ENS 40454: Difference between revisions

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| event date = 01/16/2004 11:37 EST
| event date = 01/16/2004 11:37 EST
| last update date = 01/16/2004
| last update date = 01/16/2004
| title = Automatic Reactor Trip Due To Turbine Trip
| title = Automatic Reactor Trip Due to Turbine Trip
| event text = At 1137 hours EST on January 16, 2004, with Watts Bar Unit 1 in Mode 1 at 100 % power, a turbine trip and reactor trip occurred.  This is reportable as a 4-hour notification under 10 CFR 50.72 (b)(2)(iv)(B) and an 8-hour notification under 10 CFR 50.72 (b)(3)(iv)(A).  In addition, per design, there was auto start of the Auxiliary Feedwater system which is reportable as an 8-hour notification under 10 CFR 50.72 (b)(3)(iv)(A).  Plant safety systems performed as designed and the reactor is currently stable in mode 3.
| event text = At 1137 hours EST on January 16, 2004, with Watts Bar Unit 1 in Mode 1 at 100 % power, a turbine trip and reactor trip occurred.  This is reportable as a 4-hour notification under 10 CFR 50.72 (b)(2)(iv)(B) and an 8-hour notification under 10 CFR 50.72 (b)(3)(iv)(A).  In addition, per design, there was auto start of the Auxiliary Feedwater system which is reportable as an 8-hour notification under 10 CFR 50.72 (b)(3)(iv)(A).  Plant safety systems performed as designed and the reactor is currently stable in mode 3.
At the time of the trip, plant personnel were performing scheduled Solid State Protection System (SSPS) surveillance testing on the B Train Reactor Trip Breaker.  Plant personnel are currently investigating the cause of the event.
At the time of the trip, plant personnel were performing scheduled Solid State Protection System (SSPS) surveillance testing on the B Train Reactor Trip Breaker.  Plant personnel are currently investigating the cause of the event.

Latest revision as of 22:24, 1 March 2018

ENS 40454 +/-
Where
Watts Bar Tennessee Valley Authority icon.png
Tennessee (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.82 h-0.118 days <br />-0.0168 weeks <br />-0.00386 months <br />)
Opened: Steve Smith
13:48 Jan 16, 2004
NRC Officer: Gerry Waig
Last Updated: Jan 16, 2004
40454 - NRC Website
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