ENS 41414: Difference between revisions

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| event date = 02/16/2005 21:12 EST
| event date = 02/16/2005 21:12 EST
| last update date = 02/17/2005
| last update date = 02/17/2005
| title = Reactor Trip Due To Turbine Trip As A Result Of Failed Power Supply
| title = Reactor Trip Due to Turbine Trip as a Result of Failed Power Supply
| event text = Ginna Station received a reactor trip from Turbine Trip at 2112 hrs on 02/16/05.  The Turbine Trip signal was generated from the ATWS Mitigation System Actuation Circuitry (AMSAC) related to a failed power supply in the Advanced Digital Feedwater Control System.  All control rods inserted on the reactor trip.  The plant is currently stable in Mode 3, RCS Pressure 2235 psig, Temperature 540 deg F.  AFW [Auxiliary Feed Water] did actuate as designed after the trip.
| event text = Ginna Station received a reactor trip from Turbine Trip at 2112 hrs on 02/16/05.  The Turbine Trip signal was generated from the ATWS Mitigation System Actuation Circuitry (AMSAC) related to a failed power supply in the Advanced Digital Feedwater Control System.  All control rods inserted on the reactor trip.  The plant is currently stable in Mode 3, RCS Pressure 2235 psig, Temperature 540 deg F.  AFW [Auxiliary Feed Water] did actuate as designed after the trip.
For the transient, min & max Temperatures, Pressures & Levels are:
For the transient, min & max Temperatures, Pressures & Levels are:

Latest revision as of 21:21, 1 March 2018

ENS 41414 +/-
Where
Ginna Constellation icon.png
New York (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.9 h-0.0792 days <br />-0.0113 weeks <br />-0.0026 months <br />)
Opened: Peter Bramford
00:18 Feb 17, 2005
NRC Officer: Mike Ripley
Last Updated: Feb 17, 2005
41414 - NRC Website
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