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=Text= | =Text= | ||
{{#Wiki_filter:' | {{#Wiki_filter:' | ||
O | O O | ||
a in PHILAD ELPHIA ELECTRIC COM PANY | |||
- Q '+,;J ^ > | |||
, k,/ 7.,, | |||
V'4 s | |||
-( | |||
//, | |||
PHIL A DEL.PH I A. PA.19101 | ,- s 2301 M ARKET STREET | ||
~,?. \\/ | |||
']h.- | |||
PHIL A DEL.PH I A. PA.19101 i. | |||
'.,,:, V,( _. (, < | |||
tm c | |||
f... : ;, | |||
'y | |||
. l, | |||
! \\ '\\ '.. s. | |||
t- | ?,. | ||
i^ | |||
Deputy Directcr of Recctor Projects Uni ted S t a tes At oni c Energ) C cnm i s s i on DircatorcLe of Licensing Wshi n g t on, DC | \\' | ||
'.r. | |||
mim c414000 K | |||
'yI)"'j v" 1].. / | |||
July 12, 197h | |||
/ | |||
x N::: | |||
t-fir. A. Gi cmbusso | |||
' ~ | |||
Deputy Directcr of Recctor Projects Uni ted S t a tes At oni c Energ) C cnm i s s i on DircatorcLe of Licensing Wshi n g t on, DC 20545 Oc,ar Mr. Gicmbusto: | |||
==Subject:== | ==Subject:== | ||
Abnormal Occurrence | Abnormal Occurrence TI c follo. zing c;currence was repor ted to Mr. Tom Shedlewsky, A.E.C. Region 1 Regulatcry Operations Office en July 3, 1)/h. tir i t ten noti f icat ica was rode to Mr. Jirno s P. O 'Re i l l y, Region 1 Regulatory Operat ions Of f ice on July 3,197h. | ||
TI c follo . zing c;currence was repor ted to Mr. Tom Shedlewsky, A.E.C. Region 1 Regulatcry Operations Office en July 3, 1)/h. tir i t ten noti f icat ica was rode to Mr. Jirno s P . O 'Re i l l y , Region 1 Regulatory Operat ions Of f ice on July 3,197h. In accordcocc with Section 6.7.2.A of the Technical Specificetions, Appendix A of DPR-44 for Unit 2 Peach Gottor Atcmic Fc,er Static,, the f ol lowing repor t is bein.) suiaitted to the Dirccterate of Licensing as an Abnorraa! Occurrence. | In accordcocc with Section 6.7.2.A of the Technical Specificetions, Appendix A of DPR-44 for Unit 2 Peach Gottor Atcmic Fc,er Static,, the f ol lowing repor t is bein.) suiaitted to the Dirccterate of Licensing as an Abnorraa! Occurrence. | ||
p,r,,,,,.._. | p,r,,,,,.._. | ||
~.._.. | |||
.,....., ~, ~.,,,, c.. u n u,. u n t 5umver i Technica!, ecificction Table 3 1.1 Report 'J a.. | |||
50-277-74-35 Report Date: | |||
July 12, 1974 Occurrence Date: July 2, 1974 Facility: | |||
Peach Bottom Atomic Power Statico R.D. | |||
1, Delta, Pennsylvania l'/314 | |||
. Identification of O_cc_urrence: | |||
Condensor i cr. i vacuum scrcm pressure switch setpoint found to j | Condensor i cr. i vacuum scrcm pressure switch setpoint found to j | ||
bc less censer vative than the limiting safety system setting. | |||
Condit ions Pr ion t o Occurrence: | t Condit ions Pr ion t o Occurrence: | ||
The reactor was at 39,/, pcwer. | The reactor was at 39,/, pcwer. | ||
l | l Pa sc r ip t i on r Occurr'nte: | ||
D ur i ng a . c.o t i ne i n s t r o:ra t surveillence test of P5-2-5-ilA, main condenser le.s vacuu irip input into the reactor protectic-n system, the sub jec t switch was found to trip at 19.2 in. Hg. Tiiis is j.8 in. tl3 | e D ur i ng a. c.o t i ne i n s t r o:ra t surveillence test of P5-2-5-ilA, main condenser le.s vacuu irip input into the reactor protectic-n system, the sub jec t switch was found to trip at 19.2 in. Hg. | ||
Tiiis is j.8 in. tl3 less c onrcrvative than the Technical '.pec i f i ca t i on s rp 'nt of greater than or equal t o '!? i n, lig. | |||
G401270126 740712 PDR | G401270126 740712 PDR ADOCK 05000277 e | ||
a | PDR a | ||
tot'i DENT REGIbh 'Mw | |||
Mr. A. Giar. basso July 12, 1974 | Mr. A. Giar. basso p | ||
v' Page 2 pesignation of Apnacent cause of crcurrence: | July 12, 1974 v' | ||
Page 2 pesignation of Apnacent cause of crcurrence: | |||
Se rpoi n t failure is attributed to instrument drift. | Se rpoi n t failure is attributed to instrument drift. | ||
Analysis of Occurrence: | Analysis of Occurrence: | ||
PS-2-5.llA is one channel in a one-out-of-two-twice logic arrangement. The setpoint foilure would net have preven ted t he eevice tran initiating a trip signal. The protection p ovided by tha other three channels 0+ condenser vacuum voald have becn sat isf actory fr ea a standpoint of clant s a f e t :, . Therefore, thi ., ccourrcnce Ses raininal safety implications. | PS-2-5.llA is one channel in a one-out-of-two-twice logic arrangement. The setpoint foilure would net have preven ted t he eevice tran initiating a trip signal. | ||
Corrective Action: | The protection p ovided by tha other three channels 0+ condenser vacuum voald have becn sat isf actory fr ea a standpoint of clant s a f e t :,. Therefore, thi., ccourrcnce Ses raininal safety implications. | ||
Tha . subject switch was immediately recc.!ibrated, checked fur setpoint repeat ibili ty and returned t o service. The ot her thrce | Corrective Action: | ||
Tha. subject switch was immediately recc.!ibrated, checked fur setpoint repeat ibili ty and returned t o service. The ot her thrce d tchra monitoring condenser vacuum end providing the RPS inpats were irned i a t e l y tested cr.d founa t o be s a t i s f a c t r;r y. | |||
Foilure Data: | Foilure Data: | ||
.This is the fourth setpoint f ailure of this type of de ice in this service. | |||
PS-2-5-!!A cn w ear- '; . 1974 IS-2-5-;iD en scanuary [ ly/4 PS-2-5-i l A on Apr i l 8, 1974 | Other occurrences are as follo',s: | ||
After the two setpoint f ailures of PS11A. the device was rc-placed in kind. Tnis f ailure is the fir st se t p a i n t failure of the re-placement device. | PS-2-5-!!A cn w ear- ';. 1974 IS-2-5-;iD en scanuary [ ly/4 PS-2-5-i l A on Apr i l 8, 1974 After the two setpoint f ailures of PS11A. the device was rc-placed in kind. Tnis f ailure is the fir st se t p a i n t failure of the re-placement device. | ||
'e y t r u l y ycar s, | |||
i l.!j /] | |||
l .!j /] | / | ||
4 / | |||
/ ;/c/p,,<J v; | |||
/ | |||
(;31 Park Avenuc King of Prussia, PA | 4 M. i. C oeney A s s' ' t Gen ' l S uper. iintendent Gt'ocr a t i on fii v i s i on ec: | ||
Mr. J. P. O'Reilly Director, Region i Uni ted St ate s At e:nic Energy Cov.ission | |||
(;31 Park Avenuc King of Prussia, PA 19406 | |||
.}} | |||
Latest revision as of 01:56, 14 December 2024
| ML20086K462 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 07/12/1974 |
| From: | Cooney M PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | Anthony Giambusso US ATOMIC ENERGY COMMISSION (AEC) |
| Shared Package | |
| ML20086K464 | List: |
| References | |
| AO-74-35, NUDOCS 8401270126 | |
| Download: ML20086K462 (2) | |
Text
'
O O
a in PHILAD ELPHIA ELECTRIC COM PANY
- Q '+,;J ^ >
, k,/ 7.,,
V'4 s
-(
//,
,- s 2301 M ARKET STREET
~,?. \\/
']h.-
PHIL A DEL.PH I A. PA.19101 i.
'.,,:, V,( _. (, <
tm c
f... : ;,
'y
. l,
! \\ '\\ '.. s.
?,.
i^
\\'
'.r.
mim c414000 K
'yI)"'j v" 1].. /
July 12, 197h
/
x N:::
t-fir. A. Gi cmbusso
' ~
Deputy Directcr of Recctor Projects Uni ted S t a tes At oni c Energ) C cnm i s s i on DircatorcLe of Licensing Wshi n g t on, DC 20545 Oc,ar Mr. Gicmbusto:
Subject:
Abnormal Occurrence TI c follo. zing c;currence was repor ted to Mr. Tom Shedlewsky, A.E.C. Region 1 Regulatcry Operations Office en July 3, 1)/h. tir i t ten noti f icat ica was rode to Mr. Jirno s P. O 'Re i l l y, Region 1 Regulatory Operat ions Of f ice on July 3,197h.
In accordcocc with Section 6.7.2.A of the Technical Specificetions, Appendix A of DPR-44 for Unit 2 Peach Gottor Atcmic Fc,er Static,, the f ol lowing repor t is bein.) suiaitted to the Dirccterate of Licensing as an Abnorraa! Occurrence.
p,r,,,,,.._.
~.._..
.,....., ~, ~.,,,, c.. u n u,. u n t 5umver i Technica!, ecificction Table 3 1.1 Report 'J a..
50-277-74-35 Report Date:
July 12, 1974 Occurrence Date: July 2, 1974 Facility:
Peach Bottom Atomic Power Statico R.D.
1, Delta, Pennsylvania l'/314
. Identification of O_cc_urrence:
Condensor i cr. i vacuum scrcm pressure switch setpoint found to j
bc less censer vative than the limiting safety system setting.
t Condit ions Pr ion t o Occurrence:
The reactor was at 39,/, pcwer.
l Pa sc r ip t i on r Occurr'nte:
e D ur i ng a. c.o t i ne i n s t r o:ra t surveillence test of P5-2-5-ilA, main condenser le.s vacuu irip input into the reactor protectic-n system, the sub jec t switch was found to trip at 19.2 in. Hg.
Tiiis is j.8 in. tl3 less c onrcrvative than the Technical '.pec i f i ca t i on s rp 'nt of greater than or equal t o '!? i n, lig.
G401270126 740712 PDR ADOCK 05000277 e
PDR a
tot'i DENT REGIbh 'Mw
Mr. A. Giar. basso p
July 12, 1974 v'
Page 2 pesignation of Apnacent cause of crcurrence:
Se rpoi n t failure is attributed to instrument drift.
Analysis of Occurrence:
PS-2-5.llA is one channel in a one-out-of-two-twice logic arrangement. The setpoint foilure would net have preven ted t he eevice tran initiating a trip signal.
The protection p ovided by tha other three channels 0+ condenser vacuum voald have becn sat isf actory fr ea a standpoint of clant s a f e t :,. Therefore, thi., ccourrcnce Ses raininal safety implications.
Corrective Action:
Tha. subject switch was immediately recc.!ibrated, checked fur setpoint repeat ibili ty and returned t o service. The ot her thrce d tchra monitoring condenser vacuum end providing the RPS inpats were irned i a t e l y tested cr.d founa t o be s a t i s f a c t r;r y.
Foilure Data:
.This is the fourth setpoint f ailure of this type of de ice in this service.
Other occurrences are as follo',s:
PS-2-5-!!A cn w ear- ';. 1974 IS-2-5-;iD en scanuary [ ly/4 PS-2-5-i l A on Apr i l 8, 1974 After the two setpoint f ailures of PS11A. the device was rc-placed in kind. Tnis f ailure is the fir st se t p a i n t failure of the re-placement device.
'e y t r u l y ycar s,
i l.!j /]
/
4 /
/ ;/c/p,,<J v;
/
4 M. i. C oeney A s s' ' t Gen ' l S uper. iintendent Gt'ocr a t i on fii v i s i on ec:
Mr. J. P. O'Reilly Director, Region i Uni ted St ate s At e:nic Energy Cov.ission
(;31 Park Avenuc King of Prussia, PA 19406
.