum Dependable Capacity (Gross MWe):
844.6
- 7. Maximum Dependable Capacity (Net MWe):
803.6
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
N/A
- 9. Power Level To Which Restricted,If Any (Net MWe):
N/A
- 10. Reasons For Restrictions.If Any:
N/A This Month Yr..to.Date Curimlatise
- 11. Hours In Reporting Period 744 8,760 44,568
- 12. Number Of flours Reactor Was Critical 736.5 7,165.7 28,147.5
- 13. Reactor Reserve Shutdown Hours 0
122.5 3,614.5 t
l
- 14. Hours Generator On-Line 731.2 6,938.5 27,268.2
- 15. Unit Reserve Shutdown Hours 0
0 0-
- 16. Gross Thermal Energy Generated (MWH) i As6 457 17.545.138 68.490.049
- 17. Gross Electrical Energy Generated (MWH) 590.llft_,_.
5.536.596 21.773,548 t
- 18. Net Electrical Energy Generated (MWH) 559.140 5,216,496 20,440,220 l
- 19. Unit Service Factor 98.3 79.2 61.2
- 20. Unit Availability Factor 98.3 79.2 61.2 l
- 21. Unit Capacity Factor IUsing MDC Net) 93.5 74.1 57.1 l
- 22. Unit Capacity FactoriUsing DER Net) 90.7
.71.8 55.3
- 23. Unit Forced Outage Rate 1.7 20.6 18.2
- 24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and Duration of Each):
Refuelinc Outane. January 15, 1983, Approximately 11 weeks
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
N/A
- 26. Units in Test Status tPrior to Commercial Operation):
Forecast Achiesed INITI A L CRITICALITY 8/06/77 8/09/77 INITIA L ELECTRICITY 8/20/77 8/18/77 COMMERCI AL OPER ATION 12 /n 1/ 7.7 12/01/77 (4/77)
L:
..n..
.a
.n....
..,.;.-~.~....
a DOCKET NO.
50-348
~
~
UNIT 1
~
DAE 1/06/83 CO5!PLETED BY W.G.Hairston, III
. TELEPl!ONE (205)899-5156 December MONTl!
DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (AlWe Net)
(51We Net) g, g7 810 796 2
663 33 812 3
77 g9 808 807 260 2g 4
587 807 3
21 799 805 6
22 7
809 23 803 809 797 g
24 9
809 25-797 10 808 26 809 800 801 27 gg 12 806 23 797 801 13 812
- 9 810 800 g4 30 IS 803 33 795 16 808 INSTRUCDONS On this fonnst. list the svenge daily unit power levelin MWe-Net for esch d
- y in the reporting inonth. Compute to
, the neare:t whole ne;swait.
(9p7)
O g
~
.. ~,
a 6
UNIT SilUTDOWNS AND POWER REDUCI10NS DOCKET NO.50-34o UNIT NAME J.M_FARLEY-UNIT 1 DATE 1/06/R7 COMPLETED BY W C nairston,III REPORT MONTil Decomho v-TELEPilONE (2051 899-5156 w.
E E
.! E
}
j E5 Licensee h
h Cause & Corrective No.
Date g
gg 2g5 Event g
jE 5
j5g Repori
- g{
Action to H
mU Prevent Recurrence 6
011 821202 F
12.8 A
3 NA CH INSTRU Unit tripped due to the failure of a control driver card for lA feed regulating valve power supply.
A subsequent reactor trip occurred due to Lo-Lo S/G level caused by operator error.
r l
5 l
t l
I 2
3 4
F: Forced Reason:
Method:
Exhibit G. instructions i
S; Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.
Entry Sheets for I.icensee C Refueling 3 Automatic Scram.
Event ReporI (1.ER) File (NUREG-l l
D Regulatosy Restriction 4 Other (Explain) 0161) i E Operator Training & IJcense Examination l
F-Administ rative 5
G-Opes.;tional Litor (Explain)
Exhibit 1 Same Source (9/77) ll Othes (Explain)
U