ENS 40348: Difference between revisions

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| event date = 11/21/2003 09:10 EST
| event date = 11/21/2003 09:10 EST
| last update date = 11/21/2003
| last update date = 11/21/2003
| title = Control Bank "C"  Rods Tripped Due To Incorrect  Digital Rod Position Indication (Drpi)
| title = Control Bank "C"  Rods Tripped Due to Incorrect  Digital Rod Position Indication (Drpi)
| event text = On Friday November 21, 2003, the V.C. Summer Nuclear Station was performing rod position testing in preparation for plant start-up, following refueling outage-14.  The testing is in accordance with STP-106.002 Rod Position Indication Operational Test.  Control Bank 'C'  was being withdrawn. Per STP-106.002, RCS boron concentration was verified adequate to ensure Keff less than or equal to 0.95.  When Control Bank 'C' reached 36 steps Digital Rod Position Indication system (DRPI)  indication for rod M-4 went to 18 steps.  At 0835, Control Rod motion was stopped and Abnormal Operating Procedure (AOP)-403.5, Stuck or Misaligned Control Rod, was entered after reviewing the AOP applicability versus current plant condition.  At 0910 while taking action per the AOP, it was determined that both channels of DRPI were not functioning properly and per Tech Spec 3.10.5 the Rx Trip Breakers were immediately opened (manual actuation of the Reactor Protection System - reactor scram).  Emergency Operating Procedure (EOP)-1.0, Reactor Trip, was entered.  At 0915 EOP-1.0, was exited with the plant stable in Mode 3 (Hot Standby).
| event text = On Friday November 21, 2003, the V.C. Summer Nuclear Station was performing rod position testing in preparation for plant start-up, following refueling outage-14.  The testing is in accordance with STP-106.002 Rod Position Indication Operational Test.  Control Bank 'C'  was being withdrawn. Per STP-106.002, RCS boron concentration was verified adequate to ensure Keff less than or equal to 0.95.  When Control Bank 'C' reached 36 steps Digital Rod Position Indication system (DRPI)  indication for rod M-4 went to 18 steps.  At 0835, Control Rod motion was stopped and Abnormal Operating Procedure (AOP)-403.5, Stuck or Misaligned Control Rod, was entered after reviewing the AOP applicability versus current plant condition.  At 0910 while taking action per the AOP, it was determined that both channels of DRPI were not functioning properly and per Tech Spec 3.10.5 the Rx Trip Breakers were immediately opened (manual actuation of the Reactor Protection System - reactor scram).  Emergency Operating Procedure (EOP)-1.0, Reactor Trip, was entered.  At 0915 EOP-1.0, was exited with the plant stable in Mode 3 (Hot Standby).
At this time it appears there was failure in the DRPI system.
At this time it appears there was failure in the DRPI system.

Latest revision as of 21:24, 1 March 2018

ENS 40348 +/-
Where
Summer South Carolina Electric & Gas Company icon.png
South Carolina (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+1.6 h0.0667 days <br />0.00952 weeks <br />0.00219 months <br />)
Opened: Phil Rose
15:46 Nov 21, 2003
NRC Officer: John Mackinnon
Last Updated: Nov 21, 2003
40348 - NRC Website
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