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=Text=
=Text=
{{#Wiki_filter:_.
{{#Wiki_filter:_.
t
,. i-- ?.
        ,. i-- ?.                 _
t gg MEMORANDUM FOR:.
gg MEMORANDUM FOR:.       Charles E. Rossi, Director a  <
Charles E. Rossi, Director Division of Operational Events Assessment.
Division of Operational Events Assessment .
a FROM:
FROM:               -Wayne Lanning, Acting Chief Events Assessment Branch Division of Operational Events Assessment
-Wayne Lanning, Acting Chief Events Assessment Branch Division of Operational Events Assessment


==SUBJECT:==
==SUBJECT:==
SUPMARY 0F THE OPERATING REACTORS EVENTS
SUPMARY 0F THE OPERATING REACTORS EVENTS
:. MEETING ON APRIL 20, 1987 - MEETING 87-11 On April 20, 1987, an Operating Reactors Events meeting (87-11)'was held to brief senior managers from NRR, RES, AEOD and Regional Offices en events which occurred since our last meeting on April _ 6,1987. The list ~of' attendees is included as Enclosure'1.
:. MEETING ON APRIL 20, 1987 - MEETING 87-11 On April 20, 1987, an Operating Reactors Events meeting (87-11)'was held to brief senior managers from NRR, RES, AEOD and Regional Offices en events which occurred since our last meeting on April _ 6,1987. The list ~of' attendees is included as Enclosure'1.
The events discussed and the significant elements of these events are presented in Enclosure 2. Enclosure 3 provides a summary of those presented events that will be input to NRC's performance indicator program as significant events.
The events discussed and the significant elements of these events are presented in Enclosure 2. provides a summary of those presented events that will be input to NRC's performance indicator program as significant events.
Od; int Siimed By:
Od; int Siimed By:
Wayne Lanning, . Acting Chief Events. Assessment Branch Division of Operational Events Assessment
Wayne Lanning,. Acting Chief Events. Assessment Branch Division of Operational Events Assessment


==Enclosures:==
==Enclosures:==
As stated i
As stated i
cc'w/ Encl.:
cc'w/ Encl.:
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cc w/ Encl.:
cc w/ Encl.:
See Next Page
See Next Page
                          -DISTRIBUTION g m 70 NRC PDR EAB-Rdg Oudinot Rdg w/o Enclosure EAB Members i
-DISTRIBUTION g m 70 NRC PDR EAB-Rdg Oudinot Rdg w/o Enclosure EAB Members i
a
a
                          .(SEE'ATTACHEDFORPREVIOUSCONCURRENCES*)                                                                                     h PWR:EAB*             SL:PWR:EAB*                     SL:BWR:EAB*     Al     EAB                                             j DOUDINOT             RLOBEL                         PBARAN0WSKY     W:     G                                     g 4/30/87               4/30/87                       5/1/87         5/r/87                                         Q /g/gf g i ,i v
.(SEE'ATTACHEDFORPREVIOUSCONCURRENCES*)
                                                                                                                                                    ^l guan"9 870505 m%         -                                                                                    p'
h PWR:EAB*
SL:PWR:EAB*
SL:BWR:EAB*
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g /g/g DOUDINOT RLOBEL PBARAN0WSKY W:
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                                        ,                                                                ,,:          -                                          '1 i                                 ,
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              '                                    f                                                            -
MEMORANDUM FOR:
      .                      MEMORANDUM FOR:                             Charles E." Rossi, Director                                         ..
Charles E." Rossi, Director i
i              ' Division of Operational Events Assessment                                                       ,
' Division of Operational Events Assessment
g:                                      \'             L' a           _
\\'
l is:         J           : FROM: -                   \                 Wayne Lanning,; Acting Chief                                                                   i z
L' a
1 4\      ';
g:
                                                                      ' Events . Assessment ' Branch Division of.0perational Events Assessment
is:
                                                                                                                                            ~
J
j u
: FROM: -
4 i          
\\
Wayne Lanning,; Acting Chief i
1 4
' Events. Assessment ' Branch
~
j
\\
Division of.0perational Events Assessment z
4 u
 
==SUBJECT:==
i


==SUMMARY==
==SUMMARY==
,0F THE. OPERATING REACTORS EVENTS
,0F THE. OPERATING REACTORS EVENTS
 
'y
==SUBJECT:==
.PEETING ON APRIL-20,- 1987J : MEETING 87 \\
                                                          'y         .PEETING ON APRIL-20,- 1987J : MEETING 87                     .              ,
r
                                                              \                                      r
~
                                                        ~
~
                                                                                                                                                  ~
. On April 20, 1987, an Operating Reactors Events meeting (87-11) was held to -
                      . On April 20, 1987, an Operating Reactors Events meeting (87-11) was held to -
brief the Offic'e Director, the: Division Directors and their! representatives on
brief the Offic'e Director, the: Division Directors and their! representatives on 4
' events which occurred sincefour last meeting on April 6,.1987. The list of:
                          ' events which occurred sincefour last meeting on April 6, .1987. The list of:
4 attendees is.inc.luded as Enclosure 1.
attendees is .inc.luded           ,
Yheeventsdiscu$sedandthe'significantelementsoftheseeventsarepresentedt in Enclosure 2. provides a summary of.those presented events'that-will be input:to N,RC's perfomance-indicator program as significant events.
as Enclosure 1.
)
Yheeventsdiscu$sedandthe'significantelementsoftheseeventsarepresentedt in Enclosure 2. Enclosure 3 provides a summary of.those presented events'that-will be input:to N,RC's perfomance-indicator program as significant events.
; ~
                                                                  )i                                                                                                '
i
;~                                                                   \-
\\-
                                                                      \
\\
                                                                        '\ .                                     Wayne Lanning, Acting Chief i                                       Events Assessment Branch i                                       Division of Operational Events _ Assessment
'\\.
                                                                          \
Wayne Lanning, Acting Chief i
Events Assessment Branch i
Division of Operational Events _ Assessment
\\'


==Enclosures:==
==Enclosures:==
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cc'w/ Encl.:
cc'w/ Encl.:
k See Next Page w cc w/ Encl.:
k See Next Page w cc w/ Encl.:
:                            See.Next Page                                             i t
See.Next Page i
'                                                                                        \
t
                                                                                          \
\\
DISTRIBUTION
DISTRIBUTION
                          ' Central. File                                                 '\
\\
NRC PDR                                                         \
' Central. File
EAB'Rdg Oudinot Rdg w/o Enclosure
'\\
                                                                                              \ g EAB Members                                                         i
NRC PDR
                                                                                                    \
\\
                                                                                                ~\
EAB'Rdg
                                                                                                        \
\\
Oudinot Rdg w/o Enclosure g
EAB Members i
\\
~\\
\\
(SEE ATTACHED FOR PREVIOUS CONCURRENCES *)
(SEE ATTACHED FOR PREVIOUS CONCURRENCES *)
                                                                                                          \
\\
              ;.          .PWR:EAB*                                     SL:PWR:EAB*                       \             SL:PWR:EAB*           ACT.BC:EAB
.PWR:EAB*
                          '.D00 DIN 0T                                  RLOBEL                                          PBARANOWSKY            WLANNING-
SL:PWR:EAB*
\\
SL:PWR:EAB*
ACT.BC:EAB
\\
[.
[.
l                           4/30/87                                     4/30/87                             \ s        .S/1/87                     / /87 i
'.D00 DIN 0T RLOBEL PBARANOWSKY WLANNING-l 4/30/87 4/30/87
m
.S/1/87
/ /87 s
i m


                                                                  ,                                                                  m        _
r ~' '..
r ~' '..                                 >    <                                                    g.
m g.
k               ;.        . -*          ez 3x                   .
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                                                                =                             .
=
3                             PEMORANDUM FOR:-                         Thomas E. Murley, . Director.
3 PEMORANDUM FOR:-
                                                                                ;0ffice of Nuclear. Reactor.' Regulation
Thomas E. Murley,. Director.
: i.                 "
;0ffice of Nuclear. Reactor.' Regulation i.
FROM:                                  . Wayne Lanning, Acting Chief Events Assessment Branch                                 ... .
. Wayne Lanning, Acting Chief FROM:
    ;                                                                            : Division of' Operational Events Assessment-                                                                 ,
Events Assessment Branch
SUB ECT:                        
: Division of' Operational Events Assessment-SUB ECT:


==SUMMARY==
==SUMMARY==
0FLTHE OPERATING REACTORS EVENTS                                                       -
0FLTHE OPERATING REACTORS EVENTS PEETING ON 1987 - MEETING 87-dn Apriig20,,1987, an ~0peratina-Peactor Events meeting (87-11) was held to.
PEETING ON                                           1987 - MEETING 87-
~
                                                                    ~
.i
dn Apriig20, ,1987, an ~0peratina-Peactor Events meeting (87-11) was held to .                                                                                               .i
~brief the Office. Director, the Division Directors and their representatives on '
                                      ~brief the Office. Director, the Division Directors and their representatives on '                                                                                               ,
events which occurred:since our last meeting on~ April 6,1987. The list _of.
events which occurred:since our last meeting on~ April 6,1987. The list _of.                                                                         <-
attendees is, included as En' closure 1.
attendees is, included as En' closure 1.                                                      .
S; The events' discussed and the'significant elements of these. events' are presented in Enclosure 2g-; Enclosure 3 provides a summary of:those presented events that will be input to NRC's-performance indicator program as.significant events.
S;       _
\\.
The events' discussed and the'significant elements of these. events' are presented in Enclosure 2g-; Enclosure 3 provides a summary of:those presented events that will be input to NRC's- performance indicator program as .significant events.                                                                                   -
\\.
                                                                        \.
s
                                          ,                              \.
.\\
s                                                               .
\\
                                                                            .\
Wayne Lanning, Acting Chief
                                                                                \
\\..
Wayne Lanning, Acting Chief _
Events Assessment Branch N
                                                                                \.. N
Division of Operational Events Assessment s
                                                                                                                .      Events Assessment Branch Division of Operational Events Assessment s       .
Enclosures
              ,                        Enclosures           ^
^
                                      'As stated ~                           '
' >-y
                                                                                      ' >-y cc w/ Encl.:                                               ,
'As stated ~
See Next Page                                               ;                                x cc w/ Encl..                                                                                                           .
cc w/ Encl.:
                                                                                                          =\
See Next Page x
See Next Page-                                                                                                       -
cc w/ Encl..
DI'STRIBUTION                                                                                                                                                                 .
See Next Page-
                                      ' Central File                                                               %
=\\
                                      .NRC PDR-                                                                     s 4                EAB Rdg. _                                                                   \
DI'STRIBUTION
Oudinot Rdg w/o Enclosure                                                       \
' Central File
1EAB Members L                                                                                                                         \
.NRC PDR-s EAB Rdg. _
:x                                                                           .
\\
c h
4 Oudinot Rdg w/o Enclosure
UDIN0T SL:PWR:EAB RLOBEL SL:BWR:EAB PBARAN0WSKY ACT.BC:EAB WLANNING
\\
                                              /#/87                             J g /87                                         6/[/87-                 ./ '/87 p                                                                                                                                                         >
1EAB Members L
1                         -      +
\\
b
:x h
            ,                  y l
SL:PWR:EAB SL:BWR:EAB ACT.BC:EAB c
UDIN0T RLOBEL PBARAN0WSKY WLANNING
/#/87 J g /87 6/[/87-
./ '/87 p
1
+
b l
y


9
9
  *,;      ~
~
              ,a nuou,
,a nuo,
* o,                         UNITED STATES
u o,
        !S               n            NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20565 O                 j 1,,.....,/                                   mr: arr MEMORANDUM FOR:     Charles E. Rossi, Director Division of Operational Events Assessment
UNITED STATES
                  -FROM:               Wayne Lanning, Acting Chief                         .
!S NUCLEAR REGULATORY COMMISSION n
Events Assessment Branch Division of Operational Events Assessment     ,
WASHINGTON, D. C. 20565 O
j 1,,.....,/
mr:
arr MEMORANDUM FOR:
Charles E. Rossi, Director Division of Operational Events Assessment
-FROM:
Wayne Lanning, Acting Chief Events Assessment Branch Division of Operational Events Assessment


==SUBJECT:==
==SUBJECT:==
==SUMMARY==
==SUMMARY==
OF THE OPERATING REACTORS EVENTS.
OF THE OPERATING REACTORS EVENTS.
MEETING ON APRIL 20, 1987 - MEETING 87-11 On April 20, 1987, an Operating Reactors. Events meeting -(87-1k)J was held to
MEETING ON APRIL 20, 1987 - MEETING 87-11 On April 20, 1987, an Operating Reactors. Events meeting -(87-1k)J was held to
                  .brief senior managers from NRR, RES, AEOD and Regional Offices, on e' vents which occurred since our last meeting on April 6,1987. The list'of attendees is included as Enclosure 1.
.brief senior managers from NRR, RES, AEOD and Regional Offices, on e' vents which occurred since our last meeting on April 6,1987. The list'of attendees is included as Enclosure 1.
The events discussed and the significant elements of these events are presented in Enclosure 2. Enclosure 3 provides a summary of those presented events that will be input to NRC's performance indicator program as significant events.
The events discussed and the significant elements of these events are presented in Enclosure 2. provides a summary of those presented events that will be input to NRC's performance indicator program as significant events.
                                                            ,/
,/
                                                        ))W Waynd Lanning, Ac ing hief
))W Waynd Lanning, Ac ing hief Events Assessment Division of Operational Events Assessment
;                                                          Events Assessment Division of Operational Events Assessment


==Enclosures:==
==Enclosures:==
As stated cc w/ Encl.:
As stated cc w/ Encl.:
See Next Page l
See Next Page l


I-Those Listed-                   .                                                                                    .
I-Those Listed-.
                                    . ~ .          . ...    -  --    -        -.  .
. ~.
cc: . T. . Murley -                   J. Crews, Reg. Y J. Sniezek                     C. Trammell-J. Taylor                     H. Schierling E. Jordan                     G. Knighton E. Beckjord                   H. Pastis W. Russell, Reg. I             B. Youngblood
cc:. T.. Murley -
                              .J. Nelson Grace, Reg. II       S. Stern B. Davis, Reg. III             J. Calvo R. D. Partin, Reg. IV         S. McNeil J. R. Martin, Reg. V           R. Capra W. Kane, Reg. I L. Reyes, Reg. II C. Norelius, Reg. III E. Johnson, Reg. IV D. Kirsch, Reg. V
J. Crews, Reg. Y J. Sniezek C. Trammell-J. Taylor H. Schierling E. Jordan G. Knighton E. Beckjord H. Pastis W. Russell, Reg. I B. Youngblood
                              .R. Starostecki F. Miraglia S. Varga D. Crutchfield B. Boger G. Lainas G. Holahan F. Schroeder L. Shao J. Partlow B. Grimes F. Congel H. Miller E.- Weiss S. Black T. Partin, EDO E. Merschoff i
.J. Nelson Grace, Reg. II S. Stern B. Davis, Reg. III J. Calvo R. D. Partin, Reg. IV S. McNeil J. R. Martin, Reg. V R. Capra W. Kane, Reg. I L. Reyes, Reg. II C. Norelius, Reg. III E. Johnson, Reg. IV D. Kirsch, Reg. V
__x._                 . _ .
.R. Starostecki F. Miraglia S. Varga D. Crutchfield B. Boger G. Lainas G. Holahan F. Schroeder L. Shao J. Partlow B. Grimes F. Congel H. Miller E.- Weiss S. Black T. Partin, EDO E. Merschoff i
__x._


ENCLOSURE 1 LIST'0F ATTENDEES OPERATING REACTCRS EVENTS BRIEFING (27-11)
ENCLOSURE 1 LIST'0F ATTENDEES OPERATING REACTCRS EVENTS BRIEFING (27-11)
APRIL 21, 1987 NAME           DIVISION                 NAME             DIVISION C. Rossi       NRR                       A. Thadani       NRR W. Lanning     NRR                       R. Scholl         NRR K. Heitner     NRR                       M. Caruso         NRR G. Lainas       NRR                       C. Schulten       NRR P. Baranowsky   NRR                       T. Greene         NRR F. Schroeder   NRR                       J. Calvo         NRR L. Spessard     AE0D                     H. Pastis         NRR J. Youngblood   NRR                       G. Knighton       NRR S. Black       NRR                       J. Shapaker:.   .NRR T. Martin       EDO                       J. Partlow'       NRR T. Chan         NRR                       T. Novak         AE00 R. Lob'el       NRR                       J. Thompson       NRR
APRIL 21, 1987 NAME DIVISION NAME DIVISION C. Rossi NRR A. Thadani NRR W. Lanning NRR R. Scholl NRR K. Heitner NRR M. Caruso NRR G. Lainas NRR C. Schulten NRR P. Baranowsky NRR T. Greene NRR F. Schroeder NRR J. Calvo NRR L. Spessard AE0D H. Pastis NRR J. Youngblood NRR G. Knighton NRR S. Black NRR J. Shapaker:.
:          J. Stefano     NRR                       S. Stern         NRR J. Rosenthal   AEOD                     J. Carter         NRR l         E. Weiss       AEOD                     J. Richardson     NRR B. Grimes       NRR                       H. Miller         NRR L. Shau         NRR                       R. Starostecki   NRR E. Jordan       AE00                     S. Varga         NRR C. Berlinger   NRR                       D. Crutchfield   NRR B. Boger       NRR                       F. Miraglia       NRR W. Minners     DRPS                     G. Holahan       NRR i         W. Swenson     NRR                       D. Oudinot       NRR l
.NRR T. Martin EDO J. Partlow' NRR T. Chan NRR T. Novak AE00 R. Lob'el NRR J. Thompson NRR J. Stefano NRR S. Stern NRR J. Rosenthal AEOD J. Carter NRR l
E. Weiss AEOD J. Richardson NRR B. Grimes NRR H. Miller NRR L. Shau NRR R. Starostecki NRR E. Jordan AE00 S. Varga NRR C. Berlinger NRR D. Crutchfield NRR B. Boger NRR F. Miraglia NRR W. Minners DRPS G. Holahan NRR i
W. Swenson NRR D. Oudinot NRR l
l
l
[
[


ENCLOSURE 2 OPERATING REACTORS EVEtlTS BRIEFING 87-11
ENCLOSURE 2 OPERATING REACTORS EVEtlTS BRIEFING 87-11
  ~
~
APRIL 21, 1987 DIABLO CANYON 2   LOSS OF RESIDUAL HEAT REMOVAL AND RCS THERMAL TRANSIENT OCONEE 1, 2, 8 3   FOULING OF LOW PRESSI'RE SERVICE WATER, LOW PPESSURE INJECTION AND REACT 0P BUILDING COOLING UNITS-UPDATE OCONEE 3           VALVES TO HIGH PRESSURE INJECTION PUMPS ISOLATED OTHER EVENTS OF INTEREST RIVER BEND         QA/0C PP0BLEM FOR PROCESS COMPUTER SOFTWARE CALVERT CLIFFS 1   ESF INADVERTENT ACTUATION OF CONTAINMENT SPRAYS
APRIL 21, 1987 DIABLO CANYON 2 LOSS OF RESIDUAL HEAT REMOVAL AND RCS THERMAL TRANSIENT OCONEE 1, 2, 8 3 FOULING OF LOW PRESSI'RE SERVICE WATER, LOW PPESSURE INJECTION AND REACT 0P BUILDING COOLING UNITS-UPDATE OCONEE 3 VALVES TO HIGH PRESSURE INJECTION PUMPS ISOLATED OTHER EVENTS OF INTEREST RIVER BEND QA/0C PP0BLEM FOR PROCESS COMPUTER SOFTWARE CALVERT CLIFFS 1 ESF INADVERTENT ACTUATION OF CONTAINMENT SPRAYS


4/21/87 DIABLO CANYON 2 LOSS OF RESIDUAL HEAT REM 0"Al AND RCS THERMAL TRANSIENT PROBLEM:
4/21/87 DIABLO CANYON 2 LOSS OF RESIDUAL HEAT REM 0"Al AND RCS THERMAL TRANSIENT PROBLEM:
Line 193: Line 239:
UNPLANNED DRAINAGE-FROM RCS RCS LEVEL INSTRUMENTATION ERPORS P0TENTIAL PROCEDURAL INADEQUACIES SIGNIFICANCE:
UNPLANNED DRAINAGE-FROM RCS RCS LEVEL INSTRUMENTATION ERPORS P0TENTIAL PROCEDURAL INADEQUACIES SIGNIFICANCE:
THERMAL TRANSIENT-TO BOILING CONDITIONS'WAS EXPERIENCFD IN THE RCS WHILE BOTH RCS AND CONTAINMENT EOUNDARIES WERE BREACHED P0TENTIAL FAILURE BY LICENSEE TO CLASSIFY EVENT DISCUSSION:
THERMAL TRANSIENT-TO BOILING CONDITIONS'WAS EXPERIENCFD IN THE RCS WHILE BOTH RCS AND CONTAINMENT EOUNDARIES WERE BREACHED P0TENTIAL FAILURE BY LICENSEE TO CLASSIFY EVENT DISCUSSION:
INITIAL CONDITIONS - MODE 5, CONTAINMENT EQUIPMENT HATCH REMOVED,
INITIAL CONDITIONS - MODE 5, CONTAINMENT EQUIPMENT HATCH REMOVED, STEAM GENERATOR MANWAYS BEING. REMOVED RCS DRAIN D0WN TO MID-LOOP OPERATION COMPLETED ON DAY SHIFT, VORTEXING AT RHR PUMP SUCTION OCCURRED BRIEFLY DURING THIS EVOLllTION UNEXPECTED RCS LEAKAGE COMMENCED AT APPP0XIMATELY 8:30 P.M.
                  .                  STEAM GENERATOR MANWAYS BEING. REMOVED RCS DRAIN D0WN TO MID-LOOP OPERATION COMPLETED ON DAY SHIFT, VORTEXING AT RHR PUMP SUCTION OCCURRED BRIEFLY DURING THIS EVOLllTION UNEXPECTED RCS LEAKAGE COMMENCED AT APPP0XIMATELY 8:30 P.M.
OPERATORS STARTED INVESTIGATING CAUSE RHR PUMP SHUT 0FF BY OPERATORS AT APPR0XIMATELY 9:20 P.M. DUE TO ERRATIC MOTOR CURRENT CONT ' IONS SECOND RHR PUMP STARTED c.i.D PROMPTLY SHUTDOWN DUE TO~SAME CONDITIONS (OPERATORS ATTRIBUTE RHR PUMP BEHAVIOR TO SUSPECTED VORTEXING)
OPERATORS STARTED INVESTIGATING CAUSE RHR PUMP SHUT 0FF BY OPERATORS AT APPR0XIMATELY 9:20 P.M. DUE TO ERRATIC MOTOR CURRENT CONT ' IONS SECOND RHR PUMP STARTED c.i.D PROMPTLY SHUTDOWN DUE TO~SAME CONDITIONS (OPERATORS ATTRIBUTE RHR PUMP BEHAVIOR TO SUSPECTED VORTEXING)
PHR FLOW NOT RESTORED DUE TO UNCERTAINTY REGARDING PRESENCE OF PERSONNEL IN OP NEAR STEAM GENERATORS B0ILING COMMENCED'IN RCS WITHIN APPR0XIMATELY 1 HOUR (N0 RCS TEMPERATURE INDICATION AVAILABLE)
PHR FLOW NOT RESTORED DUE TO UNCERTAINTY REGARDING PRESENCE OF PERSONNEL IN OP NEAR STEAM GENERATORS B0ILING COMMENCED'IN RCS WITHIN APPR0XIMATELY 1 HOUR (N0 RCS TEMPERATURE INDICATION AVAILABLE)
SHIFT FOREMAN DECLARED SIGNIFICANT EVENT (50.72 NOTIFICATION) AT 10:23 P.M. BASED ON EXCEEDING LCO 0F TECHNICAL SPECIFICATIONS
SHIFT FOREMAN DECLARED SIGNIFICANT EVENT (50.72 NOTIFICATION) AT 10:23 P.M. BASED ON EXCEEDING LCO 0F TECHNICAL SPECIFICATIONS
                                                                --  ~
~


                        ^~
^~
  .    .                                                                        l l
l 4/21/87 DIABLO CANYON 2 OPERATORS RESTORED RHR COOLING BY ADDING WATER TO RCS FROM REFUELING WATER STORAGE TANK AND RESTARTING RHR PUMP AT.
4/21/87 DIABLO CANYON 2 OPERATORS RESTORED RHR COOLING BY ADDING WATER TO RCS FROM REFUELING WATER STORAGE TANK AND RESTARTING RHR PUMP AT.
10:48 P.M.
10:48 P.M.
REC 0VERY TO MID-LOOP OPERATION ACHIEVED ON SUNDAY APRIL 12, OPERATORS CONDUCTED SPECIAL TEST TO DETEPMINE POINT OF VORTEXING BY LOWERING RCS LEVEL CONTAINMENT AND RCS INTEGRITY REMAINED BREACHED)
REC 0VERY TO MID-LOOP OPERATION ACHIEVED ON SUNDAY APRIL 12, OPERATORS CONDUCTED SPECIAL TEST TO DETEPMINE POINT OF VORTEXING BY LOWERING RCS LEVEL CONTAINMENT AND RCS INTEGRITY REMAINED BREACHED)
Line 209: Line 253:
J. CREWS, REG. V l
J. CREWS, REG. V l
l l
l l
L .; .    .  . . . _        .
L


April 18, 1987
('
('              -
April 18, 1987 2330 Hrs.
2330 Hrs.
4/10/87 RER EVENT  
4/10/87 RER EVENT  


==SUMMARY==
==SUMMARY==
 
Plant Status:
Plant Status:             The   Unit was in the seventh day of the first refueling outage following The plant was in aMode    shutdown on 4/3/87 at 2352 hrs.
The Unit was in the seventh day of the first refueling outage following a shutdown on 4/3/87 at 2352 hrs.
5 with the reactor coolant system temperature being maintained at approximately 87 F.       Preparations are in progress to install tho steam generator nossle dams.
The plant was in Mode 5 with the reactor coolant system temperature being maintained at approximately 87 F.
Preparations are in progress to install tho steam generator nossle dams.
The reactor vessel level is being maintained at approximately half loop to support the installation of the nossle dams.
The reactor vessel level is being maintained at approximately half loop to support the installation of the nossle dams.
Operational                 - Residual     Heat Removal pump       2-1   is   in     service Conflauration:                 providing flow       through both RHR heat exchangers (trains are cross-tied).
Operational
                .                                - Reactor       vessel   level uis being       maintained       by
- Residual Heat Removal pump 2-1 is in service Conflauration:
          -(,f.
providing flow through both RHR heat exchangers (trains are cross-tied).
V ..                                  balancing letdown flow to the VCT with the charging flow back to         the primary system (constant VCT level).       Letdown is from the RER pump discharge via HCV-133 and charging is by gravity flow from the VCT via the normal charging path (through a non-
- Reactor vessel level uis being maintained by
                                              ,    operating centrifugal charging pump).
-(,f.
                                                - Seactor Coolant System boron concentration is approximately 1997 ppm.                                         '
balancing letdown flow to the VCT with the charging V..
                                            .,  - The     containment equipment hatch and personnel             air 4                                           0       lock are open.         The emergency personnel hatch is closed.     Various jobs are in progress containment and a continuous purge is in inside        progress of with     containment ventilation exhaust fan E-3 discharging through RCV-11 and 12 to the plant vent.
flow back to the primary system (constant VCT level).
Plant Equipment               - Residual Heat Removal pump 2-1 is in service and the Conf.lguration:                 2-2     RHR pump is available for service.                   All instrumentation associated with the RNR system is in service.
Letdown is from the RER pump discharge via HCV-133 and charging is by gravity flow from the VCT via the normal charging path (through a
                                                - Both       Safety   injection pumps are # cleared"           and unavailable for service.
non-operating centrifugal charging pump).
('                                   - Centrifugal Charging Pump 2-2 is   OPERABLE       and available for immediate service.
- Seactor Coolant System boron concentration is approximately 1997 ppm.
CCP 2-1 and the 4- Tmed $ and ts0Wed V M4snkutd<refteh4                              .
- The containment equipment hatch and personnel air 4
ca.a     seet tu                         n m: ass n       i>:se   test se >e
0 lock are open.
The emergency personnel hatch is closed.
Various jobs are in progress inside of containment and a continuous purge is in progress with containment ventilation exhaust fan E-3 discharging through RCV-11 and 12 to the plant vent.
Plant Equipment
- Residual Heat Removal pump 2-1 is in service and the Conf.lguration:
2-2 RHR pump is available for service.
All instrumentation associated with the RNR system is in service.
- Both Safety injection pumps are # cleared" and unavailable for service.
('
- Centrifugal Charging Pump 2-2 is OPERABLE and available for immediate service.
CCP 2-1 and the 4-Tmed $ and ts0Wed V M4snkutd<refteh 4
ca.a seet tu n m: ass n i>:se test se >e


l positive       displacement       charging           pump       are
l positive displacement charging pump are
              * . .                                  administratively tagged         out but are available         for
:(.
:(.                                    service.
administratively tagged out but are available for service.
                                                  - The Refueling Water Storage Tank is avsilable-as a:
- The Refueling Water Storage Tank is avsilable-as a:
borated -water source with-level at- approximately 97%.
borated -water source with-level at-approximately 97%.
                                                  - All four scoumulators have been cleared and drained.
- All four scoumulators have been cleared and drained.
                                                  - Boric Acid Storage Tank 2-2 is at 80% level with a boron concentration of 22050 ppab.                   BAST 2-1 is Boric Acid Transfer pump 2-2 is available t
- Boric Acid Storage Tank 2-2 is at 80% level with a
boron concentration of 22050 ppab.
BAST 2-1 is t
empty.
empty.
for service. The 2-1 transfer pump is cleared.
Boric Acid Transfer pump 2-2 is available for service.
                                                  - Containment Fan Cooler Unita 2-1,                 2-2,   2-3 an'd 2-4 are   available     for service.       CFCU 2-5 is cleared.
The 2-1 transfer pump is cleared.
l                                                   CFCU 2-3 is in service running in slow speed.
- Containment Fan Cooler Unita 2-1, 2-2, 2-3 an'd 2-4 are available for service.
l                                                 - All     four   steam generators have         a   secondary     side water level of approximately 73% wide range with the 10% atmospheric dumps open to atmosphere.
CFCU 2-5 is cleared.
                                                  - The main and auxiliary transformer banha have been oleared and the Unit is being powered from the Startup transformer bank.               Diesel Generators       2-1, 2-2 and.1-3 are all available for servioe.                 480 volt   1
l CFCU 2-3 is in service running in slow speed.
(},                               bus 2F is cleared for outage related work.
l
                                                - All       core exit thermocouples have been               determinated
- All four steam generators have a
        ,                                            in preparation for reactor vessel head removal.
secondary side water level of approximately 73% wide range with the 10% atmospheric dumps open to atmosphere.
                                                - Post       accident monitoring panels 1 and 2 are out of service for human factors related upgrades.
- The main and auxiliary transformer banha have been oleared and the Unit is being powered from the Startup transformer bank.
                                                - Plant vent high range radiation monitor RM-29 is out of     service. All     other required process and           area
Diesel Generators 2-1, 2-2 and.1-3 are all available for servioe.
                                            ,        radiation monitors are in service.
480 volt
:                                  P r
(},
Shift       Turnover:   The previous watch had completed draining of the steam generator U-tubes per operating procedure OP A-2:II.
bus 2F is cleared for outage related work.
During the draining, it was noted that the U-tubes began to drain once vessel level as indicated on the RVLIS system reached 107'-3". It wa's reported that once the U-tubes had drained, level dropped to 106'-6" where signs of RHR pump cavitation were noted. Once level had been restored to 107'-0",                   indications of pump cavitation or vortexing stopped and level was stabilised at 107'0".               Work was ongoing to uncouple and backseat the Reactor coolant Pumps.                         Various 7-                             containment penetration leak tests were ongoing.
1
L ..
- All core exit thermocouples have been determinated in preparation for reactor vessel head removal.
2 g.d     seet E*5                           3ers ywrsn         EP:ee   486TAE90
- Post accident monitoring panels 1 and 2 are out of service for human factors related upgrades.
                                                                                            +
- Plant vent high range radiation monitor RM-29 is out of service.
All other required process and area radiation monitors are in service.
P r
Shift Turnover:
The previous watch had completed draining of the steam generator U-tubes per operating procedure OP A-2:II.
During the draining, it was noted that the U-tubes began to drain once vessel level as indicated on the RVLIS system reached 107'-3".
It wa's reported that once the U-tubes had drained, level dropped to 106'-6" where signs of RHR pump cavitation were noted.
Once level had been restored to 107'-0",
indications of pump cavitation or vortexing stopped and level was stabilised at 107'0".
Work was ongoing to uncouple and backseat the Reactor coolant Pumps.
Various 7-L..
containment penetration leak tests were ongoing.
2 g.d seet E*5 3ers ywrsn EP:ee 486TAE90
+


        . ..                                                                            2
2
(
(
TIME                               EVENT DESCRIPTION                       DATA SOURCE
TIME EVENT DESCRIPTION DATA SOURCE
                ====:============v======================================================
 
4/10/87 1700 Bra           Early in the shift, the Shift Foreman                 SFM/C0 informs the Control Operator that due to               Statements the planned work to remove the steam generator primary manways, the reactor vessel level should be maintained below approximately 107'-8". This would assure                       '
====:============v======================================================
that rater would not be allowed to spill over irto the steam generator lower head area     from   the RCS       loops.       Since indicat ions of RHR pump suotion vortexing had been stopped on the previous shift by raisint vessel level to 107'-0", the CO planned to maintain vessel level between 107'-0" to 1078-8" during the shift.
4/10/87 1700 Bra Early in the shift, the Shift Foreman SFM/C0 informs the Control Operator that due to Statements the planned work to remove the steam generator primary manways, the reactor vessel level should be maintained below approximately 107'-8".
( 1850 Hrs                 Since assuming the watch at approximately             CO Log
This would assure that rater would not be allowed to spill over irto the steam generator lower head area from the RCS loops.
              ~                     1700 hrs, the vessel water level as indicated on the RVLIS system had slowly
Since indicat ions of RHR pump suotion vortexing had been stopped on the previous shift by raisint vessel level to 107'-0",
(" .                      risen to the 1078-8".           Vessel level is C0 Statement reduced back to 107'-0" by rejecting water back to the RWST via valve 8741.
the CO planned to maintain vessel level between 107'-0" to 1078-8" during the shift.
2010 Hrs           An Engineer       enters the containment to           Engineer's begin draining containment penetration 45             Statement in preparation to perform Surveillance                 -
( 1850 Hrs Since assuming the watch at approximately CO Log
i
~
          ,                        Test Procedure V-645.         STP V-845 is     the   Security
1700
* Local Leak Rate Test (LLRT) for               that   Computer penetration. The penetration was cleared by the Operations Department on 4/9/87 to allow the leak rate test to be           completed (CR 00006713).       The penetration serves the Reactor Coolant Pump seal leakoff return line to the Volume Control Tank.
: hrs, the vessel water level as
!              2041-               The Engineer enters the regenerative heat             Engineer's exchangsr room and opens CVCS-314 as part             Statement of the : procedure to drain the penetzation prior to beginning the leak rate test.
(".
The Engineer verifies flow through the YCT on P-250 drain       valve   and then Trend Recorder exits   .the containment to log onto another SWP while the   peaetration is draining.         Since   the (s                         clearan,:e     request for the         job     was approved the       previous day,       the   Shift P
indicated on the RVLIS system had slowly C0 Statement risen to the 1078-8".
i
Vessel level is reduced back to 107'-0" by rejecting water back to the RWST via valve 8741.
,                                                            3
2010 Hrs An Engineer enters the containment to Engineer's begin draining containment penetration 45 Statement in preparation to perform Surveillance i
                            ..;      _,                          a .w.wws.o         a.   ==
Test Procedure V-645.
STP V-845 is the Security Local Leak Rate Test (LLRT) for that Computer penetration.
The penetration was cleared by the Operations Department on 4/9/87 to allow the leak rate test to be completed (CR 00006713).
The penetration serves the Reactor Coolant Pump seal leakoff return line to the Volume Control Tank.
2041-The Engineer enters the regenerative heat Engineer's exchangsr room and opens CVCS-314 as part Statement of the : procedure to drain the penetzation prior to beginning the leak rate test.
YCT on P-250 The Engineer verifies flow through the Trend Recorder drain valve and then exits
.the containment to log onto another SWP while the peaetration is draining.
Since the (s
clearan,:e request for the job was approved the previous
: day, the Shift P
i 3
a.w.wws.o a.


Foremati was unaware that the diraining of the per etration was ongoing at this time. '
==
(                                            Due   to       a       leaking           boundary . valve associrited with.the clearance,                       a drain path is created betwaan the VCT sud                                                             ~*
Foremati was unaware that the diraining of
the RCDT.     VCT level _immediately begins to decreas.e.
(
2051 Hrs                               contro3 Room operators note the downward trend                                                                                          VCT on P-250 in VCT level and increase letdown                                                     Trend Recorder from the primary system to stabilize VCT level ty further opening HCV-133. Due to the ir. crease in letdown flow, reactor vessel level begins to slowly decrease.
the per etration was ongoing at this time. '
2054 Hra                               While trying to determine the                       cause                           of       operator's the level decrease in the                         VOT, Control' Operator contacts the AO at the the      Statement Auxiliary         Building control board determine if any unusual evolutions are to      P-250 Alarm occurring.             The AO reports that the RCDT Printout level has       increased. While they are on                                                                   ,
Due to a
the phene,       the RCDT pump starts on high level.       The       C0   requests       that the                               A0 estimate the flow rate into the RCDT and
leaking boundary
. valve associrited with.the clearance, a
drain path is created betwaan the VCT sud the
~
* RCDT.
VCT level _immediately begins to decreas.e.
2051 Hrs contro3 Room operators note the downward VCT on P-250 trend in VCT level and increase letdown Trend Recorder from the primary system to stabilize VCT level ty further opening HCV-133.
Due to the ir. crease in letdown
: flow, reactor vessel level begins to slowly decrease.
2054 Hra While trying to determine the cause of operator's the level decrease in the
: VOT, the Statement Control' Operator contacts the AO at the Auxiliary Building control board to P-250 Alarm determine if any unusual evolutions are Printout occurring.
The AO reports that the RCDT level has increased.
While they are on the phene, the RCDT pump starts on high level.
The C0 requests that the A0 estimate the flow rate into the RCDT and
[c.
[c.
report bach $o the Control Room.                                                                  .
report bach $o the Control Room.
                                                                                                                                                    .v Control ; Room receives notification that SFM Log the.RCP4 have               been uncoupled             and                           are backseated.
Control ; Room receives notification that SFM Log
Due   to   the apparent loss of inventory 2124 H kgg              26s 3) fromthe                            primary                                                                      VCT on P-250 system.         Operators g ,                   j isolate                     the charging and letdown flow                                                     Trend Recorder
.v the.RCP4 have been uncoupled and are backseated.
* paths.
2124 H s 3) from Due to the apparent loss of inventory VCT on P-250 kgg 26 the primary system.
The loss of letdown flow to r,he VCT>causes VCT level to rapidly decrease.                                                       RVLIS on P-250 Level decrease in the primary system                                                           Trend Recorder stops     (107'-4").
Operators Trend Recorder
Auxiliary Building A0                     reports                                   the Control room that the estimated to                      leakage C0 statement into the RCDT is approximately 30 syn.
* g,
              ')hj' 2125 Hrs                               Operato:es notice amps on the 2-2 RER pump A /0   M,1I WY   l,y                              beginning to fluctuate. The pump is shut                                                       P-250 Alarm down a:'ter starting the 2-1                     pump. Ampe Printout also fluotuate on the 2-1 pump and it is                                                       SIM Statement secured almost immediately. Operators are dispatched
j isolate the charging and letdown flow paths.
( .,                                                                to     vent the pumps and                               seal coolers on both RHR pumps.
The loss of letdown flow to r,he RVLIS on P-250 VCT>causes VCT level to rapidly decrease.
4 90*d                         SBEC EP5                                 6 *g58 3*u*H*s (1                           Et*:80 486L'87/PO
Trend Recorder Level decrease in the primary system stops (107'-4").
Auxiliary Building A0 reports to the C0 statement Control room that the estimated leakage into the RCDT is approximately 30 syn.
')hj' 2125 Hrs Operato:es notice amps on the 2-2 RER pump P-250 Alarm
/0 I WY beginning to fluctuate.
The pump is shut Printout A M,1 l,y down a:'ter starting the 2-1 pump.
Ampe also fluotuate on the 2-1 pump and it is SIM Statement secured almost immediately. Operators are dispatched to vent the pumps and seal
(.,
coolers on both RHR pumps.
4 90*d SBEC EP5 6 *g58 3*u*H*s (1 Et*:80 486L'87/PO


                                .Due to the unexpected RHR pump cavitation
(-
* SFH Statement
.Due to the unexpected RHR pump cavitation
(-                    or   vartexinsi operatora suspect validity of the JRVLIS ' indication.-- the operator -is                                   An sent into containment to verify level indication on Tygon" Tube.
* SFH Statement or vartexinsi operatora suspect the validity of the JRVLIS ' indication.--
Outage Coordinator is requested to. verify                 SFM Statement the at-stus of the work on Steam Generator manway.s.
An operator -is sent into containment to verify level indication on Tygon" Tube.
Operators     continue work to locate the source of the leakage.                                     SFH Statement 2138 Hrs       Operators       close LCV-1120 to stop inventory loss from the VCT.                               Co Los
Outage Coordinator is requested to. verify SFM Statement the at-stus of the work on Steam Generator manway.s.
'-                              isolatos the VCT from the RCDT.
Operators continue work to locate the SFH Statement source of the leakage.
This valve The level decrease in the VCT stops.
2138 Hrs Operators close LCV-1120 to stop Co Los inventory loss from the VCT.
2147 Hrs         The Engineer performing the           leak rate           Security test     re-enters     the   containment       to         Computer continue the local leak rate test.
This valve isolatos the VCT from the RCDT.
2200 Hrs       The             valves
The level decrease in the VCT stops.
!      [7-vent penetration             associated with the being drained Engineer I                                                                  are opened.             Statement
2147 Hrs The Engineer performing the leak rate Security test re-enters the containment to Computer continue the local leak rate test.
        'l After opening the valves,         the Engineer goes to find a Decon Tech to assist with the leth rate test.
2200 Hrs The vent valves associated with the Engineer
2203 Bra       Contro3 Room is notified that the venting on the 2-1 RHR pump has been completed.                     co Los 2221' Brs       Control Room has received notification SFH that     the Tyson Tube level is between                   Statement kh ./.b;-       106'-9"     and   107'-0".     The     Control l                       Alb   Operator       throttled 'the discharge and               P-250 Alarm
[7-penetration being drained are opened.
!                      8 s/   started RER 2-1.       Pump was vented before             Printout i                             and during the re-start.           Pump amps are
Statement I
!                              awinging by about 20 amps.
'l After opening the valves, the Engineer goes to find a Decon Tech to assist with the leth rate test.
2203 Bra Contro3 Room is notified that the venting co Los on the 2-1 RHR pump has been completed.
2221 Brs Control Room has received notification SFH that the Tyson Tube level is between Statement kh./.b;-
106'-9" and 107'-0".
The Control l
Alb Operator throttled 'the discharge and P-250 Alarm 8 s/
started RER 2-1.
Pump was vented before Printout i
and during the re-start.
Pump amps are awinging by about 20 amps.
Pump is immediately shut down.
Pump is immediately shut down.
2223 Hrs       Shift     Foreman   declares   a   Significant Event.                                                     SFH Log s'
2223 Hrs Shift Foreman declares a
5 g .d   MM                           n m pj 3 a v s n   tv:N     IN "'"
Significant SFH Log Event.
__:          _=--:==n:                                         2   ::: :: ._ :, ._    . _ - - - - , _ _ , .-.
s' 5
g.d MM n m pj 3 a v s n tv:N IN "'"
=--:==n:
2


L .       2225 Hrs                         Operaters re-cpen LCV-112C in an attempt                   t     VCT on P-250 to localise the source of the leakage.
L
  ~(.                                      VCT     level again begins. to decrease.
~(.
Trend Recorder I                                           Operatcra close LCV-112C and VCT level                           CO Statemen\Y stabilises.
2225 Hrs Operaters re-cpen LCV-112C in an attempt t VCT on P-250 to localise the source of the leakage.
2226 Hrs                         The Engineer performing the leak rate                             Engineer test finds a large amount of water on the                         Statement 91' elevation of the containment and believes that the water is associated with his draining of the penetration. He notifies Rad Protection personnel of the spill and isolates the vent valves from the penetration.
Trend Recorder VCT level again begins. to decrease.
2230 Hrs                         HP     Tech       on the 140' elovation                 of       HP Tech containnent notices airborno                   activity         Statement levels increasing and begins taking air samples       to locate the source,                   Rad Protection personnel begin evacuation                   of workers       off of the 115' eleva. tion due to elevated airborne readings.
I Operatcra close LCV-112C and VCT level CO Statemen\\Y stabilises.
(; 2233 3rs                             HP     Tech       on     115'     elevation notes               HP Tech
2226 Hrs The Engineer performing the leak rate Engineer test finds a large amount of water on the Statement 91' elevation of the containment and believes that the water is associated with his draining of the penetration.
      .,,                                  background on friskers exceeding.the X10                         Statement soale.       Continuous Air Monitors on the 140' elsvation are alarming.
He notifies Rad Protection personnel of the spill and isolates the vent valves from the penetration.
2238 Hrs                         Operations       personnel       believe     steam     is       CO Log being generated in the head as indicated by     a slow       trend     up   on     the       RVLIS       SFM Statement
2230 Hrs HP Tech on the 140' elovation of HP Tech containnent notices airborno activity Statement levels increasing and begins taking air samples to locate the
* indication.             The Control     Operator is notifieil that th; Steam Generator primary manways have not been             removed.       Valves 8805 A and B are opened to                   establish makeup ,o the remotor vessel.
: source, Rad Protection personnel begin evacuation of workers off of the 115' eleva. tion due to elevated airborne readings.
2243 !!ra                         HP Foroman is notified by the Control EP Tech Room of a possible containment evacuation                         Statement due to the problems with the IUDL system.
(; 2233 3rs HP Tech on 115' elevation notes HP Tech background on friskers exceeding.the X10 Statement soale.
HP Forenan then enters the contaisment to begin         evacuation         of     unnecessary personnol.
Continuous Air Monitors on the 140' elsvation are alarming.
(. _
2238 Hrs Operations personnel believe steam is CO Log being generated in the head as indicated by a
6 gg d   Seeg Ep5                           6 *D3ti 0*ti'N'S*P   FP:80 486DB2/PO
slow trend up on the RVLIS SFM Statement
* indication.
The Control Operator is notifieil that th; Steam Generator primary manways have not been removed.
Valves 8805 A and B are opened to establish makeup
,o the remotor vessel.
2243 !!ra HP Foroman is notified by the Control EP Tech Room of a possible containment evacuation Statement due to the problems with the IUDL system.
HP Forenan then enters the contaisment to begin evacuation of unnecessary personnol.
(.
6 gg d Seeg Ep5 6 *D3ti 0*ti'N'S*P FP:80 486DB2/PO


                    . / .*       ..
. /.*
            ' - 2250 Hrs                     The Cet Trol Room is notified by personnel                                               #
' - 2250 Hrs
(                              inside                                                                                         Engineer was'                  of containment that the leak path                                       -Statement the it.ontified as being associated with
(
                                .                    Inah rate test and that the- leakage gU                  was ist. lated (valve CVCS-314).
The Cet Trol Room is notified by personnel Engineer inside of containment that the leak path
i 2251 Bra               Reactor                             vessel level is             indicating 4,IJ, & h,lN. 3 ft 0D               1 approximately 1108                               Operators start RHR                       RVLIS on P-250
-Statement it.ontified as being associated was' with the Inah rate test and that the-leakage was ist. lated (valve CVCS-314).
                                      '/ pump         i:-2. Pump amps                                                                     Trend Recorder v'             immedia,tely after the . pump                           fluotuate slightly stabilise.                                                              start,     but         P-250 Alarm Printer Short1r following the pump start, RHR         RHR Discharge pump     discharge board recorder rises to                    temperature               on the   control         Temp Recorder 220 F.                             Within 6 minutes,                 approximately the pump discharge temperature has dropped to less than 2C 0 F.
gU i
2253 Bra               Operatcra                               note     minor cavitation                               on indication of the running RHR pump.                             BFH Log i
2251 Bra Reactor vessel level is indicating RVLIS on P-250 4,IJ, & h,lN. 3 ft 0D 1 approximately 1108 Operators start RHR Trend Recorder
Valve           8980                     (RWST to RER
/' pump i:-2.
!                                        partially                                                                auction) is             CO Log opened to increase makeup to the reactor vessel. Pump amps stabilise.
Pump amps fluotuate slightly v'
0-)                                                                                                           .
immedia,tely after the. pump
2258 Hrs                 Control                 room receives notification of Q,g steam venting from a ruptured on the                                                                     tygon tube            SFM Log reactor head vent.
: start, but P-250 Alarm stabilise.
i                                        Containment Evacuation alarm initiated at                                                         SFM Log the direction of the Shift Foreman.
Printer Short1r following the pump
f                                                                                   .                                                                    .
: start, RHR pump discharge temperature on the control RHR Discharge Temp Recorder board recorder rises to approximately 220 F.
2310 3rs                 Shift         Foreman requests that the operator HP Tech /CO insidevant head       of conatinment      which is supplying     isolate the       thereactor            Statements leak i.n the tygon hose.                                                           steam HP Tech and operator the le.sk.            descend                   to   head area           and isolate No visible condensation or water i.: noted in the area.
Within 6
!              2313 Hra
: minutes, the pump discharge temperature has dropped to less than 2C 0 F.
'                                      Control room notified that the reactor         CO Log vessel head vent has been isolated.
2253 Bra Operatcra note minor indication of BFH Log cavitation on the running RHR pump.
7 g .d       mBE'Et3                                                 n 'U3H 3*W N'S*P             SP:00     486t/8E/PO .
i Valve 8980 (RWST to RER auction) is CO Log partially opened to increase makeup to the reactor vessel.
  - - ::n             - _ -                      - _..- -- -.-__-,__- - - -___-.
0-)
Pump amps stabilise.
2258 Hrs Control room receives notification of SFM Log Q
steam venting from a ruptured tygon tube
,g on the reactor head vent.
Containment Evacuation alarm initiated at the direction of the Shift Foreman.
i SFM Log f
2310 3rs Shift Foreman requests that the operator inside of conatinment isolate the reactor HP Tech /CO head Statements vant which is supplying the steam leak i.n the tygon hose.
HP Tech and operator descend to head area and isolate the le.sk.
No visible condensation or water i.: noted in the area.
2313 Hra Control room notified that the reactor CO Log vessel head vent has been isolated.
7 g.d mBE'Et3 n 'U3H 3*W N'S*P SP:00 486t/8E/PO
- - ::n


232n Hrs   Control Room is notified by HP Fersonnel                 SFM Statement
232n Hrs Control Room is notified by HP Fersonnel SFM Statement
            'r                               that     the containment airborne is greater'             "
'r that the containment airborne is greater' than 1
('                              than     1     MPC and is high in             Iodine. C0 Log Operat ors place the containment Iodine Remova.1 fans into service to attempt t'o reduc < airborne activity.
MPC and is high in Iodine.
232! Hrs   Shift     Foreman goes to       the containment         Security persor nel       hatch to verify the status of           Computer the ocntainment evacuation. While there, he in informed by the RP Foreman of the                   SFH/RP Foreman water leakage from the steam generator                   Statements manway s.
C0 Log
2342 Hrs   Level in the           pressurizer has       reached     CO Los approximately         40%. Operators       begin divert ing letdown flow to the LHUT to reduce level and minimize the leakage from the steam generator manways.
('
0044 Hrs     Operators         open   valve   8741   to     begin     CO Log pumping primary system water back to the RWST to         further   reduce   level   in the primary       system. Letdown divert to the
Operat ors place the containment Iodine Remova.1 fans into service to attempt t'o reduc < airborne activity.
(,.                             LHUT is secured at this time.
232! Hrs Shift Foreman goes to the containment Security persor nel hatch to verify the status of Computer the ocntainment evacuation.
0102 Bra     Operators       stop rejecting water back to             CO Log /
While there, he in informed by the RP Foreman of the SFH/RP Foreman water leakage from the steam generator Statements manway s.
the     RWST.     Valve 8741 closed.           RVLIS     RVLIS on P-250 indicating approximately 114'-0".                         Trend Recorder 0320 Hrs     Reactor vessel level is reduced to             half-     CO Log loop asd leakage from the steam generator                               '
2342 Hrs Level in the pressurizer has reached CO Los approximately 40%.
manways is stopped.
Operators begin divert ing letdown flow to the LHUT to reduce level and minimize the leakage from the steam generator manways.
approximately 108'-4".
0044 Hrs Operators open valve 8741 to begin CO Log pumping primary system water back to the RWST to further reduce level in the primary system.
RVLIS indication at V
Letdown divert to the
8 pg.a w. w,                           n pi+i a WN*M*ll   W 3NH /A LN'W
(,.
LHUT is secured at this time.
0102 Bra Operators stop rejecting water back to CO Log /
the RWST.
Valve 8741 closed.
RVLIS RVLIS on P-250 indicating approximately 114'-0".
Trend Recorder 0320 Hrs Reactor vessel level is reduced to half-CO Log loop asd leakage from the steam generator manways is stopped.
RVLIS indication at approximately 108'-4".
V 8
pg.a
: w. w, n pi+i a WN*M*ll W 3NH
/A LN'W


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4/21/87' OCONEE 1, 2, AND 3 - FOULING OF LOW PRESSURE SERVICE WATER, 1.0W PRESSl!PE INJECTION AND REACTOP PUILDING COOLING UNITS llPDATE PROBLEM:
4/21/87' OCONEE 1, 2, AND 3 - FOULING OF LOW PRESSURE SERVICE WATER, 1.0W PRESSl!PE INJECTION AND REACTOP PUILDING COOLING UNITS llPDATE PROBLEM:
REDUCED HEAT TRANSFER CAPABILITY OF THE LOW PRESSURE INJECTION (LPI) AND REACTOR BUILDING COOLING UNIT 1RBCU) HEAT EXCHANGERS LIMITS REACTOR OPERATING POWEP CAUSE:       LAKE SEDIMENT DEPOSITED IN HEAT EXCHANGERS SIGNIFICAPCE:
REDUCED HEAT TRANSFER CAPABILITY OF THE LOW PRESSURE INJECTION (LPI) AND REACTOR BUILDING COOLING UNIT 1RBCU) HEAT EXCHANGERS LIMITS REACTOR OPERATING POWEP CAUSE:
LAKE SEDIMENT DEPOSITED IN HEAT EXCHANGERS SIGNIFICAPCE:
SAFETY EQUIPMENT INCAPABLE OF PERFORMING THE DESIGN HEAT REJECTION SAFETY FUNCTION DISCUSSION:
SAFETY EQUIPMENT INCAPABLE OF PERFORMING THE DESIGN HEAT REJECTION SAFETY FUNCTION DISCUSSION:
THE LOW PRESSURE SERVICE WATER SYSTEM TAKES RAW LAKE WATER TO C00L THE LPI AND RBCU HEAT EXCHANGERS LICENSEE ANALYZED THE TEST DATA AND CORRELATED IT TO EMERGENCY CONDITIONS THE-ANALYSIS SHOWED THAT UNDER LOCA CONDITIONS, THE PEAT EXCHANGERS WOULD NOT PERF0PM AT DESIGN RATING J
THE LOW PRESSURE SERVICE WATER SYSTEM TAKES RAW LAKE WATER TO C00L THE LPI AND RBCU HEAT EXCHANGERS LICENSEE ANALYZED THE TEST DATA AND CORRELATED IT TO EMERGENCY CONDITIONS THE-ANALYSIS SHOWED THAT UNDER LOCA CONDITIONS, THE PEAT EXCHANGERS WOULD NOT PERF0PM AT DESIGN RATING J
Line 410: Line 585:
ON APRIL 10, 1987, NRR ISSUED A CONFIRMATORY ORDER WHICH REQUIRED THAT THE HEAT EXCHANGERS BE CLEANED AND TESTED REACTOR OPERATION AT LOWER POWER LEVELS WITHIN THE HEAT TRANSFER CAPABILITY OF THE HEAT EXCHANGERS THE REACTOR HIGH FLUX TRIP SETPOINTS TO BE REDUCED CONTACT:
ON APRIL 10, 1987, NRR ISSUED A CONFIRMATORY ORDER WHICH REQUIRED THAT THE HEAT EXCHANGERS BE CLEANED AND TESTED REACTOR OPERATION AT LOWER POWER LEVELS WITHIN THE HEAT TRANSFER CAPABILITY OF THE HEAT EXCHANGERS THE REACTOR HIGH FLUX TRIP SETPOINTS TO BE REDUCED CONTACT:
H. PASTIS, NRR
H. PASTIS, NRR
                                                                                                                  - -_ _ _ j
- -_ _ _ j


4/21/87 OCONEE 3   VALVES TO HIGH PRESSURE INJECTTON PUMPS ISOLATED
4/21/87 OCONEE 3 VALVES TO HIGH PRESSURE INJECTTON PUMPS ISOLATED
        -PROBLEM:
-PROBLEM:
BOTH MOTOR OPERATED SUCTION VALVES FROM THE B0 RATED WATER STORAGE TANK TO THE HIGH. PRESSURE INJECTION PUMPS WERE IN THEIR NORMAL Cl.0 SED POSITION BUT THE MOTOR SUPPLY BREAKERS WERE OPEN.
BOTH MOTOR OPERATED SUCTION VALVES FROM THE B0 RATED WATER STORAGE TANK TO THE HIGH. PRESSURE INJECTION PUMPS WERE IN THEIR NORMAL Cl.0 SED POSITION BUT THE MOTOR SUPPLY BREAKERS WERE OPEN.
CAUSE:   NUMEROUS PERSONNEL ERRORS SIGNIFICANCE HIGH PRESSURE INJECTION SYSTEM COULD NOT HAVE RESPONDED TO AN ENGINEERED SAFEGUARDS SIGNAL DISCUSSION:
CAUSE:
NUMEROUS PERSONNEL ERRORS SIGNIFICANCE HIGH PRESSURE INJECTION SYSTEM COULD NOT HAVE RESPONDED TO AN ENGINEERED SAFEGUARDS SIGNAL DISCUSSION:
OCONEE UNIT 3 WAS HEATING UP WHEN VALVES VERE DISCOVERED INOPERABLE FOR TWENTY HOURS SITl'ATION CORRECTED IMMEDI ATELY UPON IDENTIFICATION FOLLOWUP:
OCONEE UNIT 3 WAS HEATING UP WHEN VALVES VERE DISCOVERED INOPERABLE FOR TWENTY HOURS SITl'ATION CORRECTED IMMEDI ATELY UPON IDENTIFICATION FOLLOWUP:
ENFORCEMENT CONFERENCE HAS BEEN SCHEDULED l
ENFORCEMENT CONFERENCE HAS BEEN SCHEDULED l
Line 422: Line 598:


4/21/87-OTHER EVENT OF' INTEREST.
4/21/87-OTHER EVENT OF' INTEREST.
RIVER BEND - QA/0C PROBLEM FOR PROCESS COMPUTER SOFTWARE PROBLEM:       RIVER BEND STATION EXCEEDED LICENSED THEPMAL LIMIT CAllSE:     INADEQUATE QA/0C BY VENDOR ON SOFTWAPE'FOR-PROCESS. CONTROL COMPUTER SIGNIFICANCE:
RIVER BEND - QA/0C PROBLEM FOR PROCESS COMPUTER SOFTWARE PROBLEM:
RIVER BEND STATION EXCEEDED LICENSED THEPMAL LIMIT CAllSE:
INADEQUATE QA/0C BY VENDOR ON SOFTWAPE'FOR-PROCESS. CONTROL COMPUTER SIGNIFICANCE:
QA/QC 0N SOFTWARE FOR PLANT COMPUTER ERROR IN SOFTWARE OF A NON-SAFETY PELATED COMPUTER IMPACTS POWER LEVEL DISCUSSION:-
QA/QC 0N SOFTWARE FOR PLANT COMPUTER ERROR IN SOFTWARE OF A NON-SAFETY PELATED COMPUTER IMPACTS POWER LEVEL DISCUSSION:-
ON.MAY 13, 1987, LICENSEE INSTALLED VENDOR SUPPLIED SOFTWARE 0N PLANT COMPUTER
ON.MAY 13, 1987, LICENSEE INSTALLED VENDOR SUPPLIED SOFTWARE 0N PLANT COMPUTER VEND 0F, GE, STATED SOFTWARE ONLY' IMPACTS B0P PARAMETERS LICENSEE HAD BENCH CHECKED SOFTWARE AGAINST VEND 0P SPECIFICATIONS ALERT OPERATOR NOTICED COMPUTER' THERMAL POWER READ 0VTS NOT CCRRECTLY RESPONDING TO CHANGES IN RECIRCULATION FLOW LICENSEE REDUCED POWER, SilBSTITUTED OLD SOFTWARE - PP0BLEM RESOLVED.
                      -      VEND 0F, GE, STATED SOFTWARE ONLY' IMPACTS B0P PARAMETERS LICENSEE HAD BENCH CHECKED SOFTWARE AGAINST VEND 0P SPECIFICATIONS ALERT OPERATOR NOTICED COMPUTER' THERMAL POWER READ 0VTS NOT CCRRECTLY RESPONDING TO CHANGES IN RECIRCULATION FLOW LICENSEE REDUCED POWER, SilBSTITUTED OLD SOFTWARE - PP0BLEM RESOLVED.
' THERMAL LIMIT EXCEEDED FOR MAXIMUM 0F FOUR HOURS PEAK THERMAL POWER 101,15 LICENSE LIMIT FOLLOWUP:
                        ' THERMAL LIMIT EXCEEDED FOR MAXIMUM 0F FOUR HOURS
                      -      PEAK THERMAL POWER 101,15 LICENSE LIMIT FOLLOWUP:
LICENSEE /GE PERFORMING IN DEPTH ROOT CAUSE ANALYSIS REGION IV FOLLOWING UP WITH LICENSEE, WILL ISSUE INSPECTION REPORT VENDOR INSPECTIONS FOLLOWING UP WITH GE INFORMATION NOTICE ON MAXIMUM LICENSED POWER LEVEL UNDER REVIEW BY NRR CONTACT:
LICENSEE /GE PERFORMING IN DEPTH ROOT CAUSE ANALYSIS REGION IV FOLLOWING UP WITH LICENSEE, WILL ISSUE INSPECTION REPORT VENDOR INSPECTIONS FOLLOWING UP WITH GE INFORMATION NOTICE ON MAXIMUM LICENSED POWER LEVEL UNDER REVIEW BY NRR CONTACT:
S. STERN, NRR
S. STERN, NRR
Line 436: Line 612:
INADVERTENT SAFETY SYSTEM ACTUATION RESULTING FROM GPEPATOR ACTIONS ON WRONG UNIT POTENTIAL FOR ELECTRICAL EQUIPMENT DEGRADATION DUE TO WETTING BY BORATED WATER (BORIC ACID INTRUSION)
INADVERTENT SAFETY SYSTEM ACTUATION RESULTING FROM GPEPATOR ACTIONS ON WRONG UNIT POTENTIAL FOR ELECTRICAL EQUIPMENT DEGRADATION DUE TO WETTING BY BORATED WATER (BORIC ACID INTRUSION)
PERSONNEL CONTAMINATION
PERSONNEL CONTAMINATION
          - DISCllSSION:
- DISCllSSION:
UNIT 1 IN MODE 5, ELECTRICAL TERMINAL B0XES OPENED FOR EQ MAINTENANCE, AND CONTAINMENT SPRAY CONTAINMENT ISOLATION (CS/CI)
UNIT 1 IN MODE 5, ELECTRICAL TERMINAL B0XES OPENED FOR EQ MAINTENANCE, AND CONTAINMENT SPRAY CONTAINMENT ISOLATION (CS/CI)
BLOCK VALVE DE-ENERGIZED (FAIL OPEN) FOR EQ MAINTENANCE OPERATOR ON 12-HOUR SHIFT; UNIT 2 (4:00-8:00 A.M.), UNIT 1 (8:00 A.M.-4:00 P.M.)
BLOCK VALVE DE-ENERGIZED (FAIL OPEN) FOR EQ MAINTENANCE OPERATOR ON 12-HOUR SHIFT; UNIT 2 (4:00-8:00 A.M.), UNIT 1 (8:00 A.M.-4:00 P.M.)
OPERATOR ERRCNE00 SLY WENT TO UNIT 2 PENETRATION ROOM INSTEAD OF UNIT 1 PENETRATION ROOM FOR CLOSURE OF CS/CI VALVE FOLLOW-UP:
OPERATOR ERRCNE00 SLY WENT TO UNIT 2 PENETRATION ROOM INSTEAD OF UNIT 1 PENETRATION ROOM FOR CLOSURE OF CS/CI VALVE FOLLOW-UP:
LICENSEE WILL:                   ANALYZE POTENTIAL SAFETY IMPLICATION OF OPENED TERMINAL B0XES TO BORIC ACID DEGRADATION INVESTIGATE THE HUMAN ERROR AND CONTRIBUTING FACTORS INVOLVED FOR THE WRONG UNIT EVENT INVESTIGATE POSSIBLE UNIT 1/ UNIT 2 LABELING INADE0tlACIES FOR EQUIPMENT REGION I TO FOLLOW UP ON CORRECTIVE ACTION MEASURES TAKEN BY LICENSEE, INCLUDING LATE NOTIFICATION OF 50,72 CODE SECTION ON REPORTABLE EVENTS FOR OPERATION OF ESF SYSTEMS CONTACT:
LICENSEE WILL:
ANALYZE POTENTIAL SAFETY IMPLICATION OF OPENED TERMINAL B0XES TO BORIC ACID DEGRADATION INVESTIGATE THE HUMAN ERROR AND CONTRIBUTING FACTORS INVOLVED FOR THE WRONG UNIT EVENT INVESTIGATE POSSIBLE UNIT 1/ UNIT 2 LABELING INADE0tlACIES FOR EQUIPMENT REGION I TO FOLLOW UP ON CORRECTIVE ACTION MEASURES TAKEN BY LICENSEE, INCLUDING LATE NOTIFICATION OF 50,72 CODE SECTION ON REPORTABLE EVENTS FOR OPERATION OF ESF SYSTEMS CONTACT:
J. THOMPSON, NRR
J. THOMPSON, NRR


  ;i; .;
;i; REA:iDR SCRAM SUVARY WEEK ENDINS 04/12/87
REA:iDR SCRAM SUVARY WEEK ENDINS 04/12/87
!.-PLANT SPECIFIC DATA IATE SITE LNIT F0sER E 3 CcUEE COMPLI-VT3 YT3 Yi; CAI D i 43IiE EELCd 70TAL 151 !!!
                                                                !.-PLANT SPECIFIC DATA IATE     SITE             LNIT F0sER E 3 CcUEE                       COMPLI-   VT3 YT3     Yi; CAI D i 43IiE EELCd 70TAL 151 !!!
04/06/97 FARLEY OA EQUIFMENT/SRM N0 3
04/06/97 FARLEY               !      OA EQUIFMENT/SRM N0                         3   1     4 04/06/37 FERN!               2     31 A FER3CNhEL                   NO         '3   0     -3 04/07/S7 EALEM               2     90 A -UNrNCWN                   NO           2   1     3 04/09/37 CATAWiA               1   100 A E901FMENT/ VALVE YES                     3   0-     3 04/09/87 CATAWBA             '1       0M EGUIPMENT/RPI NO ~                       3   1     4 04/09/87 SAINTLUCIE           2 100 A PERSCMMEL                       NO           3   0'     3 04/10/B7DREitEN               3 100 A EQUIPMENT / PIPE NO                         2   0     2 04/10/97VOSTLE                 1     30 A EQUIFMENT/VALVENO                       2   6     8 04/11/97V05TLE                 1     21 A EQUIFMENT/ VAL'lE NC                     3   6     9 04/12/67 PALISA:ES             1     75 M EQUIPMENT / PIPE NO-                     1   0     1 04/12/97 MILLSTONE           I     66 A EGUIFMENT/ PUMP NO                     ~3   1     4 02/12/37 PARRIS               1     65 M FI'!:NNEL                   NO           7   2     9-04/!2!37 MILLSTChE             !    10 A PERICUEL                   NO           3   2     i
1 4
04/06/37 FERN!
2 31 A FER3CNhEL NO
'3 0
-3 04/07/S7 EALEM 2
90 A -UNrNCWN NO 2
1 3
04/09/37 CATAWiA 1
100 A E901FMENT/ VALVE YES 3
0-3 04/09/87 CATAWBA
'1 0M EGUIPMENT/RPI NO ~
3 1
4 04/09/87 SAINTLUCIE 2 100 A PERSCMMEL NO 3
0' 3
04/10/B7DREitEN 3 100 A EQUIPMENT / PIPE NO 2
0 2
04/10/97VOSTLE 1
30 A EQUIFMENT/VALVENO 2
6 8
04/11/97V05TLE 1
21 A EQUIFMENT/ VAL'lE NC 3
6 9
04/12/67 PALISA:ES 1
75 M EQUIPMENT / PIPE NO-1 0
1 04/12/97 MILLSTONE I
66 A EGUIFMENT/ PUMP NO
~3 1
4 02/12/37 PARRIS 1
65 M FI'!:NNEL NO 7
2 9-04/!2!37 MILLSTChE 10 A PERICUEL NO 3
2 i


==SUMMARY==
==SUMMARY==
OF COMPLICATIONS SITE             liNIT           COMPLICATIONS CATAWBA             1 BORCN DILUTICN MITISATION SYSTEM INITIATED ESF AFTER SCRAM
OF COMPLICATIONS SITE liNIT COMPLICATIONS CATAWBA 1 BORCN DILUTICN MITISATION SYSTEM INITIATED ESF AFTER SCRAM
__ _        _      _        ._                  ~ _ _ . . . - , . . . . .
~ _ _... -,.....


y II. COMPARISON OF WEEKLY ETATISTICS-WITH INDUSTRY AVERAGES SCRAMS FOR WEEK ENDING 04/12/87 ECRf41 CAUSE         POWER     NUMBER         -1997         1986   1985 CF       WEEELY       WIEKLY WEEKLY SCRAM 3(5)     AVERAGE AVERAGE AVERAGE YTD     (3)(4) (8) (9)
y II. COMPARISON OF WEEKLY ETATISTICS-WITH INDUSTRY AVERAGES SCRAMS FOR WEEK ENDING 04/12/87 ECRf41 CAUSE POWER NUMBER
                        ** FOWER 15%
-1997 1986 1985 CF WEEELY WIEKLY WEEKLY SCRAM 3(5)
EOUIP. RELATED       >15%             6           3.9         4.3     5.4 PERS. RELATED(6) >15%                 3             1.7       1.8     2.0
AVERAGE AVERAGE AVERAGE YTD (3)(4)
                        -OTHER(7)               >15%             1           1.0         0.4   0.6
(8) (9)
                        ** Subtotal **
** FOWER 15%
10           6.5         6.5     8.0 t* POWER <15%
EOUIP. RELATED
EQUIP. RELATED       <15%             2           'i . 2       1.4     1.3 PERS. RELATED       <15%             1           1.O         O.8     O.9 OTHER                 <15%             0           O.4         O.2   0.I tk Gubtotal i4 3           2 . 6 .'   2.4     2.1
>15%
  ,                    4t1 fatal 414
6 3.9 4.3 5.4 PERS. RELATED(6) >15%
* 13           9 .' 1     9.9   10.4 MANUAL VS AUTO SCRAMS TYPE                     i    NUMBER           1987         1986   1985 OF       WEEKLY       WEEKLY NEEKLY SCRAMS       AVEPAGE AVERAGE AVERAGE YTD MANUAL SCRAMS                         3           1.5         1.O     1.O AUTOMATIC SCRAMS                     10           7.5         7.9   9.4
3 1.7 1.8 2.0
-OTHER(7)
>15%
1 1.0 0.4 0.6
** Subtotal **
10 6.5 6.5 8.0 t*
POWER <15%
EQUIP. RELATED
<15%
2
'i. 2 1.4 1.3 PERS. RELATED
<15%
1 1.O O.8 O.9 OTHER
<15%
0 O.4 O.2 0.I tk Gubtotal i4 3
2. 6.'
2.4 2.1 4t1 fatal 414 13 9.' 1 9.9 10.4 MANUAL VS AUTO SCRAMS TYPE NUMBER 1987 1986 1985 i
OF WEEKLY WEEKLY NEEKLY SCRAMS AVEPAGE AVERAGE AVERAGE YTD MANUAL SCRAMS 3
1.5 1.O 1.O AUTOMATIC SCRAMS 10 7.5 7.9 9.4


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[ WEEKENDING 04/19/67
                              ,                                                                                            !. PLANT SPECIFIC DATA i
!. PLANT SPECIFIC DATA i
id                                                   iO CATE.                 $1TE . d       ti!T,?0'4ER RFS CAUSE
id iO CATE.
                                                                                                                                                  -C3.9.!-     YT3 . YTD' : fTD
$1TE. d ti!T,?0'4ER RFS CAUSE
                                                    ,                                          ./                                                   CATIONS ??!'iE iELOW -TCTAL g i-                                                                                           151 15%
-C3.9.!-
W                       .                .
YT3. YTD' : fTD
3;
./
                #                                              '04/13/97 WATERFORD.                 '3 .100 A EQUIPMENT /CEAC NO                               .3     01
CATIONS ??!'iE iELOW -TCTAL g i-151 15%
          ..      ;                                              .04/13/97 PERRY                     !        10 M ' E2VIFMENT/ FIFE NO                         1-   2       3
W
              $                                                ~04/14/97 SA!MT LUCIE                 1         0A FERSONNEL -                   ' NO .         0     2-     2
'04/13/97 WATERFORD.
            '*              e                                  - 04/14/97 HMRIS -                   !        87 M . FERSONNEL                   . N3           3     2     -10 04/15/97 WATERFORD               3 - 50 A PEFSONNEL~                             NO-       /4       0       4
'3.100 A EQUIPMENT /CEAC NO
: e.                         '.            04/15/97 MC6UIRE                  1 ' 100 A UNtNCH                                NO          2    0      2 W.                   M'                                 " 04/16/87 HALDAM NECK                       l'!;'100 A UNKNGWN                             NO           1   .O.     1 3
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~04/14/97 SA!MT LUCIE 1
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    .,    -g
- g II. COMPARISON OF WEEKLY STATISTICS WITH INDUSTRY AVERAGES SCRAMS FOR WEEK ENDING s
* II. COMPARISON OF WEEKLY STATISTICS WITH INDUSTRY AVERAGES SCRAMS FOR WEEK ENDING                     s 04/19/87~
04/19/87~
SCRAM CAUSE     POWER         NUME.ER         1987     19S6     1925
SCRAM CAUSE POWER NUME.ER 1987 19S6 1925 OF WEEf:LY WEEi'LY WFI; _Y ECRAME (3 )
* OF       WEEf:LY WEEi'LY WFI; _Y ECRAME (3 )     AVERAGE AVERAGE A'.'ERAGE YTD   (3) (4) (S)(9)
AVERAGE AVERAGE A'.'ERAGE YTD (3) (4)
              ** POWER >157.
(S)(9)
EQUIP. RELATED   > 15 *'.             3         3.7       4.0     5.4 FERS. RELATED(6) >15%                   2         1.7       1.2     2.0 OTHER(7)         >15%                 6         1.3       0.4     0.6
** POWER >157.
              ** Subtotal **                                                                 '
EQUIP. RELATED
11         6.7       6.5     8.0 t* POWER <15%
> 15 *'.
EQUIP. RELATED   <15%                 1         1.2       1.4     1.3 PERS. RELATED     <15%                 1         1. 0     0.8     0.9 OTHER             '15%                 o         O.4       0.2     O.2 kt Subtet=1 tv 2         2.S       2. 4     Z.'
3 3.7 4.0 5.4 FERS. RELATED(6) >15%
444 Total 161 13         9.3       8.9   10.4 MANUAL VS AUTO SCRAMS TYPE                             NUMBER         1987     1986     1985 OF       WEEV.LY WEEKLY   WEEKLY ECRAMS       AVERAGE AVERAGE A'/ERAGE YTD MANUAL SCRAMS                           2         1.5       1.0     1.0 AUTOMATIC SCRAMS                     11         7.8       7.9     9.4
2 1.7 1.2 2.0 OTHER(7)
[. . . . .    . . . .      _
>15%
6 1.3 0.4 0.6
** Subtotal **
11 6.7 6.5 8.0 t* POWER <15%
EQUIP. RELATED
<15%
1 1.2 1.4 1.3 PERS. RELATED
<15%
1
: 1. 0 0.8 0.9 OTHER
'15%
o O.4 0.2 O.2 kt Subtet=1 tv 2
2.S
: 2. 4 Z.'
444 Total 161 13 9.3 8.9 10.4 MANUAL VS AUTO SCRAMS TYPE NUMBER 1987 1986 1985 OF WEEV.LY WEEKLY WEEKLY ECRAMS AVERAGE AVERAGE A'/ERAGE YTD MANUAL SCRAMS 2
1.5 1.0 1.0 AUTOMATIC SCRAMS 11 7.8 7.9 9.4
[.
s
s


    ,        3 NOTES
3 NOTES 1.
: 1. PLANT SPECIFIC DATA PASED ON INITIAL REVIEW OF 50.72 REFORTS FOR THE WEEK OF INTEREST. PERIOD IS MIDNIGHT Sl!NDAY TPROUGH MIDNIGHT SUNDAY SCRANS ARE DEFINED AS REACTOR PROTECTIVE ACTUATIONS WHICH RESULT IN ROD MOTION, AND EXCLUDE PLANNED TESTS OR SCRAMS AS PART OF PLANNED SHUTDOWN IN' ACCORDANCE WITH A PLANT PROCEDURE.
PLANT SPECIFIC DATA PASED ON INITIAL REVIEW OF 50.72 REFORTS FOR THE WEEK OF INTEREST. PERIOD IS MIDNIGHT Sl!NDAY TPROUGH MIDNIGHT SUNDAY SCRANS ARE DEFINED AS REACTOR PROTECTIVE ACTUATIONS WHICH RESULT IN ROD MOTION, AND EXCLUDE PLANNED TESTS OR SCRAMS AS PART OF PLANNED SHUTDOWN IN' ACCORDANCE WITH A PLANT PROCEDURE.
: 2. RECOVERY COMPLICATED BY EQUIPMENT FAILURES OR PERSONNEL ERRORS UNRELATED TO CAUSE OF SCRAM.
2.
: 3. 1986 INFORMATION DERIVED FROM ORAS STUDY OF UNPLANNED REACTOR TRIPS IN 1986. WEEKLY DATA DETERMINED BY TAKING TOTAL TRIPS IN A GIVEN CATEGORY AND DIVIDING BY 52 WEEKS / YEAR.
RECOVERY COMPLICATED BY EQUIPMENT FAILURES OR PERSONNEL ERRORS UNRELATED TO CAUSE OF SCRAM.
A. IN 1986, THERE WERE AN ESTIMATED TOTAL OF 461 AUTOMATIC AND MANUAL UNPLANNED REACTOR TRIPS AT 104 REACTORS (HOLDING OPERATING LICEN$ES). THIS YIELDS AN AVERAGE RATE OF 4.4 TRIPS PER REACTOR PER YEAR AND AN AVERAGE RATE OF 8.8 TRIPS PER WEEK FOR ALL REACTORS.
3.
: 5. BASED ON 107 REACTORS HOLDING AN OPERATING LICENSE.
1986 INFORMATION DERIVED FROM ORAS STUDY OF UNPLANNED REACTOR TRIPS IN 1986. WEEKLY DATA DETERMINED BY TAKING TOTAL TRIPS IN A GIVEN CATEGORY AND DIVIDING BY 52 WEEKS / YEAR.
: 6. PERSONNEL RELATED PROBLEMS INCLUDE HUMAN ERROR, PROCEDURAL DEFICIENCIES, AND MANUAL STEAM GENERATOR LEVEL CONTROL PROBLEMS.
A.
IN 1986, THERE WERE AN ESTIMATED TOTAL OF 461 AUTOMATIC AND MANUAL UNPLANNED REACTOR TRIPS AT 104 REACTORS (HOLDING OPERATING LICEN$ES). THIS YIELDS AN AVERAGE RATE OF 4.4 TRIPS PER REACTOR PER YEAR AND AN AVERAGE RATE OF 8.8 TRIPS PER WEEK FOR ALL REACTORS.
5.
BASED ON 107 REACTORS HOLDING AN OPERATING LICENSE.
6.
PERSONNEL RELATED PROBLEMS INCLUDE HUMAN ERROR, PROCEDURAL DEFICIENCIES, AND MANUAL STEAM GENERATOR LEVEL CONTROL PROBLEMS.
1 I
1 I
i                       7.   "0THER" INCLUDES AUTOMATIC SCRAMS ATTRIBUTED TO ENVIRONMENTAL j                             CAUSES (LIGHTNING), SYSTEM DESIGN, OR UNKNOWN CAUSE.
i 7.
l
"0THER" INCLUDES AUTOMATIC SCRAMS ATTRIBUTED TO ENVIRONMENTAL j
: 8. 1985 INFORMATION DERIVED FROM AN ORAS STUDY OF UNPLANNED REACTOR TRIPS IN 1985. WEEKLY DATA DETERMINED BY TAKING TOTAL TRIPS IN A GIVEN CATEGORY AND DIVIDING BY 52 WEEKS / YEAR.
CAUSES (LIGHTNING), SYSTEM DESIGN, OR UNKNOWN CAUSE.
: 9. IN 1985, THERE WERE AN ESTIMATED TOTAL OF 541 AUTOMATIC AND MANUAL UNPLANNED REACTOR TRIPS AT 93 REACTORS (HOLDING FULL POWER LICENSES). THIS YIELDS AN AVERAGE RATE OF 5.8 TRIPS PER REACTOR
l 8.
,                              YEAR AND AN AVERAGE RATE OF 10.4 TRIPS PER WEEK FOR ALL REACTORS.
1985 INFORMATION DERIVED FROM AN ORAS STUDY OF UNPLANNED REACTOR TRIPS IN 1985. WEEKLY DATA DETERMINED BY TAKING TOTAL TRIPS IN A GIVEN CATEGORY AND DIVIDING BY 52 WEEKS / YEAR.
9.
IN 1985, THERE WERE AN ESTIMATED TOTAL OF 541 AUTOMATIC AND MANUAL UNPLANNED REACTOR TRIPS AT 93 REACTORS (HOLDING FULL POWER LICENSES). THIS YIELDS AN AVERAGE RATE OF 5.8 TRIPS PER REACTOR YEAR AND AN AVERAGE RATE OF 10.4 TRIPS PER WEEK FOR ALL REACTORS.


7,
1 7,
                                                                                                                                  .    .,_                                                           1
a,_
                            .cy a,_
.cy ENCLOSURE 3 Pa;a N2.
ENCLOSURE 3 Pa;a N2.         'l 04/21/E7.
' l 04/21/E7.
SIGNIFICANT EVENTS FREQUENCY PERFCRMANCE INDICATOR No. 3 PLANTNAME                         EVENT         EVENT DESCRIPTION           .                                              GTR CAUSE DATE
SIGNIFICANT EVENTS FREQUENCY PERFCRMANCE INDICATOR No. 3 PLANTNAME EVENT EVENT DESCRIPTION GTR CAUSE DATE
                    - 5IA!LO CAMON 2 -                   04/11!374C5THERNLTRU:S!ENTCLETOLCISOFRH?WHILEBOTHRCS                                           ~ 1 E2 'FMENT FAILURE & FERSONNEL EEROR .
- 5IA!LO CAMON 2 -
AND CCNTAIMENT BOUNDARIES BREACHED
04/11!374C5THERNLTRU:S!ENTCLETOLCISOFRH?WHILEBOTHRCS
,                      OCONEE 3-                       ' 04/11/97 YALVES TO HPI INJECTION PURFS FOUND ISOLATED DURING 2 PER$0h 2 ERROR HEATUP e
~ 1 E2 'FMENT FAILURE & FERSONNEL EEROR.
:e s, .
AND CCNTAIMENT BOUNDARIES BREACHED OCONEE 3-
' 04/11/97 YALVES TO HPI INJECTION PURFS FOUND ISOLATED DURING 2 PER$0h 2 ERROR HEATUP e
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Latest revision as of 21:42, 3 December 2024

Summary of Operating Reactors Events Meeting 87-11 on 870420.List of Attendees,Viewgraphs & Input to NRC Performance Indicator Program Encl
ML20215L328
Person / Time
Site: Calvert Cliffs, Oconee, River Bend, Diablo Canyon, 05000000
Issue date: 05/05/1987
From: Lanning W
Office of Nuclear Reactor Regulation
To: Rossi C
Office of Nuclear Reactor Regulation
References
OREM-87-011, OREM-87-11, NUDOCS 8705120189
Download: ML20215L328 (28)


Text

_.

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t gg MEMORANDUM FOR:.

Charles E. Rossi, Director Division of Operational Events Assessment.

a FROM:

-Wayne Lanning, Acting Chief Events Assessment Branch Division of Operational Events Assessment

SUBJECT:

SUPMARY 0F THE OPERATING REACTORS EVENTS

. MEETING ON APRIL 20, 1987 - MEETING 87-11 On April 20, 1987, an Operating Reactors Events meeting (87-11)'was held to brief senior managers from NRR, RES, AEOD and Regional Offices en events which occurred since our last meeting on April _ 6,1987. The list ~of' attendees is included as Enclosure'1.

The events discussed and the significant elements of these events are presented in Enclosure 2. provides a summary of those presented events that will be input to NRC's performance indicator program as significant events.

Od; int Siimed By:

Wayne Lanning,. Acting Chief Events. Assessment Branch Division of Operational Events Assessment

Enclosures:

As stated i

cc'w/ Encl.:

See Next Page L

cc w/ Encl.:

See Next Page

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MEMORANDUM FOR:

Charles E." Rossi, Director i

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.PEETING ON APRIL-20,- 1987J : MEETING 87 \\

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. On April 20, 1987, an Operating Reactors Events meeting (87-11) was held to -

brief the Offic'e Director, the: Division Directors and their! representatives on

' events which occurred sincefour last meeting on April 6,.1987. The list of:

4 attendees is.inc.luded as Enclosure 1.

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Wayne Lanning, Acting Chief i

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Enclosures:

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3 PEMORANDUM FOR:-

Thomas E. Murley,. Director.

0ffice of Nuclear. Reactor.' Regulation i.

. Wayne Lanning, Acting Chief FROM:

Events Assessment Branch

Division of' Operational Events Assessment-SUB ECT:

SUMMARY

0FLTHE OPERATING REACTORS EVENTS PEETING ON 1987 - MEETING 87-dn Apriig20,,1987, an ~0peratina-Peactor Events meeting (87-11) was held to.

~

.i

~brief the Office. Director, the Division Directors and their representatives on '

events which occurred:since our last meeting on~ April 6,1987. The list _of.

attendees is, included as En' closure 1.

S; The events' discussed and the'significant elements of these. events' are presented in Enclosure 2g-; Enclosure 3 provides a summary of:those presented events that will be input to NRC's-performance indicator program as.significant events.

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Wayne Lanning, Acting Chief

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arr MEMORANDUM FOR:

Charles E. Rossi, Director Division of Operational Events Assessment

-FROM:

Wayne Lanning, Acting Chief Events Assessment Branch Division of Operational Events Assessment

SUBJECT:

SUMMARY

OF THE OPERATING REACTORS EVENTS.

MEETING ON APRIL 20, 1987 - MEETING 87-11 On April 20, 1987, an Operating Reactors. Events meeting -(87-1k)J was held to

.brief senior managers from NRR, RES, AEOD and Regional Offices, on e' vents which occurred since our last meeting on April 6,1987. The list'of attendees is included as Enclosure 1.

The events discussed and the significant elements of these events are presented in Enclosure 2. provides a summary of those presented events that will be input to NRC's performance indicator program as significant events.

,/

))W Waynd Lanning, Ac ing hief Events Assessment Division of Operational Events Assessment

Enclosures:

As stated cc w/ Encl.:

See Next Page l

I-Those Listed-.

. ~.

cc:. T.. Murley -

J. Crews, Reg. Y J. Sniezek C. Trammell-J. Taylor H. Schierling E. Jordan G. Knighton E. Beckjord H. Pastis W. Russell, Reg. I B. Youngblood

.J. Nelson Grace, Reg. II S. Stern B. Davis, Reg. III J. Calvo R. D. Partin, Reg. IV S. McNeil J. R. Martin, Reg. V R. Capra W. Kane, Reg. I L. Reyes, Reg. II C. Norelius, Reg. III E. Johnson, Reg. IV D. Kirsch, Reg. V

.R. Starostecki F. Miraglia S. Varga D. Crutchfield B. Boger G. Lainas G. Holahan F. Schroeder L. Shao J. Partlow B. Grimes F. Congel H. Miller E.- Weiss S. Black T. Partin, EDO E. Merschoff i

__x._

ENCLOSURE 1 LIST'0F ATTENDEES OPERATING REACTCRS EVENTS BRIEFING (27-11)

APRIL 21, 1987 NAME DIVISION NAME DIVISION C. Rossi NRR A. Thadani NRR W. Lanning NRR R. Scholl NRR K. Heitner NRR M. Caruso NRR G. Lainas NRR C. Schulten NRR P. Baranowsky NRR T. Greene NRR F. Schroeder NRR J. Calvo NRR L. Spessard AE0D H. Pastis NRR J. Youngblood NRR G. Knighton NRR S. Black NRR J. Shapaker:.

.NRR T. Martin EDO J. Partlow' NRR T. Chan NRR T. Novak AE00 R. Lob'el NRR J. Thompson NRR J. Stefano NRR S. Stern NRR J. Rosenthal AEOD J. Carter NRR l

E. Weiss AEOD J. Richardson NRR B. Grimes NRR H. Miller NRR L. Shau NRR R. Starostecki NRR E. Jordan AE00 S. Varga NRR C. Berlinger NRR D. Crutchfield NRR B. Boger NRR F. Miraglia NRR W. Minners DRPS G. Holahan NRR i

W. Swenson NRR D. Oudinot NRR l

l

[

ENCLOSURE 2 OPERATING REACTORS EVEtlTS BRIEFING 87-11

~

APRIL 21, 1987 DIABLO CANYON 2 LOSS OF RESIDUAL HEAT REMOVAL AND RCS THERMAL TRANSIENT OCONEE 1, 2, 8 3 FOULING OF LOW PRESSI'RE SERVICE WATER, LOW PPESSURE INJECTION AND REACT 0P BUILDING COOLING UNITS-UPDATE OCONEE 3 VALVES TO HIGH PRESSURE INJECTION PUMPS ISOLATED OTHER EVENTS OF INTEREST RIVER BEND QA/0C PP0BLEM FOR PROCESS COMPUTER SOFTWARE CALVERT CLIFFS 1 ESF INADVERTENT ACTUATION OF CONTAINMENT SPRAYS

4/21/87 DIABLO CANYON 2 LOSS OF RESIDUAL HEAT REM 0"Al AND RCS THERMAL TRANSIENT PROBLEM:

LOSS OF RHR WHILE IN MODE.5, MID-LOOP OPERATION WITH STEAM GENERATOR MANWAY. REMOVAL IN PROGRESS AND CONTAINMENT ECUIPMENT HATCH REMOVED, CAUSE:-

UNPLANNED DRAINAGE-FROM RCS RCS LEVEL INSTRUMENTATION ERPORS P0TENTIAL PROCEDURAL INADEQUACIES SIGNIFICANCE:

THERMAL TRANSIENT-TO BOILING CONDITIONS'WAS EXPERIENCFD IN THE RCS WHILE BOTH RCS AND CONTAINMENT EOUNDARIES WERE BREACHED P0TENTIAL FAILURE BY LICENSEE TO CLASSIFY EVENT DISCUSSION:

INITIAL CONDITIONS - MODE 5, CONTAINMENT EQUIPMENT HATCH REMOVED, STEAM GENERATOR MANWAYS BEING. REMOVED RCS DRAIN D0WN TO MID-LOOP OPERATION COMPLETED ON DAY SHIFT, VORTEXING AT RHR PUMP SUCTION OCCURRED BRIEFLY DURING THIS EVOLllTION UNEXPECTED RCS LEAKAGE COMMENCED AT APPP0XIMATELY 8:30 P.M.

OPERATORS STARTED INVESTIGATING CAUSE RHR PUMP SHUT 0FF BY OPERATORS AT APPR0XIMATELY 9:20 P.M. DUE TO ERRATIC MOTOR CURRENT CONT ' IONS SECOND RHR PUMP STARTED c.i.D PROMPTLY SHUTDOWN DUE TO~SAME CONDITIONS (OPERATORS ATTRIBUTE RHR PUMP BEHAVIOR TO SUSPECTED VORTEXING)

PHR FLOW NOT RESTORED DUE TO UNCERTAINTY REGARDING PRESENCE OF PERSONNEL IN OP NEAR STEAM GENERATORS B0ILING COMMENCED'IN RCS WITHIN APPR0XIMATELY 1 HOUR (N0 RCS TEMPERATURE INDICATION AVAILABLE)

SHIFT FOREMAN DECLARED SIGNIFICANT EVENT (50.72 NOTIFICATION) AT 10:23 P.M. BASED ON EXCEEDING LCO 0F TECHNICAL SPECIFICATIONS

~

^~

l 4/21/87 DIABLO CANYON 2 OPERATORS RESTORED RHR COOLING BY ADDING WATER TO RCS FROM REFUELING WATER STORAGE TANK AND RESTARTING RHR PUMP AT.

10:48 P.M.

REC 0VERY TO MID-LOOP OPERATION ACHIEVED ON SUNDAY APRIL 12, OPERATORS CONDUCTED SPECIAL TEST TO DETEPMINE POINT OF VORTEXING BY LOWERING RCS LEVEL CONTAINMENT AND RCS INTEGRITY REMAINED BREACHED)

NOTE RCS LEVEL INSTRUPENT INDICATION WAS EPPATIC PRIOR TO AND DURING EVEFT, AT NO TIME DURING EVENT DID LEVEL INSTRUMENTATION INDICATE LOWERING OF PCS LEVEL FOLLOWUP:

AUGFENTED INSPECTION TEAM (AIT) INVESTIGATION ~CONTINU!NG CONTACT:

J. CREWS, REG. V l

l l

L

('

April 18, 1987 2330 Hrs.

4/10/87 RER EVENT

SUMMARY

Plant Status:

The Unit was in the seventh day of the first refueling outage following a shutdown on 4/3/87 at 2352 hrs.

The plant was in Mode 5 with the reactor coolant system temperature being maintained at approximately 87 F.

Preparations are in progress to install tho steam generator nossle dams.

The reactor vessel level is being maintained at approximately half loop to support the installation of the nossle dams.

Operational

- Residual Heat Removal pump 2-1 is in service Conflauration:

providing flow through both RHR heat exchangers (trains are cross-tied).

- Reactor vessel level uis being maintained by

-(,f.

balancing letdown flow to the VCT with the charging V..

flow back to the primary system (constant VCT level).

Letdown is from the RER pump discharge via HCV-133 and charging is by gravity flow from the VCT via the normal charging path (through a

non-operating centrifugal charging pump).

- Seactor Coolant System boron concentration is approximately 1997 ppm.

- The containment equipment hatch and personnel air 4

0 lock are open.

The emergency personnel hatch is closed.

Various jobs are in progress inside of containment and a continuous purge is in progress with containment ventilation exhaust fan E-3 discharging through RCV-11 and 12 to the plant vent.

Plant Equipment

- Residual Heat Removal pump 2-1 is in service and the Conf.lguration:

2-2 RHR pump is available for service.

All instrumentation associated with the RNR system is in service.

- Both Safety injection pumps are # cleared" and unavailable for service.

('

- Centrifugal Charging Pump 2-2 is OPERABLE and available for immediate service.

CCP 2-1 and the 4-Tmed $ and ts0Wed V M4snkutd<refteh 4

ca.a seet tu n m: ass n i>:se test se >e

l positive displacement charging pump are

(.

administratively tagged out but are available for service.

- The Refueling Water Storage Tank is avsilable-as a:

borated -water source with-level at-approximately 97%.

- All four scoumulators have been cleared and drained.

- Boric Acid Storage Tank 2-2 is at 80% level with a

boron concentration of 22050 ppab.

BAST 2-1 is t

empty.

Boric Acid Transfer pump 2-2 is available for service.

The 2-1 transfer pump is cleared.

- Containment Fan Cooler Unita 2-1, 2-2, 2-3 an'd 2-4 are available for service.

CFCU 2-5 is cleared.

l CFCU 2-3 is in service running in slow speed.

l

- All four steam generators have a

secondary side water level of approximately 73% wide range with the 10% atmospheric dumps open to atmosphere.

- The main and auxiliary transformer banha have been oleared and the Unit is being powered from the Startup transformer bank.

Diesel Generators 2-1, 2-2 and.1-3 are all available for servioe.

480 volt

(},

bus 2F is cleared for outage related work.

1

- All core exit thermocouples have been determinated in preparation for reactor vessel head removal.

- Post accident monitoring panels 1 and 2 are out of service for human factors related upgrades.

- Plant vent high range radiation monitor RM-29 is out of service.

All other required process and area radiation monitors are in service.

P r

Shift Turnover:

The previous watch had completed draining of the steam generator U-tubes per operating procedure OP A-2:II.

During the draining, it was noted that the U-tubes began to drain once vessel level as indicated on the RVLIS system reached 107'-3".

It wa's reported that once the U-tubes had drained, level dropped to 106'-6" where signs of RHR pump cavitation were noted.

Once level had been restored to 107'-0",

indications of pump cavitation or vortexing stopped and level was stabilised at 107'0".

Work was ongoing to uncouple and backseat the Reactor coolant Pumps.

Various 7-L..

containment penetration leak tests were ongoing.

2 g.d seet E*5 3ers ywrsn EP:ee 486TAE90

+

2

(

TIME EVENT DESCRIPTION DATA SOURCE

:============v==================================================

4/10/87 1700 Bra Early in the shift, the Shift Foreman SFM/C0 informs the Control Operator that due to Statements the planned work to remove the steam generator primary manways, the reactor vessel level should be maintained below approximately 107'-8".

This would assure that rater would not be allowed to spill over irto the steam generator lower head area from the RCS loops.

Since indicat ions of RHR pump suotion vortexing had been stopped on the previous shift by raisint vessel level to 107'-0",

the CO planned to maintain vessel level between 107'-0" to 1078-8" during the shift.

( 1850 Hrs Since assuming the watch at approximately CO Log

~

1700

hrs, the vessel water level as

(".

indicated on the RVLIS system had slowly C0 Statement risen to the 1078-8".

Vessel level is reduced back to 107'-0" by rejecting water back to the RWST via valve 8741.

2010 Hrs An Engineer enters the containment to Engineer's begin draining containment penetration 45 Statement in preparation to perform Surveillance i

Test Procedure V-645.

STP V-845 is the Security Local Leak Rate Test (LLRT) for that Computer penetration.

The penetration was cleared by the Operations Department on 4/9/87 to allow the leak rate test to be completed (CR 00006713).

The penetration serves the Reactor Coolant Pump seal leakoff return line to the Volume Control Tank.

2041-The Engineer enters the regenerative heat Engineer's exchangsr room and opens CVCS-314 as part Statement of the : procedure to drain the penetzation prior to beginning the leak rate test.

YCT on P-250 The Engineer verifies flow through the Trend Recorder drain valve and then exits

.the containment to log onto another SWP while the peaetration is draining.

Since the (s

clearan,:e request for the job was approved the previous

day, the Shift P

i 3

a.w.wws.o a.

==

Foremati was unaware that the diraining of

(

the per etration was ongoing at this time. '

Due to a

leaking boundary

. valve associrited with.the clearance, a

drain path is created betwaan the VCT sud the

~

VCT level _immediately begins to decreas.e.

2051 Hrs contro3 Room operators note the downward VCT on P-250 trend in VCT level and increase letdown Trend Recorder from the primary system to stabilize VCT level ty further opening HCV-133.

Due to the ir. crease in letdown

flow, reactor vessel level begins to slowly decrease.

2054 Hra While trying to determine the cause of operator's the level decrease in the

VOT, the Statement Control' Operator contacts the AO at the Auxiliary Building control board to P-250 Alarm determine if any unusual evolutions are Printout occurring.

The AO reports that the RCDT level has increased.

While they are on the phene, the RCDT pump starts on high level.

The C0 requests that the A0 estimate the flow rate into the RCDT and

[c.

report bach $o the Control Room.

Control ; Room receives notification that SFM Log

.v the.RCP4 have been uncoupled and are backseated.

2124 H s 3) from Due to the apparent loss of inventory VCT on P-250 kgg 26 the primary system.

Operators Trend Recorder

  • g,

j isolate the charging and letdown flow paths.

The loss of letdown flow to r,he RVLIS on P-250 VCT>causes VCT level to rapidly decrease.

Trend Recorder Level decrease in the primary system stops (107'-4").

Auxiliary Building A0 reports to the C0 statement Control room that the estimated leakage into the RCDT is approximately 30 syn.

')hj' 2125 Hrs Operato:es notice amps on the 2-2 RER pump P-250 Alarm

/0 I WY beginning to fluctuate.

The pump is shut Printout A M,1 l,y down a:'ter starting the 2-1 pump.

Ampe also fluotuate on the 2-1 pump and it is SIM Statement secured almost immediately. Operators are dispatched to vent the pumps and seal

(.,

coolers on both RHR pumps.

4 90*d SBEC EP5 6 *g58 3*u*H*s (1 Et*:80 486L'87/PO

(-

.Due to the unexpected RHR pump cavitation

  • SFH Statement or vartexinsi operatora suspect the validity of the JRVLIS ' indication.--

An operator -is sent into containment to verify level indication on Tygon" Tube.

Outage Coordinator is requested to. verify SFM Statement the at-stus of the work on Steam Generator manway.s.

Operators continue work to locate the SFH Statement source of the leakage.

2138 Hrs Operators close LCV-1120 to stop Co Los inventory loss from the VCT.

This valve isolatos the VCT from the RCDT.

The level decrease in the VCT stops.

2147 Hrs The Engineer performing the leak rate Security test re-enters the containment to Computer continue the local leak rate test.

2200 Hrs The vent valves associated with the Engineer

[7-penetration being drained are opened.

Statement I

'l After opening the valves, the Engineer goes to find a Decon Tech to assist with the leth rate test.

2203 Bra Contro3 Room is notified that the venting co Los on the 2-1 RHR pump has been completed.

2221 Brs Control Room has received notification SFH that the Tyson Tube level is between Statement kh./.b;-

106'-9" and 107'-0".

The Control l

Alb Operator throttled 'the discharge and P-250 Alarm 8 s/

started RER 2-1.

Pump was vented before Printout i

and during the re-start.

Pump amps are awinging by about 20 amps.

Pump is immediately shut down.

2223 Hrs Shift Foreman declares a

Significant SFH Log Event.

s' 5

g.d MM n m pj 3 a v s n tv:N IN "'"

=--:==n:

2

L

~(.

2225 Hrs Operaters re-cpen LCV-112C in an attempt t VCT on P-250 to localise the source of the leakage.

Trend Recorder VCT level again begins. to decrease.

I Operatcra close LCV-112C and VCT level CO Statemen\\Y stabilises.

2226 Hrs The Engineer performing the leak rate Engineer test finds a large amount of water on the Statement 91' elevation of the containment and believes that the water is associated with his draining of the penetration.

He notifies Rad Protection personnel of the spill and isolates the vent valves from the penetration.

2230 Hrs HP Tech on the 140' elovation of HP Tech containnent notices airborno activity Statement levels increasing and begins taking air samples to locate the

source, Rad Protection personnel begin evacuation of workers off of the 115' eleva. tion due to elevated airborne readings.

(; 2233 3rs HP Tech on 115' elevation notes HP Tech background on friskers exceeding.the X10 Statement soale.

Continuous Air Monitors on the 140' elsvation are alarming.

2238 Hrs Operations personnel believe steam is CO Log being generated in the head as indicated by a

slow trend up on the RVLIS SFM Statement

  • indication.

The Control Operator is notifieil that th; Steam Generator primary manways have not been removed.

Valves 8805 A and B are opened to establish makeup

,o the remotor vessel.

2243 !!ra HP Foroman is notified by the Control EP Tech Room of a possible containment evacuation Statement due to the problems with the IUDL system.

HP Forenan then enters the contaisment to begin evacuation of unnecessary personnol.

(.

6 gg d Seeg Ep5 6 *D3ti 0*ti'N'S*P FP:80 486DB2/PO

. /.*

' - 2250 Hrs

(

The Cet Trol Room is notified by personnel Engineer inside of containment that the leak path

-Statement it.ontified as being associated was' with the Inah rate test and that the-leakage was ist. lated (valve CVCS-314).

gU i

2251 Bra Reactor vessel level is indicating RVLIS on P-250 4,IJ, & h,lN. 3 ft 0D 1 approximately 1108 Operators start RHR Trend Recorder

/' pump i:-2.

Pump amps fluotuate slightly v'

immedia,tely after the. pump

start, but P-250 Alarm stabilise.

Printer Short1r following the pump

start, RHR pump discharge temperature on the control RHR Discharge Temp Recorder board recorder rises to approximately 220 F.

Within 6

minutes, the pump discharge temperature has dropped to less than 2C 0 F.

2253 Bra Operatcra note minor indication of BFH Log cavitation on the running RHR pump.

i Valve 8980 (RWST to RER auction) is CO Log partially opened to increase makeup to the reactor vessel.

0-)

Pump amps stabilise.

2258 Hrs Control room receives notification of SFM Log Q

steam venting from a ruptured tygon tube

,g on the reactor head vent.

Containment Evacuation alarm initiated at the direction of the Shift Foreman.

i SFM Log f

2310 3rs Shift Foreman requests that the operator inside of conatinment isolate the reactor HP Tech /CO head Statements vant which is supplying the steam leak i.n the tygon hose.

HP Tech and operator descend to head area and isolate the le.sk.

No visible condensation or water i.: noted in the area.

2313 Hra Control room notified that the reactor CO Log vessel head vent has been isolated.

7 g.d mBE'Et3 n 'U3H 3*W N'S*P SP:00 486t/8E/PO

- - ::n

232n Hrs Control Room is notified by HP Fersonnel SFM Statement

'r that the containment airborne is greater' than 1

MPC and is high in Iodine.

C0 Log

('

Operat ors place the containment Iodine Remova.1 fans into service to attempt t'o reduc < airborne activity.

232! Hrs Shift Foreman goes to the containment Security persor nel hatch to verify the status of Computer the ocntainment evacuation.

While there, he in informed by the RP Foreman of the SFH/RP Foreman water leakage from the steam generator Statements manway s.

2342 Hrs Level in the pressurizer has reached CO Los approximately 40%.

Operators begin divert ing letdown flow to the LHUT to reduce level and minimize the leakage from the steam generator manways.

0044 Hrs Operators open valve 8741 to begin CO Log pumping primary system water back to the RWST to further reduce level in the primary system.

Letdown divert to the

(,.

LHUT is secured at this time.

0102 Bra Operators stop rejecting water back to CO Log /

the RWST.

Valve 8741 closed.

RVLIS RVLIS on P-250 indicating approximately 114'-0".

Trend Recorder 0320 Hrs Reactor vessel level is reduced to half-CO Log loop asd leakage from the steam generator manways is stopped.

RVLIS indication at approximately 108'-4".

V 8

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4/21/87' OCONEE 1, 2, AND 3 - FOULING OF LOW PRESSURE SERVICE WATER, 1.0W PRESSl!PE INJECTION AND REACTOP PUILDING COOLING UNITS llPDATE PROBLEM:

REDUCED HEAT TRANSFER CAPABILITY OF THE LOW PRESSURE INJECTION (LPI) AND REACTOR BUILDING COOLING UNIT 1RBCU) HEAT EXCHANGERS LIMITS REACTOR OPERATING POWEP CAUSE:

LAKE SEDIMENT DEPOSITED IN HEAT EXCHANGERS SIGNIFICAPCE:

SAFETY EQUIPMENT INCAPABLE OF PERFORMING THE DESIGN HEAT REJECTION SAFETY FUNCTION DISCUSSION:

THE LOW PRESSURE SERVICE WATER SYSTEM TAKES RAW LAKE WATER TO C00L THE LPI AND RBCU HEAT EXCHANGERS LICENSEE ANALYZED THE TEST DATA AND CORRELATED IT TO EMERGENCY CONDITIONS THE-ANALYSIS SHOWED THAT UNDER LOCA CONDITIONS, THE PEAT EXCHANGERS WOULD NOT PERF0PM AT DESIGN RATING J

UPDATE:

ON APRIL 10, 1987, NRR ISSUED A CONFIRMATORY ORDER WHICH REQUIRED THAT THE HEAT EXCHANGERS BE CLEANED AND TESTED REACTOR OPERATION AT LOWER POWER LEVELS WITHIN THE HEAT TRANSFER CAPABILITY OF THE HEAT EXCHANGERS THE REACTOR HIGH FLUX TRIP SETPOINTS TO BE REDUCED CONTACT:

H. PASTIS, NRR

- -_ _ _ j

4/21/87 OCONEE 3 VALVES TO HIGH PRESSURE INJECTTON PUMPS ISOLATED

-PROBLEM:

BOTH MOTOR OPERATED SUCTION VALVES FROM THE B0 RATED WATER STORAGE TANK TO THE HIGH. PRESSURE INJECTION PUMPS WERE IN THEIR NORMAL Cl.0 SED POSITION BUT THE MOTOR SUPPLY BREAKERS WERE OPEN.

CAUSE:

NUMEROUS PERSONNEL ERRORS SIGNIFICANCE HIGH PRESSURE INJECTION SYSTEM COULD NOT HAVE RESPONDED TO AN ENGINEERED SAFEGUARDS SIGNAL DISCUSSION:

OCONEE UNIT 3 WAS HEATING UP WHEN VALVES VERE DISCOVERED INOPERABLE FOR TWENTY HOURS SITl'ATION CORRECTED IMMEDI ATELY UPON IDENTIFICATION FOLLOWUP:

ENFORCEMENT CONFERENCE HAS BEEN SCHEDULED l

CONTACT:

H. PASTIS, NRR

4/21/87-OTHER EVENT OF' INTEREST.

RIVER BEND - QA/0C PROBLEM FOR PROCESS COMPUTER SOFTWARE PROBLEM:

RIVER BEND STATION EXCEEDED LICENSED THEPMAL LIMIT CAllSE:

INADEQUATE QA/0C BY VENDOR ON SOFTWAPE'FOR-PROCESS. CONTROL COMPUTER SIGNIFICANCE:

QA/QC 0N SOFTWARE FOR PLANT COMPUTER ERROR IN SOFTWARE OF A NON-SAFETY PELATED COMPUTER IMPACTS POWER LEVEL DISCUSSION:-

ON.MAY 13, 1987, LICENSEE INSTALLED VENDOR SUPPLIED SOFTWARE 0N PLANT COMPUTER VEND 0F, GE, STATED SOFTWARE ONLY' IMPACTS B0P PARAMETERS LICENSEE HAD BENCH CHECKED SOFTWARE AGAINST VEND 0P SPECIFICATIONS ALERT OPERATOR NOTICED COMPUTER' THERMAL POWER READ 0VTS NOT CCRRECTLY RESPONDING TO CHANGES IN RECIRCULATION FLOW LICENSEE REDUCED POWER, SilBSTITUTED OLD SOFTWARE - PP0BLEM RESOLVED.

' THERMAL LIMIT EXCEEDED FOR MAXIMUM 0F FOUR HOURS PEAK THERMAL POWER 101,15 LICENSE LIMIT FOLLOWUP:

LICENSEE /GE PERFORMING IN DEPTH ROOT CAUSE ANALYSIS REGION IV FOLLOWING UP WITH LICENSEE, WILL ISSUE INSPECTION REPORT VENDOR INSPECTIONS FOLLOWING UP WITH GE INFORMATION NOTICE ON MAXIMUM LICENSED POWER LEVEL UNDER REVIEW BY NRR CONTACT:

S. STERN, NRR

4/21/87 OTHER EVENT OF INTEREST CALVERT CLIFFS 1 - ESF INADVERTENT ACTUATION OF CONTAINMENT SPPAYS PROBLEM:

ESF INADVERTENT ACTUATION OF CONTAINMENT SPRAYS CAUSE:

OPERATOR ERROR SIGNIFICANCE:

INADVERTENT SAFETY SYSTEM ACTUATION RESULTING FROM GPEPATOR ACTIONS ON WRONG UNIT POTENTIAL FOR ELECTRICAL EQUIPMENT DEGRADATION DUE TO WETTING BY BORATED WATER (BORIC ACID INTRUSION)

PERSONNEL CONTAMINATION

- DISCllSSION:

UNIT 1 IN MODE 5, ELECTRICAL TERMINAL B0XES OPENED FOR EQ MAINTENANCE, AND CONTAINMENT SPRAY CONTAINMENT ISOLATION (CS/CI)

BLOCK VALVE DE-ENERGIZED (FAIL OPEN) FOR EQ MAINTENANCE OPERATOR ON 12-HOUR SHIFT; UNIT 2 (4:00-8:00 A.M.), UNIT 1 (8:00 A.M.-4:00 P.M.)

OPERATOR ERRCNE00 SLY WENT TO UNIT 2 PENETRATION ROOM INSTEAD OF UNIT 1 PENETRATION ROOM FOR CLOSURE OF CS/CI VALVE FOLLOW-UP:

LICENSEE WILL:

ANALYZE POTENTIAL SAFETY IMPLICATION OF OPENED TERMINAL B0XES TO BORIC ACID DEGRADATION INVESTIGATE THE HUMAN ERROR AND CONTRIBUTING FACTORS INVOLVED FOR THE WRONG UNIT EVENT INVESTIGATE POSSIBLE UNIT 1/ UNIT 2 LABELING INADE0tlACIES FOR EQUIPMENT REGION I TO FOLLOW UP ON CORRECTIVE ACTION MEASURES TAKEN BY LICENSEE, INCLUDING LATE NOTIFICATION OF 50,72 CODE SECTION ON REPORTABLE EVENTS FOR OPERATION OF ESF SYSTEMS CONTACT:

J. THOMPSON, NRR

i; REA
iDR SCRAM SUVARY WEEK ENDINS 04/12/87

!.-PLANT SPECIFIC DATA IATE SITE LNIT F0sER E 3 CcUEE COMPLI-VT3 YT3 Yi; CAI D i 43IiE EELCd 70TAL 151 !!!

04/06/97 FARLEY OA EQUIFMENT/SRM N0 3

1 4

04/06/37 FERN!

2 31 A FER3CNhEL NO

'3 0

-3 04/07/S7 EALEM 2

90 A -UNrNCWN NO 2

1 3

04/09/37 CATAWiA 1

100 A E901FMENT/ VALVE YES 3

0-3 04/09/87 CATAWBA

'1 0M EGUIPMENT/RPI NO ~

3 1

4 04/09/87 SAINTLUCIE 2 100 A PERSCMMEL NO 3

0' 3

04/10/B7DREitEN 3 100 A EQUIPMENT / PIPE NO 2

0 2

04/10/97VOSTLE 1

30 A EQUIFMENT/VALVENO 2

6 8

04/11/97V05TLE 1

21 A EQUIFMENT/ VAL'lE NC 3

6 9

04/12/67 PALISA:ES 1

75 M EQUIPMENT / PIPE NO-1 0

1 04/12/97 MILLSTONE I

66 A EGUIFMENT/ PUMP NO

~3 1

4 02/12/37 PARRIS 1

65 M FI'!:NNEL NO 7

2 9-04/!2!37 MILLSTChE 10 A PERICUEL NO 3

2 i

SUMMARY

OF COMPLICATIONS SITE liNIT COMPLICATIONS CATAWBA 1 BORCN DILUTICN MITISATION SYSTEM INITIATED ESF AFTER SCRAM

~ _ _... -,.....

y II. COMPARISON OF WEEKLY ETATISTICS-WITH INDUSTRY AVERAGES SCRAMS FOR WEEK ENDING 04/12/87 ECRf41 CAUSE POWER NUMBER

-1997 1986 1985 CF WEEELY WIEKLY WEEKLY SCRAM 3(5)

AVERAGE AVERAGE AVERAGE YTD (3)(4)

(8) (9)

    • FOWER 15%

EOUIP. RELATED

>15%

6 3.9 4.3 5.4 PERS. RELATED(6) >15%

3 1.7 1.8 2.0

-OTHER(7)

>15%

1 1.0 0.4 0.6

    • Subtotal **

10 6.5 6.5 8.0 t*

POWER <15%

EQUIP. RELATED

<15%

2

'i. 2 1.4 1.3 PERS. RELATED

<15%

1 1.O O.8 O.9 OTHER

<15%

0 O.4 O.2 0.I tk Gubtotal i4 3

2. 6.'

2.4 2.1 4t1 fatal 414 13 9.' 1 9.9 10.4 MANUAL VS AUTO SCRAMS TYPE NUMBER 1987 1986 1985 i

OF WEEKLY WEEKLY NEEKLY SCRAMS AVEPAGE AVERAGE AVERAGE YTD MANUAL SCRAMS 3

1.5 1.O 1.O AUTOMATIC SCRAMS 10 7.5 7.9 9.4

gp

]P' r

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. y ? -d.

',y

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[? "

REACTOR.iCRAM 5'.i? MARY ~

!di

[ WEEKENDING 04/19/67

!. PLANT SPECIFIC DATA i

id iO CATE.

$1TE. d ti!T,?0'4ER RFS CAUSE

-C3.9.!-

YT3. YTD' : fTD

./

CATIONS ??!'iE iELOW -TCTAL g i-151 15%

W

'04/13/97 WATERFORD.

'3.100 A EQUIPMENT /CEAC NO

.3 01 3;

.04/13/97 PERRY 10 M ' E2VIFMENT/ FIFE NO 1-2 3

~04/14/97 SA!MT LUCIE 1

0A FERSONNEL -

' NO.

0 2-2

- 04/14/97 HMRIS -

87 M. FERSONNEL

. N3 3

2

-10 e

04/15/97 MC6UIRE 1 ' 100 A UNtNCH NO 2

0 2

04/15/97 WATERFORD 3 - 50 A PEFSONNEL~

NO-

/4 0

4 e.

W.

M'

" 04/16/87 HALDAM NECK l'!;'100 A UNKNGWN NO 1

.O.

1 3

' rh -

04/15/97 MILLSTONE 2 100 A EQUIPMENT /BKR NO 2

0 2

~

  • 2 100 A UNENEWN-NO 1

0 1

04/16/27.!US20EHANNA

~g 04/16/87 PALD VERSE 2 100 A UNKNOWN -

NO

,t 0

1 2#

!Y 04/17/97 INI!AN FDIh?

3. 100 A UNKNCWN N0' 3

1 4

'4.

-04/19/57 WOLF MEEX-10 A - dKG41 N0 3'

0-3 04/19!67 N*.Riii ANNA 1,

!! A EGU!F?ENT/C ?E M

'l 0

1

'[

.,p f

1*

r.

/

i O

f

+

l s -'

y'

)p '

.Q y

l l

19 tc

). '

>f I

L

.f(

l I

I i

i l

L...

- g II. COMPARISON OF WEEKLY STATISTICS WITH INDUSTRY AVERAGES SCRAMS FOR WEEK ENDING s

04/19/87~

SCRAM CAUSE POWER NUME.ER 1987 19S6 1925 OF WEEf:LY WEEi'LY WFI; _Y ECRAME (3 )

AVERAGE AVERAGE A'.'ERAGE YTD (3) (4)

(S)(9)

    • POWER >157.

EQUIP. RELATED

> 15 *'.

3 3.7 4.0 5.4 FERS. RELATED(6) >15%

2 1.7 1.2 2.0 OTHER(7)

>15%

6 1.3 0.4 0.6

    • Subtotal **

11 6.7 6.5 8.0 t* POWER <15%

EQUIP. RELATED

<15%

1 1.2 1.4 1.3 PERS. RELATED

<15%

1

1. 0 0.8 0.9 OTHER

'15%

o O.4 0.2 O.2 kt Subtet=1 tv 2

2.S

2. 4 Z.'

444 Total 161 13 9.3 8.9 10.4 MANUAL VS AUTO SCRAMS TYPE NUMBER 1987 1986 1985 OF WEEV.LY WEEKLY WEEKLY ECRAMS AVERAGE AVERAGE A'/ERAGE YTD MANUAL SCRAMS 2

1.5 1.0 1.0 AUTOMATIC SCRAMS 11 7.8 7.9 9.4

[.

s

3 NOTES 1.

PLANT SPECIFIC DATA PASED ON INITIAL REVIEW OF 50.72 REFORTS FOR THE WEEK OF INTEREST. PERIOD IS MIDNIGHT Sl!NDAY TPROUGH MIDNIGHT SUNDAY SCRANS ARE DEFINED AS REACTOR PROTECTIVE ACTUATIONS WHICH RESULT IN ROD MOTION, AND EXCLUDE PLANNED TESTS OR SCRAMS AS PART OF PLANNED SHUTDOWN IN' ACCORDANCE WITH A PLANT PROCEDURE.

2.

RECOVERY COMPLICATED BY EQUIPMENT FAILURES OR PERSONNEL ERRORS UNRELATED TO CAUSE OF SCRAM.

3.

1986 INFORMATION DERIVED FROM ORAS STUDY OF UNPLANNED REACTOR TRIPS IN 1986. WEEKLY DATA DETERMINED BY TAKING TOTAL TRIPS IN A GIVEN CATEGORY AND DIVIDING BY 52 WEEKS / YEAR.

A.

IN 1986, THERE WERE AN ESTIMATED TOTAL OF 461 AUTOMATIC AND MANUAL UNPLANNED REACTOR TRIPS AT 104 REACTORS (HOLDING OPERATING LICEN$ES). THIS YIELDS AN AVERAGE RATE OF 4.4 TRIPS PER REACTOR PER YEAR AND AN AVERAGE RATE OF 8.8 TRIPS PER WEEK FOR ALL REACTORS.

5.

BASED ON 107 REACTORS HOLDING AN OPERATING LICENSE.

6.

PERSONNEL RELATED PROBLEMS INCLUDE HUMAN ERROR, PROCEDURAL DEFICIENCIES, AND MANUAL STEAM GENERATOR LEVEL CONTROL PROBLEMS.

1 I

i 7.

"0THER" INCLUDES AUTOMATIC SCRAMS ATTRIBUTED TO ENVIRONMENTAL j

CAUSES (LIGHTNING), SYSTEM DESIGN, OR UNKNOWN CAUSE.

l 8.

1985 INFORMATION DERIVED FROM AN ORAS STUDY OF UNPLANNED REACTOR TRIPS IN 1985. WEEKLY DATA DETERMINED BY TAKING TOTAL TRIPS IN A GIVEN CATEGORY AND DIVIDING BY 52 WEEKS / YEAR.

9.

IN 1985, THERE WERE AN ESTIMATED TOTAL OF 541 AUTOMATIC AND MANUAL UNPLANNED REACTOR TRIPS AT 93 REACTORS (HOLDING FULL POWER LICENSES). THIS YIELDS AN AVERAGE RATE OF 5.8 TRIPS PER REACTOR YEAR AND AN AVERAGE RATE OF 10.4 TRIPS PER WEEK FOR ALL REACTORS.

1 7,

a,_

.cy ENCLOSURE 3 Pa;a N2.

' l 04/21/E7.

SIGNIFICANT EVENTS FREQUENCY PERFCRMANCE INDICATOR No. 3 PLANTNAME EVENT EVENT DESCRIPTION GTR CAUSE DATE

- 5IA!LO CAMON 2 -

04/11!374C5THERNLTRU:S!ENTCLETOLCISOFRH?WHILEBOTHRCS

~ 1 E2 'FMENT FAILURE & FERSONNEL EEROR.

AND CCNTAIMENT BOUNDARIES BREACHED OCONEE 3-

' 04/11/97 YALVES TO HPI INJECTION PURFS FOUND ISOLATED DURING 2 PER$0h 2 ERROR HEATUP e

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