ENS 46020: Difference between revisions
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| event date = 06/16/2010 19:20 EDT | | event date = 06/16/2010 19:20 EDT | ||
| last update date = 06/16/2010 | | last update date = 06/16/2010 | ||
| title = Automatic Reactor Trip Due | | title = Automatic Reactor Trip Due to a Lightning Storm | ||
| event text = On 6-16-2010 at 1920 hours, Unit 2 experienced an automatic reactor trip/turbine trip from 98% power. A severe lightning storm was in progress at the time of the trip and a lightning strike appears to be the cause of the event. The reactor trip was actuated from Channel 1 and Channel 2 Over Temperature Delta T. All control rods fully inserted into the core during the trip. The control room staff responded to the trip in accordance with plant procedures and the unit is stable in Mode 3. This event is reportable per 10CFR50.72(b)(2)(iv)(B). | | event text = On 6-16-2010 at 1920 hours, Unit 2 experienced an automatic reactor trip/turbine trip from 98% power. A severe lightning storm was in progress at the time of the trip and a lightning strike appears to be the cause of the event. The reactor trip was actuated from Channel 1 and Channel 2 Over Temperature Delta T. All control rods fully inserted into the core during the trip. The control room staff responded to the trip in accordance with plant procedures and the unit is stable in Mode 3. This event is reportable per 10CFR50.72(b)(2)(iv)(B). | ||
The Auxiliary Feedwater pumps started as designed following the reactor trip and steam generator inventory was restored to normal operating level. The Auxiliary Feedwater pumps have been secured and returned to automatic. This event is reportable per 10CFR50.72(b)(3)(iv)(A) due to the ESF actuation. | The Auxiliary Feedwater pumps started as designed following the reactor trip and steam generator inventory was restored to normal operating level. The Auxiliary Feedwater pumps have been secured and returned to automatic. This event is reportable per 10CFR50.72(b)(3)(iv)(A) due to the ESF actuation. |
Latest revision as of 21:09, 1 March 2018
Where | |
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North Anna Virginia (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-2.2 h-0.0917 days <br />-0.0131 weeks <br />-0.00301 months <br />) | |
Opened: | Page Kemp 21:08 Jun 16, 2010 |
NRC Officer: | Dong Park |
Last Updated: | Jun 16, 2010 |
46020 - NRC Website
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