ENS 49432: Difference between revisions

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| event date = 10/13/2013 04:20 EDT
| event date = 10/13/2013 04:20 EDT
| last update date = 10/13/2013
| last update date = 10/13/2013
| title = Secondary Containment Differential Pressure At Zero Inches Water Gauge
| title = Secondary Containment Differential Pressure at Zero Inches Water Gauge
| event text = On October 13, 2013 at 0420 [EDT], Susquehanna Steam Electric Station control room operators received an alarm for a local secondary containment ventilation control panel.  Investigation revealed that Zone II (Unit 2 Reactor Building) secondary containment differential pressure was at zero inches water gauge.  Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge.  All fans and dampers appeared to be operating normally and there was no apparent equipment malfunction.  Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable.
| event text = On October 13, 2013 at 0420 [EDT], Susquehanna Steam Electric Station control room operators received an alarm for a local secondary containment ventilation control panel.  Investigation revealed that Zone II (Unit 2 Reactor Building) secondary containment differential pressure was at zero inches water gauge.  Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge.  All fans and dampers appeared to be operating normally and there was no apparent equipment malfunction.  Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable.
Zone II differential pressure recovered within five minutes and was verified to be stable.  LCO 3.6.4.1 was entered for both units at 0420 and exited at 0425.
Zone II differential pressure recovered within five minutes and was verified to be stable.  LCO 3.6.4.1 was entered for both units at 0420 and exited at 0425.

Latest revision as of 21:59, 1 March 2018

ENS 49432 +/-
Where
Susquehanna Talen Energy icon.png
Pennsylvania (NRC Region 1)
Reporting
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Time - Person (Reporting Time:+0.85 h0.0354 days <br />0.00506 weeks <br />0.00116 months <br />)
Opened: Alexander Mclellan
09:11 Oct 13, 2013
NRC Officer: John Shoemaker
Last Updated: Oct 13, 2013
49432 - NRC Website
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