ML20086G006: Difference between revisions

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=Text=
=Text=
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PHILADELPHIA ELECTRIC' COMPANY 2301 MARKET STREET PHILADELPHIA PA.19101 12151 841 4o00 August 27, 1975                                                   ,
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PHILADELPHIA ELECTRIC' COMPANY 2301 MARKET STREET PHILADELPHIA PA.19101 12151 841 4o00 August 27, 1975 u,
JI Mr. Roger S. Boyd                                                     (
JI Mr. Roger S. Boyd
                                                                                                    . c.
(
Acting Director Division of Reactor Licensing                                                                     '
. c.
Office of Nuclear Reactor Regulations                                                             -
Acting Director Division of Reactor Licensing Office of Nuclear Reactor Regulations United States Nuclear Regulatory Commission
United States Nuclear Regulatory Commission                                   '.              ~
~
Washington, DC     20555
Washington, DC 20555


==Dear Mr. Boyd:==
==Dear Mr. Boyd:==
==Subject:==
==Subject:==
Abnormal Occurrence The following occurrence was reported to Mr. Jim Partlow, Region 1, Office of Inspection and Enforcement, United States Nuclear Regulatory Commission on August 17, 1975. Written notification was made to Mr. James P. O'Reilly, Office of Inspection and Enforcement, Region 1 United States Nuclear Regulatory Commission on August 18, 1975 In accor-dance with Section 6.7.2.A of the Technical Specifications, Appendix A of DPR-44 for Unit 2 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Reactor Licensing as an Abnormal Occurrence.
Abnormal Occurrence The following occurrence was reported to Mr. Jim Partlow, Region 1, Office of Inspection and Enforcement, United States Nuclear Regulatory Commission on August 17, 1975. Written notification was made to Mr. James P. O'Reilly, Office of Inspection and Enforcement, Region 1 United States Nuclear Regulatory Commission on August 18, 1975 In accor-dance with Section 6.7.2.A of the Technical Specifications, Appendix A of DPR-44 for Unit 2 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Reactor Licensing as an Abnormal Occurrence.
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==Reference:==
==Reference:==
3.7.D.2, Table 3.7.1 Report No.:         50-277-75-57 Report Date:       August 27, 1975 Occurrence Date: August 17, 1975 Facility:           Peach Bottom Atomic Power Station R.D. 1, Delta, Pennsylvania   17314 Identification of Occurrencc:
3.7.D.2, Table 3.7.1 Report No.:
50-277-75-57 Report Date:
August 27, 1975 Occurrence Date: August 17, 1975 Facility:
Peach Bottom Atomic Power Station R.D. 1, Delta, Pennsylvania 17314 Identification of Occurrencc:
Reactor Recirculation System Outboard Sample Isolation Valve, A0-2-2-40 failure to close during test.
Reactor Recirculation System Outboard Sample Isolation Valve, A0-2-2-40 failure to close during test.
Conditions Prior to Occurrence:
Conditions Prior to Occurrence:
Unit 2 reactor shutdown.
Unit 2 reactor shutdown.
Description of Occurrence:
Description of Occurrence:
i t
i During the performance of ST 1.3, the PCIS Logic System Functional t
'                    During the performance of ST 1.3, the PCIS Logic System Functional Test, valve A0-2-2-40 failed to close.
Test, valve A0-2-2-40 failed to close.
8401090787 750827                                                             297
8401090787 750827 297
                                                                                              ""              /
/
PDR S
PDR ADOCK 05000277
ADOCK 05000277
$' PY SENTREGION iw
:                                                                                                          /
/
,                                PDR                                      $' PY SENTREGION iw h                                                                                                                   _
S PDR h


                                                                                      ^
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g Mr. R. S. Boyd
g 50-277-75-57 l
* 50-277-75-57 l   .
Mr. R. S. Boyd *
()                                 ()
' August 27, 1975 ()
      ' August 27, 1975                                                  P:ga 2 Designation of Apparent Cause of Occurrence:
()
P:ga 2 Designation of Apparent Cause of Occurrence:
Stuck aolenoid valve.
Stuck aolenoid valve.
Analysis of Occurrence:
Analysis of Occurrence:
The safety significance of this occurrence is minimal because the inboard isolation valve A0-2-2-39 was found to close satisfactorily, i       Corrective Action:
The safety significance of this occurrence is minimal because the inboard isolation valve A0-2-2-39 was found to close satisfactorily, i
Corrective Action:
The solenoid valve was disassembled and cleaned. The valve was retested satisfactorily after repair. In the interim, the inboard isolation valve A0-2-2-39 was maintained closed.
The solenoid valve was disassembled and cleaned. The valve was retested satisfactorily after repair. In the interim, the inboard isolation valve A0-2-2-39 was maintained closed.
t   .        ..                              ,
t Failure Data:
Failure Data:
Previous failures of this type were reported as: A0-50-227-75-14, and A0-50-278-74-23.
Previous failures of this type were reported as: A0-50-227-75-14, and A0-50-278-74-23.
Very truly yours, h ((Cf bL
Very truly yours, h ((Cf bL
(%
(%
M. J. Cooney Ass't Gen't Superintendent Generation Division P
M. J. Cooney Ass't Gen't Superintendent Generation Division P
cc: Mr. J. P. O'Reilly Director, Region 1 Office of Inspection and Enforcement United States Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA     19406 i
cc: Mr. J. P. O'Reilly Director, Region 1 Office of Inspection and Enforcement United States Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 i
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Latest revision as of 02:12, 14 December 2024

AO 75-57:on 750817,reactor Recirculation Sys Outboard Sample Isolation Valve AO-2-2-40 Failed to Close During Test.Caused by Stuck Solenoid Valve.Solenoid Valve Disassembled & Cleaned
ML20086G006
Person / Time
Site: Peach Bottom 
Issue date: 08/27/1975
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Boyd R
Office of Nuclear Reactor Regulation
Shared Package
ML20086G009 List:
References
AO-75-57, NUDOCS 8401090787
Download: ML20086G006 (2)


Text

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v V

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PHILADELPHIA ELECTRIC' COMPANY 2301 MARKET STREET PHILADELPHIA PA.19101 12151 841 4o00 August 27, 1975 u,

JI Mr. Roger S. Boyd

(

. c.

Acting Director Division of Reactor Licensing Office of Nuclear Reactor Regulations United States Nuclear Regulatory Commission

~

Washington, DC 20555

Dear Mr. Boyd:

Subject:

Abnormal Occurrence The following occurrence was reported to Mr. Jim Partlow, Region 1, Office of Inspection and Enforcement, United States Nuclear Regulatory Commission on August 17, 1975. Written notification was made to Mr. James P. O'Reilly, Office of Inspection and Enforcement, Region 1 United States Nuclear Regulatory Commission on August 18, 1975 In accor-dance with Section 6.7.2.A of the Technical Specifications, Appendix A of DPR-44 for Unit 2 Peach Bottom Atomic Power Station, the following report is being submitted to the Directorate of Reactor Licensing as an Abnormal Occurrence.

Re ference : License Number DPR-44 Technical Specification

Reference:

3.7.D.2, Table 3.7.1 Report No.:

50-277-75-57 Report Date:

August 27, 1975 Occurrence Date: August 17, 1975 Facility:

Peach Bottom Atomic Power Station R.D. 1, Delta, Pennsylvania 17314 Identification of Occurrencc:

Reactor Recirculation System Outboard Sample Isolation Valve, A0-2-2-40 failure to close during test.

Conditions Prior to Occurrence:

Unit 2 reactor shutdown.

Description of Occurrence:

i During the performance of ST 1.3, the PCIS Logic System Functional t

Test, valve A0-2-2-40 failed to close.

8401090787 750827 297

/

PDR ADOCK 05000277

$' PY SENTREGION iw

/

S PDR h

^

g 50-277-75-57 l

Mr. R. S. Boyd *

' August 27, 1975 ()

()

P:ga 2 Designation of Apparent Cause of Occurrence:

Stuck aolenoid valve.

Analysis of Occurrence:

The safety significance of this occurrence is minimal because the inboard isolation valve A0-2-2-39 was found to close satisfactorily, i

Corrective Action:

The solenoid valve was disassembled and cleaned. The valve was retested satisfactorily after repair. In the interim, the inboard isolation valve A0-2-2-39 was maintained closed.

t Failure Data:

Previous failures of this type were reported as: A0-50-227-75-14, and A0-50-278-74-23.

Very truly yours, h ((Cf bL

(%

M. J. Cooney Ass't Gen't Superintendent Generation Division P

cc: Mr. J. P. O'Reilly Director, Region 1 Office of Inspection and Enforcement United States Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 i

9 0

1 e

4 l

4

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