ENS 56912: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot change)
(StriderTol Bot change)
 
(One intermediate revision by the same user not shown)
Line 15: Line 15:
| NRC officer = Brian Parks
| NRC officer = Brian Parks
| event date = 01/03/2024 12:57 EST
| event date = 01/03/2024 12:57 EST
| last update date = 01/03/2024
| last update date = 02/12/2024
| title = Pressure Boundary Degraded / Both Trains of High Pressure Safety Injection Inoperable
| title = Pressure Boundary Degraded / Both Trains of High Pressure Safety Injection Inoperable
| event text = At 1257 EST on January 3, 2024, it was determined that a class 1 system barrier had a through wall flaw with leakage.  The leakage renders both trains of high pressure safety injection inoperable.  The unit is being cooled down to cold shutdown to comply with technical specifications.
| event text = At 1257 EST on January 3, 2024, it was determined that a class 1 system barrier had a through wall flaw with leakage.  The leakage renders both trains of high pressure safety injection inoperable.  The unit is being cooled down to cold shutdown to comply with technical specifications.
Line 22: Line 22:
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officer Report Guidance:
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officer Report Guidance:
At the time of the discovery, the unit was shutdown in mode 3. The unit was experiencing signs of reactor coolant system leakage and a shutdown was initiated in order to search for possible sources. The unit is currently cooling down and proceeding to mode 5, where the safety function is not required.
At the time of the discovery, the unit was shutdown in mode 3. The unit was experiencing signs of reactor coolant system leakage and a shutdown was initiated in order to search for possible sources. The unit is currently cooling down and proceeding to mode 5, where the safety function is not required.
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2024/20240104en.html#en56912
* * *UPDATE AT 1257 EST ON 02/12/24 FROM B. MURRELL TO T. HERRITY***
The purpose of this notification update is to retract a portion of a previous report, made on 1/03/2024 at 1257 EST (EN 56912). Notification of the event to the NRC was initially made as a result of declaring both trains of unit 2 high pressure safety injection system inoperable due to reactor coolant barrier through wall leak on the vent line for the 2A2 safety injection tank.
Subsequent to the initial report, Florida Power and Light has concluded that the through wall leak rate was insignificant, and therefore the safety injection system's safety-related function was maintained.
Therefore, this portion of the event is not considered a safety system functional failure and is not reportable to the NRC pursuant 10 CFR 50.72(3)(v)(D).
This update does not affect the original 10 CFR 50.72(b)(3)(ii)(A) report for the degraded condition related to the reactor coolant barrier through wall leak.
The NRC Resident Inspector has been notified.
Notified R2DO (Miller).
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2024/20240213en.html#en56912
}}{{unit info
}}{{unit info
| Unit = 2
| Unit = 2

Latest revision as of 07:30, 13 February 2024

ENS 56912 +/-
Where
Saint Lucie NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded

10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Time - Person (Reporting Time:+-2.32 h-0.0967 days <br />-0.0138 weeks <br />-0.00318 months <br />)
Opened: Eric Laettner
15:38 Jan 3, 2024
NRC Officer: Brian Parks
Last Updated: Feb 12, 2024
56912 - NRC Website
Loading map...