NRC Generic Letter 1980-12: Difference between revisions

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{{#Wiki_filter:me c1FW74f4L-F"4r UNITED STATES NUCLEAR REGULATORY  
{{#Wiki_filter:me c1FW74f4L-F"4r UNITED STATES
COMMISSION
                                NUCLEAR   REGULATORY       COMMISSION
REGION I 631 PARK AVENUE KING OF PRUSSIA, PENNSYLVANIA  
                                                REGION I
19406 February 8, 1980 Docket Nos. 50-03 50-247 Consolidated Edison Company of New York, Inc.ATTN: Mr. W. J. Cahill, Jr.Vice President 4 Irving Place New York, New York 10003 Gentlemen:
                                            631 PARK AVENUE
The enclosed IE Bulletin No. 80-04, is forwarded for action. A written response is required.
                                  KING OF PRUSSIA, PENNSYLVANIA 19406 February 8, 1980
  Docket Nos. 50-03
                50-247 Consolidated Edison Company of New York, Inc.


If you desire additional information regarding this matter, please contact this office.Sincerely, j Boyce H. Grier C/- Director Enclosures:
ATTN: Mr. W. J. Cahill, Jr.
1. IE Bulletin No. 80-04 2. List of Recently Issued IE Bulletins  
 
Vice President
        4 Irving Place New York, New York 10003 Gentlemen:
        The enclosed IE Bulletin No. 80-04, is forwarded for action. A written response is required. If you desire additional information regarding this matter, please contact this office.
 
Sincerely, j     Boyce H. Grier C/-   Director Enclosures:
        1.     IE Bulletin No. 80-04
        2. List of Recently Issued IE Bulletins  


==CONTACT==
==CONTACT==
: 0. L. Caphton (215-337-5253)
:   0. L. Caphton
cc w/encls: L. 0. Brooks, Project Manager, IP Nuclear W. Monti, Manager -Nuclear Power Generation Department M. Shatkouski, Plant Manager J. M. Makepeace, Director, Technical Engineering W. D. Hamlin, Assistant to Resident Manager J. D. Block, Esquire, Executive Vice President  
                    (215-337-5253)
-Administration Joyce P. Davis, Esquire.7-800,8,8,60
          cc w/encls:
il-'116'  
          L. 0. Brooks, Project Manager, IP Nuclear W. Monti, Manager - Nuclear Power Generation Department M. Shatkouski, Plant Manager J. M. Makepeace, Director, Technical Engineering W. D. Hamlin, Assistant to Resident Manager J. D. Block, Esquire, Executive Vice President - Administration Joyce P. Davis, Esquire
ENCLOSURE  
                                                        .7-
1 UNITED STATES SSINS No.: 6820 NUCLEAR REGULATORY  
                                                                      800,8,8,60 il-'116'
COMMISSION  
 
Accessions No.: OFFICE OF INSPECTION  
ENCLOSURE 1 UNITED STATES             SSINS No.: 6820
AND ENFORCEMENT  
                          NUCLEAR REGULATORY COMMISSION     Accessions No.:
7910250504 WASHINGTON, D.C. 20555 IE Bulletin No. 80-04 Date: February 8, 1980 ANALYSIS OF A PWR MAIN STEAM LINE BREAK WITH CONTINUED  
                      OFFICE OF INSPECTION AND ENFORCEMENT 7910250504 WASHINGTON, D.C. 20555 IE Bulletin No. 80-04 Date: February 8, 1980 ANALYSIS OF A PWR MAIN STEAM LINE BREAK WITH CONTINUED FEEDWATER ADDITION
FEEDWATER  
ADDITION  


==Description of Circumstances==
==Description of Circumstances==
:
:
Virginia Electric and Power Co. submitted a report to the Nuclear Regulatory Commission dated September  
Virginia Electric and Power Co. submitted a report to the Nuclear Regulatory Commission dated September 7, 1979 that identified a deficiency in the original analysis of containment pressurization as a result of reanalysis of steam line break for North Anna Power Station, Units 3 and 4.
7, 1979 that identified a deficiency in the original analysis of containment pressurization as a result of reanalysis of steam line break for North Anna Power Station, Units 3 and 4.Stone and Webster Engineering Corporation performed a reanalysis of containment pressure following a main steam line break and determined that, if the auxiliary feedwater system continued to supply feedwater at runout conditions to the steam generator that had experienced the steam line break, containment design pressure would be exceeded in approximately  
 
10 minutes. The long term blowdown of the water supplied under runout conditions by the auxiliary feedwater system had not been considered in the earlier analysis.On October 1, 1979, the foregoing information was provided to all holders of operating licenses and construction permits in IE Information Notice No.79-24. The Palisades facility did an accident analysis review pursuant to the information in the notice and discovered that with offsite power available, the condensate pumps would feed the affected generator at an excessive rate.This excessive feed was not considered in the analysis for the steam line break accident.On January 30, 1980, Maine Yankee Atomic Power Company informed the NRC of an error in the main steam line break analysis for the Maine Yankee plant.During a review of the main steam line break analysis, for zero or low power at the end of core life, the licensee identified an incorrect postulation that the startup feedwater control valves would remain positioned "as is" during the transient.
Stone and Webster Engineering Corporation performed a reanalysis of containment pressure following a main steam line break and determined that, if the auxiliary feedwater system continued to supply feedwater at runout conditions to the steam generator that had experienced the steam line break, containment design pressure would be exceeded in approximately 10 minutes. The long term blowdown of the water supplied under runout conditions by the auxiliary feedwater system had not been considered in the earlier analysis.
 
On October 1, 1979, the foregoing information was provided to all holders of operating licenses and construction permits in IE Information Notice No.
 
79-24. The Palisades facility did an accident analysis review pursuant to the information in the notice and discovered that with offsite power available, the condensate pumps would feed the affected generator at an excessive rate.
 
This excessive feed was not considered in the analysis for the steam line break accident.
 
On January 30, 1980, Maine Yankee Atomic Power Company informed the NRC of an error in the main steam line break analysis for the Maine Yankee plant.
 
During a review of the main steam line break analysis, for zero or low power at the end of core life, the licensee identified an incorrect postulation that the startup feedwater control valves would remain positioned "as is" during the transient. In reality, the startup feedwater control valves will ramp to
80% full open due to an override signal resulting from the low steam generator pressure reactor trip signal. Reanalysis of the event shows the opening of the startup valve and associated high feedwater addition to the affected steam generator would cause a rapid reactor cooldown and resultant return-to-power, a condition outside the plant design basis.
 
Actions to be Taken by the Licensee:
For all pressurized water power reactors with an operating license and those reactors listed in Attachment 1:
 
Enclosure 1                                              IE Bulletin No. 80-04 Date: February 8, 1980 1.    Review the containment pressure response analysis to determine if the potential for containment overpressure for a main steam line break inside containment included the impact of runout flow from the auxiliary feedwater system and the impact of other'energy sources, such as continuation of feedwater or condensate flow. In your review, consider your ability to detect and isolate the damaged steam generator from these sources and the ability of the pumps to remain operable after extended operation at runout flow.
 
2.    Review your analysis of the reactivity increase which results from a main steam line break inside or outside containment. This review should consider the reactor cooldown rate and the potential for the reactor to return to power with the'most reactive control rod in the fully withdrawn position. If your previous analysis did not consider all potential water sources (such as those listed in 1 above) and if the reactivity increase is greater than previous analysis indicated the report of this review should include:
      a.  The boundary conditions for the analysis, e.g., the end of life shutdown margin, the moderator temperature coefficient, power level and the net effect of the associated steam generator water inventory on the reactor system cooling, etc.,
      b.  The most restrictive single active failure in the safety injection system and the effect of that failure on delaying the delivery of high concentration boric acid solution to the reactor coolant system, c.  The effect of extended water supply to the affected steam generator on the core criticality and return to power, d.  The hot channel factors corresponding to the most reactive rod in the fully withdrawn position at the end of life, and the Minimum Departure from Nucleate Boiling Ratio (MDNBR)
          values for the analyzed transient.
 
3.    If the potential for containment overpressure exists or the reactor-re- turn-to-power response worsens, provide a proposed corrective action and a schedule for completion of the corrective action. If the unit is operating, provide a description of any interim action that will be taken until the proposed corrective action is completed.


In reality, the startup feedwater control valves will ramp to 80% full open due to an override signal resulting from the low steam generator pressure reactor trip signal. Reanalysis of the event shows the opening of the startup valve and associated high feedwater addition to the affected steam generator would cause a rapid reactor cooldown and resultant return-to-power, a condition outside the plant design basis.Actions to be Taken by the Licensee: For all pressurized water power reactors with an operating license and those reactors listed in Attachment
4.   Within 90 days of the date of this Bulletin, complete the review and evaluation required by this Bulletin and provide a written response describing your reviews and actions taken in response to each item.
1:
Enclosure
1 IE Bulletin No. 80-04 Date: February 8, 1980 1. Review the containment pressure response analysis to determine if the potential for containment overpressure for a main steam line break inside containment included the impact of runout flow from the auxiliary feedwater system and the impact of other'energy sources, such as continuation of feedwater or condensate flow. In your review, consider your ability to detect and isolate the damaged steam generator from these sources and the ability of the pumps to remain operable after extended operation at runout flow.2. Review your analysis of the reactivity increase which results from a main steam line break inside or outside containment.


This review should consider the reactor cooldown rate and the potential for the reactor to return to power with the'most reactive control rod in the fully withdrawn position.
Reports should be submitted to the Director of the appropriate NRC Regional Office and a copy should be forwarded to the NRC Office of Inspection and Enforcement, Division of Reactor Operations Inspection, Washington, D.C.


If your previous analysis did not consider all potential water sources (such as those listed in 1 above) and if the reactivity increase is greater than previous analysis indicated the report of this review should include: a. The boundary conditions for the analysis, e.g., the end of life shutdown margin, the moderator temperature coefficient, power level and the net effect of the associated steam generator water inventory on the reactor system cooling, etc., b. The most restrictive single active failure in the safety injection system and the effect of that failure on delaying the delivery of high concentration boric acid solution to the reactor coolant system, c. The effect of extended water supply to the affected steam generator on the core criticality and return to power, d. The hot channel factors corresponding to the most reactive rod in the fully withdrawn position at the end of life, and the Minimum Departure from Nucleate Boiling Ratio (MDNBR)values for the analyzed transient.
20555.


3. If the potential for containment overpressure exists or the reactor-re- turn-to-power response worsens, provide a proposed corrective action and a schedule for completion of the corrective action. If the unit is operating, provide a description of any interim action that will be taken until the proposed corrective action is completed.
Enclosure 1                                          .IE Bulletin No. 80-04 Date: February 8, 1980 For boiling water reactors with an operating license or a construction permit and all pressurized water reactors with a construction permit, not listed in Attachment 1, this Bulletin is for information purposes only and no written response is required.


4. Within 90 days of the date of this Bulletin, complete the review and evaluation required by this Bulletin and provide a written response describing your reviews and actions taken in response to each item.Reports should be submitted to the Director of the appropriate NRC Regional Office and a copy should be forwarded to the NRC Office of Inspection and Enforcement, Division of Reactor Operations Inspection, Washington, D.C.20555.
Approved by GAO, B180225 (R0072); clearance expires 7/31/80. Approval was given under a blanket clearance specifically for identified generic problems.


Enclosure
Attachment No. 1 to IE Bulletin No. 80-04 Plants with construction permits that are required to respond to the bulletin:
1.IE Bulletin No. 80-04 Date: February 8, 1980 For boiling water reactors with an and all pressurized water reactors Attachment
                    Diablo Canyon McGuire North Anna 2 Salem 2 Sequoyah If the permit holders have responded to earlier requests from the NRC on some of the items presented in the bulletin, they may respond to the bulletin by reference to the response to the earlier request.
1, this Bulletin is for response is required.operating license or a construction permit with a construction permit, not listed in information purposes only and no written Approved by GAO, B180225 (R0072); clearance expires 7/31/80. Approval was given under a blanket clearance specifically for identified generic problems.


Attachment No. 1 to IE Bulletin No. 80-04 Plants with construction permits that are required to respond to the bulletin: Diablo Canyon McGuire North Anna 2 Salem 2 Sequoyah If the permit holders have responded to earlier requests from the NRC on some of the items presented in the bulletin, they may respond to the bulletin by reference to the response to the earlier request.
-
                                ENCLOSURE 2 IE Bulletin No. 80-04 Date: February 8, 1980 RECENTLY ISSUED IE BULLETINS
  Bulletin  Subject                  Date Issued              Issued To No.


-ENCLOSURE
79-25     Failures of Westinghouse 11/2/79                 All Power Reactor BFD Relays in Safety-                             Facilities with an Related Systems                                    Operating License (OL)
2 IE Bulletin No. 80-04 Date: February 8, 1980 RECENTLY ISSUED IE BULLETINS Bulletin No.79-25 79-02 (Rev. 2)79-26 79-27 79-28 79-01B 80-01 80-02 80-03 Subject Date Issued Failures of Westinghouse  
                                                              or Construction Permit (CP) (for Action)
11/2/79 BFD Relays in Safety-Related Systems Pipe Base Plate Designs 11/8/79 Using Concrete Expansion Bolts Issued To All Power Reactor Facilities with an Operating License (OL)or Construction Permit (CP) (for Action)All Power Reactor Facilities with an OL or CP All BWR Power Reactor Facilities with an OL All Power Reactor Facilities with an OL and those nearing Licensing (for Action)All Power Reactor Facilities with a CP (for Information).
  79-02    Pipe Base Plate Designs 11/8/79                    All Power Reactor (Rev. 2) Using Concrete Expansion                          Facilities with an Bolts                                              OL or CP
Boron Loss From BWR Control Blades Loss of Non-Class-1-E
  79-26    Boron Loss From BWR        1l20/79                All BWR Power Reactor Control Blades                                    Facilities with an OL
Instrumentation and Con-trol Power System Bus During Operation Possible Malfunction of NAMCO Model EA180 Limit Switches at Elevated Temperatures Environmental Quali-fication of Class IE Equipment 1l20/79 11/30/79 127n9 All Power Reactor Facilities with an OL or CP 1/14/80 All Power Reactors with an OL except SEP Plants Operability of ADS Valve 1/14/80 Pneumatic Supply All OL BWRs with an Inadequate Quality Assurance for Nuclear Supplied Equipment Loss of Charcoal From Standard Type II, 2 Inch, Tray Adsorber Cells 1/21/80 All BWRs with an OL or CP 2/6/80 All Power Reactor Facilities with an OL or CP}}
  79-27    Loss of Non-Class-1-E    11/30/79                All Power Reactor Instrumentation and Con-                          Facilities with an OL
          trol Power System Bus                              and those nearing During Operation                                  Licensing (for Action)
                                                              All Power Reactor Facilities with a CP
                                                              (for Information).
  79-28    Possible Malfunction     127n9                    All Power Reactor of NAMCO Model EA180                               Facilities with an Limit Switches at                                 OL or CP
          Elevated Temperatures
  79-01B  Environmental Quali-     1/14/80                 All Power Reactors fication of Class IE                              with an OL except Equipment                                          SEP Plants
  80-01    Operability of ADS Valve 1/14/80                   All BWRs with an Pneumatic Supply                                  OL
  80-02    Inadequate Quality       1/21/80                 All BWRs with an Assurance for Nuclear                              OL or CP
          Supplied Equipment
  80-03    Loss of Charcoal From    2/6/80                   All Power Reactor Standard Type II, 2 Inch,                          Facilities with an Tray Adsorber Cells                                OL or CP}}


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Latest revision as of 01:53, 24 November 2019

NRC Generic Letter 1980-012, Transmittal of IE Bulletin 1980-004: Analysis of a PWR Main Steam Line Break with Continued Feedwater Addition
ML031350294
Person / Time
Issue date: 02/08/1980
From: Grier B
NRC Region 1
To:
References
BL-80-004 GL-80-012, NUDOCS 8002250445
Download: ML031350294 (6)


me c1FW74f4L-F"4r UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

631 PARK AVENUE

KING OF PRUSSIA, PENNSYLVANIA 19406 February 8, 1980

Docket Nos. 50-03

50-247 Consolidated Edison Company of New York, Inc.

ATTN: Mr. W. J. Cahill, Jr.

Vice President

4 Irving Place New York, New York 10003 Gentlemen:

The enclosed IE Bulletin No. 80-04, is forwarded for action. A written response is required. If you desire additional information regarding this matter, please contact this office.

Sincerely, j Boyce H. Grier C/- Director Enclosures:

1. IE Bulletin No. 80-04

2. List of Recently Issued IE Bulletins

CONTACT

0. L. Caphton

(215-337-5253)

cc w/encls:

L. 0. Brooks, Project Manager, IP Nuclear W. Monti, Manager - Nuclear Power Generation Department M. Shatkouski, Plant Manager J. M. Makepeace, Director, Technical Engineering W. D. Hamlin, Assistant to Resident Manager J. D. Block, Esquire, Executive Vice President - Administration Joyce P. Davis, Esquire

.7-

800,8,8,60 il-'116'

ENCLOSURE 1 UNITED STATES SSINS No.: 6820

NUCLEAR REGULATORY COMMISSION Accessions No.:

OFFICE OF INSPECTION AND ENFORCEMENT 7910250504 WASHINGTON, D.C. 20555 IE Bulletin No. 80-04 Date: February 8, 1980 ANALYSIS OF A PWR MAIN STEAM LINE BREAK WITH CONTINUED FEEDWATER ADDITION

Description of Circumstances

Virginia Electric and Power Co. submitted a report to the Nuclear Regulatory Commission dated September 7, 1979 that identified a deficiency in the original analysis of containment pressurization as a result of reanalysis of steam line break for North Anna Power Station, Units 3 and 4.

Stone and Webster Engineering Corporation performed a reanalysis of containment pressure following a main steam line break and determined that, if the auxiliary feedwater system continued to supply feedwater at runout conditions to the steam generator that had experienced the steam line break, containment design pressure would be exceeded in approximately 10 minutes. The long term blowdown of the water supplied under runout conditions by the auxiliary feedwater system had not been considered in the earlier analysis.

On October 1, 1979, the foregoing information was provided to all holders of operating licenses and construction permits in IE Information Notice No.

79-24. The Palisades facility did an accident analysis review pursuant to the information in the notice and discovered that with offsite power available, the condensate pumps would feed the affected generator at an excessive rate.

This excessive feed was not considered in the analysis for the steam line break accident.

On January 30, 1980, Maine Yankee Atomic Power Company informed the NRC of an error in the main steam line break analysis for the Maine Yankee plant.

During a review of the main steam line break analysis, for zero or low power at the end of core life, the licensee identified an incorrect postulation that the startup feedwater control valves would remain positioned "as is" during the transient. In reality, the startup feedwater control valves will ramp to

80% full open due to an override signal resulting from the low steam generator pressure reactor trip signal. Reanalysis of the event shows the opening of the startup valve and associated high feedwater addition to the affected steam generator would cause a rapid reactor cooldown and resultant return-to-power, a condition outside the plant design basis.

Actions to be Taken by the Licensee:

For all pressurized water power reactors with an operating license and those reactors listed in Attachment 1:

Enclosure 1 IE Bulletin No. 80-04 Date: February 8, 1980 1. Review the containment pressure response analysis to determine if the potential for containment overpressure for a main steam line break inside containment included the impact of runout flow from the auxiliary feedwater system and the impact of other'energy sources, such as continuation of feedwater or condensate flow. In your review, consider your ability to detect and isolate the damaged steam generator from these sources and the ability of the pumps to remain operable after extended operation at runout flow.

2. Review your analysis of the reactivity increase which results from a main steam line break inside or outside containment. This review should consider the reactor cooldown rate and the potential for the reactor to return to power with the'most reactive control rod in the fully withdrawn position. If your previous analysis did not consider all potential water sources (such as those listed in 1 above) and if the reactivity increase is greater than previous analysis indicated the report of this review should include:

a. The boundary conditions for the analysis, e.g., the end of life shutdown margin, the moderator temperature coefficient, power level and the net effect of the associated steam generator water inventory on the reactor system cooling, etc.,

b. The most restrictive single active failure in the safety injection system and the effect of that failure on delaying the delivery of high concentration boric acid solution to the reactor coolant system, c. The effect of extended water supply to the affected steam generator on the core criticality and return to power, d. The hot channel factors corresponding to the most reactive rod in the fully withdrawn position at the end of life, and the Minimum Departure from Nucleate Boiling Ratio (MDNBR)

values for the analyzed transient.

3. If the potential for containment overpressure exists or the reactor-re- turn-to-power response worsens, provide a proposed corrective action and a schedule for completion of the corrective action. If the unit is operating, provide a description of any interim action that will be taken until the proposed corrective action is completed.

4. Within 90 days of the date of this Bulletin, complete the review and evaluation required by this Bulletin and provide a written response describing your reviews and actions taken in response to each item.

Reports should be submitted to the Director of the appropriate NRC Regional Office and a copy should be forwarded to the NRC Office of Inspection and Enforcement, Division of Reactor Operations Inspection, Washington, D.C.

20555.

Enclosure 1 .IE Bulletin No. 80-04 Date: February 8, 1980 For boiling water reactors with an operating license or a construction permit and all pressurized water reactors with a construction permit, not listed in Attachment 1, this Bulletin is for information purposes only and no written response is required.

Approved by GAO, B180225 (R0072); clearance expires 7/31/80. Approval was given under a blanket clearance specifically for identified generic problems.

Attachment No. 1 to IE Bulletin No. 80-04 Plants with construction permits that are required to respond to the bulletin:

Diablo Canyon McGuire North Anna 2 Salem 2 Sequoyah If the permit holders have responded to earlier requests from the NRC on some of the items presented in the bulletin, they may respond to the bulletin by reference to the response to the earlier request.

-

ENCLOSURE 2 IE Bulletin No. 80-04 Date: February 8, 1980 RECENTLY ISSUED IE BULLETINS

Bulletin Subject Date Issued Issued To No.

79-25 Failures of Westinghouse 11/2/79 All Power Reactor BFD Relays in Safety- Facilities with an Related Systems Operating License (OL)

or Construction Permit (CP) (for Action)

79-02 Pipe Base Plate Designs 11/8/79 All Power Reactor (Rev. 2) Using Concrete Expansion Facilities with an Bolts OL or CP

79-26 Boron Loss From BWR 1l20/79 All BWR Power Reactor Control Blades Facilities with an OL

79-27 Loss of Non-Class-1-E 11/30/79 All Power Reactor Instrumentation and Con- Facilities with an OL

trol Power System Bus and those nearing During Operation Licensing (for Action)

All Power Reactor Facilities with a CP

(for Information).

79-28 Possible Malfunction 127n9 All Power Reactor of NAMCO Model EA180 Facilities with an Limit Switches at OL or CP

Elevated Temperatures79-01B Environmental Quali- 1/14/80 All Power Reactors fication of Class IE with an OL except Equipment SEP Plants

80-01 Operability of ADS Valve 1/14/80 All BWRs with an Pneumatic Supply OL

80-02 Inadequate Quality 1/21/80 All BWRs with an Assurance for Nuclear OL or CP

Supplied Equipment

80-03 Loss of Charcoal From 2/6/80 All Power Reactor Standard Type II, 2 Inch, Facilities with an Tray Adsorber Cells OL or CP

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