ENS 49796: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by Mark Hawes)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 02/05/2014 13:00 EST
| event date = 02/05/2014 13:00 EST
| last update date = 02/05/2014
| last update date = 02/05/2014
| title = Degraded Condition Discovered On Pressurizer Nozzle Weld During Testing
| title = Degraded Condition Discovered on Pressurizer Nozzle Weld During Testing
| event text = On February 5, 2014, during planned inspections, an ultrasonic examination performed on weld PCS-6-PRS-1C1-1 (RV-1041) revealed two axial indications in the root area of the weld. The weld containing the indications is the nozzle to safe end dissimilar metal weld on the flange for pressurizer safety valve RV-1041. These two indications do not meet applicable acceptance criteria under ASME, Section XI, IWB-3600,  'Analytical Evaluation of Flaws,'  or ASME Section Xl, Table IWB-3410, 'Acceptance Standards,'  and will require a repair or replacement activity in order return the weld to an acceptable condition.
| event text = On February 5, 2014, during planned inspections, an ultrasonic examination performed on weld PCS-6-PRS-1C1-1 (RV-1041) revealed two axial indications in the root area of the weld. The weld containing the indications is the nozzle to safe end dissimilar metal weld on the flange for pressurizer safety valve RV-1041. These two indications do not meet applicable acceptance criteria under ASME, Section XI, IWB-3600,  'Analytical Evaluation of Flaws,'  or ASME Section Xl, Table IWB-3410, 'Acceptance Standards,'  and will require a repair or replacement activity in order return the weld to an acceptable condition.
The plant was in cold shutdown at 0% power for a planned refueling outage at the time of discovery. Replacement or repair actions will be completed prior to plant startup from the outage.
The plant was in cold shutdown at 0% power for a planned refueling outage at the time of discovery. Replacement or repair actions will be completed prior to plant startup from the outage.

Latest revision as of 21:51, 1 March 2018

ENS 49796 +/-
Where
Palisades Entergy icon.png
Michigan (NRC Region 3)
Reporting
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Time - Person (Reporting Time:+-1.72 h-0.0717 days <br />-0.0102 weeks <br />-0.00236 months <br />)
Opened: Barb Dotson
16:17 Feb 5, 2014
NRC Officer: Jeff Rotton
Last Updated: Feb 5, 2014
49796 - NRC Website
Loading map...